National Productivity Summit-IMTMA 19 · 2019-08-26 · JH PM QM DM OTPM E&T SHE RGET CORPORATE...
Transcript of National Productivity Summit-IMTMA 19 · 2019-08-26 · JH PM QM DM OTPM E&T SHE RGET CORPORATE...
National Productivity Summit-IMTMA 19
Carborundum Universal- Murugappa Group
Chennai
SLIDE NO : 1
INR 295 Billion Conglomerate One of the largest family promoted, professionally managed, diversified business groups…
Murugappa Group
Founded in 1900 and headquartered in
Chennai.
28 businesses
50,000 employees
Group Head Office
SLIDE NO : 2
Abrasives product portfolio
SLIDE NO : 3
Capacity Augmentation in Organic Product Line
Concept - OSKKK Methodology
with the support of KK Pillar TPM Approach.
The Team
KM Natarajan – Associate Vice President - Operations
E. Karthick –Assistant General Manager – Organic Module Head
B. Raghavendra – Project Engineering Group
SLIDE NO : 4
Background • Average Opportunity Loss of 5 to 6 Cr/month
• High Demand for these Products in the Market
• Loss of Business leads to Competitor Gain
Aim To Increase our Market Share with short lead time
APPROACH TO STRATEGIC TPMCorporate Vision
Corporate Mission
SWOT Analysis
CORE
VALUES
Strategy
Key Business Indices
Key Management Indices
Key Performance Indices
Key Activity Indices
Balance
Score Card
PQCDSME
CIRCLE
TARGET
KK
JH
PM
QM
DM
OTPM
E&T
SHE PIL
LA
R T
AR
GE
T
CORPORATE
LEVEL
PLANT
LEVEL
SLIDE NO : 5
Cross SWOT
Analysis
Strategy
To use
our internal
strengths to take
advantage of the
existing
external
opportunities
To use the
external
opportunities to
overcome the
internal weaknesses
experiencing
Strategy
To take advantage of
our strengths
to avoid or mitigate
real and potential
external threats
Strategy
To minimize our
internal weaknesses
and avoid
external threats
Strategy
SLIDE NO : 6
Strategy :
Capacity augmentation – Strategy
Investments
Machine flexibility, Semi Automation of
process
Level 2 Matrix KMI-KPI Linkage
SLIDE NO : 7
10 Step JIPM Methodology of KK Pillar
Select Model Equipment line and process
Organize Project Team
Understand present losses
Set Improvement themes and target
Draft Improvement Plan
Perform analysis and evaluate countermeasures
Implement Improvement
Confirm Results
Take measures to prevent recurrence
Horizontal Replication
SLIDE NO : 8
SLIDE NO : 9
Step 1 - Select Model Equipment Line- Makigami
Makigami analysis technique is a structured approach to
detect all the losses that are occurring in the flow of an
activity.
It captures all the sub activities of a process in depth.
Analysis is done for identifying the non value added
activities or losses and action taken to solve them.
7 Type of Lossess –
Value/Process/Accuracy/Speed/Idle/Cost/Communication
O – Observe CloselyProcess, working Methodology, Material Flow,
Material handling methods
K- Kaizen the Equipment Decide parts requirement Fix WIP, FG, RM Stock
Process Flow CSM and FSM
Equipment Selection Simulate &verify options
Information Flow Implement Change
OSKKK - METHODOLOGY
S- Standardize the WorkStandardize work combination table,
Standardize operation sheet
Production capacity sheet
Work Chart
Element instruction Sheet
K- Kaizen the flowSingle Piece Flow / Fifo
Sequential Pull
Supermarket
Batch Processing
K- Kaizen the manKaizen for Cycle time of Operators
O
S
KF
KE
KM
Representation
Select Model Equipment line – Organic products
33254 3456436756
29560
36750
1002 1152 1213 837 9370
5000
10000
15000
20000
25000
30000
35000
40000
Oct-18 Nov-18 Dec-18 Jan-19 Feb-19
Qty produced
Snagging Precision
Mass Production – Snagging wheels
Specialty items – Precision wheels
Team Formation- Pillars involved- KK,PM,SHE and Moulds
SLIDE NO : 11
O – Observe Closely
O
S
KF
KE
KM
Understand Present Losses
Man Related Loss Data Collection & Analysis
SLIDE NO : 12
Loss
No.
Loss
DescriptionJIPM Loss Definition CUMI - Loss Interpretation
9Management
Loss
Waiting losses that are caused by management such
as waiting for materials, waiting for a dolly, waiting for
tools, waiting for instructions etc.
Stoppage or idling of machine due to want of Raw
Materials / Manpower / Tools / Moulds / Trays / Stands /
Trolleys etc. Also, due to power cuts / waiting for decision
/ want of production booklets / want of drawings / waiting
for inspection / excess time
10 Motion LossMan-hour losses arising from differences in skills
invloved in etc.
Man hour losses due to skill difference between
operatives
11Line organisation
Loss
Idle time losses when waiting for multiple processes or
multiple platforms
Idle time losses when waiting for multiple processes.
Example : 1 operative working on 2 or 3 machines
12 Distribution LossDistribution man-hour losses due to transport of
materials, products (processed products) and dollies.
Man-hour losses due to movement of rawmaterial /
products / stands / trolleys etc. from one place to another
13Measurement &
Adjustment Loss
Work losses from frequent measurement and
adjustment in order to prevent the occurrence and
outflow of quality defects
Stoppage losses for adjusting the machine settings /
parameters to prevent quality defects. Example :
Finetuning of settings like template, weighing hopper
vibrator, plunger in auto presses, Program correction in
CNC machines, etc.
Losses that impedes human work
efficiency
16534 min
Mgt. Loss
390 mins
Motion
Loss
135 mins
Line Org.
Loss
L-11
14256 mins
Distribution
Loss
L-12
1782 mins
Measure & Adj.
496 mins
O
S
KF
KE
KM
Understand Present Losses – VSM
Overall Flow
SLIDE NO : 13
O
S
KF
KE
KM
Understand Present Losses – VSM
Finishing Operations
SLIDE NO : 14
O
S
KF
KE
KM
Understand Present Losses - VTR Analysis
SLIDE NO : 15
O
S
KF
KE
KM
VTR Analysis – NVA Graphical representation
SLIDE NO : 16
O
S
KF
KE
KM
Spaghetti Analysis – Material Flow
SLIDE NO : 17
O
S
KF
KE
KM
SLIDE NO : 18
VSM
• Bottleneck Stage identified
VTR• VA , NVA
Identified
Spaghetti Analysis
• Zig Zag movements Identified
O
S
KF
KE
KM
Observe – Key Learnings - Summary
Set Improvement themes and Target
TAKT Time Calculation
Customer Demand
8035 997713035
10546
0
10000
20000
Nov-18 Dec-18 Jan-19 Feb-19
Customer Demand
Demand
48
118
76
38
1122
70
0
20
40
60
80
100
120
140
Time(sec)
Line Balancing
SLIDE NO : 19
O
S
KF
KE
KM
Glenday sieve Analysis
Symbol Machine/Process
A Boring Machine
B Bore Painting
C ID/OD Horizontal
D Discing
E Balancing
F Inspection and
Packing
G Alex R50
H ID/OD Vertical
I Conical edger
J CNC Machine
K Precision Packing
SLIDE NO : 20
Glenday sieve Analysis :
• Max Number of Products should travel less distance
• Use of Pareto chart in identifying Runners , Repeaters
etc.O
S
KF
KE
KM
SLIDE NO : 21
Customer Demand
• Predicting customer demand
TAKT Time • Line Balancing
Glenday Sieve
Analysis
• Identifying Runners , repeaters
O
S
KF
KE
KM
Standardization – Key Learnings - Summary
Simulation ---- Snap Shot
O
S
KF
KE
KM
Simulation and Implementation of new layout
Simulation Study using Jenga Blocks
Before After
SLIDE NO : 23
O
S
KF
KE
KM
KK Matrix
S.L.No
Loss/Activity Pa
inti
ng
Sta
nd
Air
co
oli
ng
Syst
em
Sp
ray g
un
Fla
t ta
ble
s
lab
el
pri
nti
ng
ma
ch
ine
Ro
lle
r ta
ble
s
Co
mb
inin
g o
f a
cti
vit
ies
Ru
bb
er
she
ets
Sh
ifti
ng
of
ove
ns
Ho
ist
for
ove
ns
Se
qu
en
cin
g o
f m
ach
ine
s
Ne
w g
an
gw
ay
Du
st c
oll
ecti
on
syst
em
To
tal
1 To eliminate fatigue in painting process 1 1 1 3
2 To eliminate process deviation in painting 1 1
3 To eliminate bending activity in stenciling 1 1 1 3
4 To reduce time taking for labeling process 1 1 1 3
5 To eliminate waiting time spent on getting printed labels 1 1
6 To eliminate lifting of the wheels 1 1 2
7 To eliminate line organization losses 2 2
8 To eliminate unncessary movement of wheels 1 1 2
9 To eliminate chip loss 3 3
10 To decrease the distance travelled by wheels 3 1 7 1 12
11 To remove dust from machines 5 5
12 Total KAIZENS 1 1 1 4 1 3 2 6 3 2 7 1 5 37
Improvements
SLIDE NO : 24
O
S
KF
KE
KM
CUMI
YM Test
Painting & Stenciling
Labelling
Balancing
Packingdistance =15m
Time = 10mins
SLIDE NO : 25
K- Kaizen the flow – single piece flow
distance =32m
Time = 270mins
Before After
Before After
SLIDE NO : 26
Cost of Implementation
Shifting of Machines
and ovens-2 lakh
Roller tables -
1.2 lakhs
Duct Engineering
1.2 lakh
Printing m/c- 2 lakhs
K- Kaizen the flow – unidirectional material Flow
O
S
KF
KE
KM
SLIDE NO : 27
Layout Simulation
• Using paper and Jenga blocks
Single Piece Flow
• Creating FIFO by continuous improvements
Kaizens
• Implementing 3 days continuous improvements
O
S
KF
KE
KM
Kaizen the Flow – Key Learnings - Summary
Press OCC
Time
(min
)
Min/
Occ %
Press
type
1000T 33 495 15 5% Manual
100T 12 60 5 1% Manual
1500T 352 6125 17 57% Manual
600T 164 1640 10 15% Manual
BRP 9 252 28 2%
Semi-
Auto
POGGI 3 2142 714 21% Auto
Grand
Total 574 10714 Manual
Setup & Adjustment Loss - Stratification
Moulding Machines - Stratification
Mixing 10%
Moulding 65%
Curing 10%
Finishing 15%
SLIDE NO : 28
K- Kaizen the Equipment - Machine
O
S
KF
KE
KM
Product
Category Capability
300
diameter Yes
400
diameter Challenged
450
diameter Challenged
Automatic Moulding Press
SLIDE NO : 2940
O
S
KF
KE
KM
Auto Press Press – ComponentsInvolved in Changeover activity
SLIDE NO : 30
O
S
KF
KE
KM
Setup & Adjustment Loss – VTR Study
Type Cate S. No. Activity
Time
Duration(
Sec)
VA NVA Internal External E C R SProposed
Duration
Bottom Plate Removing 1 Ejecting the bottom plate 120 VA Y S 120
Bottom Plate Removing 2 Place the steel rod inbetween barrel & bottom plate 60 NVA Y E 0
Bottom Plate Removing 3 Indexing 10 VA Y S 10
Bottom Plate Removing 4 Lift the bottom plate manually 120 VA Y S 0
Bottom Plate Removing 5 Place the Bottom Plate on the Stand 30 VA Y S 0
Ejection rod Removing 6 Removing the Ejection Rod from the Bottom plate - 3 Nos. 240 VA Y E 0
Pin Removing 7 Removing the Tefflon Sheet 30 VA Y S 30
Pin Removing 8 Removing the centre bolt by Ratchat 60 VA Y S 60
Pin Removing 9 Remove the pin manually 30 VA Y E 0
Pin Removing 10 Place the Pin on the Stand 30 VA Y E 0
Barrel Removing 11 Searching for Spanner 600 NVA Y E 0
Barrel Removing 12 Outer Ring 12 Bolts Removing 400 VA Y S 180
Barrel Removing 13 Lift the outer ring manually 60 VA Y S 60
Barrel Removing 14 Eye bolt fixing - 1 80 VA Y E 0
Barrel Removing 15 Searching for Rope 300 NVA E 0
Barrel Removing 16 Roping the eyebolt 120 VA Y E 0
Barrel Removing 17 Stakker positioning - 1 120 NVA Y E 0
Barrel Removing 18 Lift the barrel - 1 180 VA Y S 60
Barrel Removing 19 Place the Barrel on Stand 30 VA Y S 30
Barrel Removing 20 Removing the Eye Bolt 80 VA Y E 0
Pin Locating BushRemoving 21 Removing Using Spanner 300 VA Y E 0
Bottom plate Fixing 230 Removing the Steel piece , locating the bottom plate 180 VA Y E 0
Trial Adjust 231 Mix Charging 300 VA Y C 0
Trial Adjust 232Enter the Mix Weight, Ring Ht Setting, Wheel Thickness
Setting 300 VA Y S 120
Trial Adjust 233 Trial Run 400 VA Y S 150
Trial Adjust 2341st good piece output from the machine after set-up change 1200 VA Y S 1200
Present time – 714 min Target time – 60 min
SLIDE NO : 31
O
S
KF
KE
KM
Setup & Adjustment Loss - Approach
Do Video Tape Recording
Value Added
activity
Classify activities
Non Value Added
activity
714
min
486
min
Eliminate
228
min
Activity
Time
Duration
(min)
Corrective measure
Forklift usage for removng, fixing, adjusting the setup 90 Push Pull trolley
Eye bolt usage for handling setup 109 Push Pull trolley
Steel rod uasge for removing Bottom plate 14 vaccum lifter
Searching for tools 15 Tool board fixed near machine
SLIDE NO : 32
O
S
KF
KE
KM
Setup & Adjustment Loss - Approach
Value Added Activity
External Activities Internal activities
Combine Assembled set
486
min
435
min
52
min
35
min
17
min
Activity
Time
Duration
(min)
Corrective measure
C Cleaning bottom plate 17 Made ready for the next size
S Removing & fixing Ejection rod 35 Permanently fixed with ejection piston rod
SLIDE NO : 33
O
S
KF
KE
KM
Setup & Adjustment Loss - Approach
Value Added Activity
Internal activities
Eliminate Combine Rearrange Simplify
156
min
338
min
0
96
min
SLIDE NO : 34
435
min
486
min
O
S
KF
KE
KM
Top Plunger Adapter Combined with RAM
SLIDE NO : 35
INTERNAL – COMBINE
O
S
KF
KE
KM
SLIDE NO : 36
O
S
KF
KE
KM
Results – Machine Efficiency
In Machine related losses setup and Adjustment losses were high.
To Enhance flexibility of manufacturing and Quick change over to various sizes of snagging
wheel using new concept of QCD – Telescopic mould in Auto Press
As per pattern production, the manufacturing starts from 300 dia to 450 mm dia.
Setup / Tool change over time takes 16 hrs from setup to other setup (300 –
450 takes 16 hrs.)
Curtail the supplies of various dia of snagging wheel to the market.
Product mix not as per the market demand.
SLIDE NO : 37
K- Kaizen the Equipment - Mould
O
S
KF
KE
KM
Reducing Setup changeover time
SLIDE NO : 38
O
S
KF
KE
KM
New Moulds design- Machine load carrying capacity
779.8
1050.8
795.2
0
200
400
600
800
1000
1200
Dia 450 setup Dia 400 Setup Dia 300 Setup
Wei
ght
in K
gs
Moulds Dia wise setup weight
1377.3
0
200
400
600
800
1000
1200
1400
1600
Dia 450 setup Dia 400 & 300 Setup
We
igh
t in
Kgs
Combined Mould setup weight
779.8
18
O
S
KF
KE
KM
As per manufacture machine design load carrying capacity should be 1500Kg .
Mail From Machine supplier about
their Design Limitation
Setup & Adjustment Loss –KK Matrix
IMPROVEMENTS
LOSS / ACTIVITY
1 Tools Searching 4 4
2 Assembling on floor 5 3 8
3 Mould setup lifting/pulling 2 2 2 6
4 Plunger/Adapter dismantling & fitting 1 3 5 9
5 Bottom plate removal & fixing 6 6
6 Racker & levelling plate removal & fixing 3 3
7 Wheel unloading vaccum pad removal & fixing 3 3
8 Barrel Holding rings unfastening & fastening 6 6
9 Material charging 4 4
Total 5 8 2 3 8 6 8 3 2 4 49
Eje
cti
on
un
it
mo
dif
icati
on
Setu
p h
old
ing
un
it
rin
gs m
od
ifia
tio
n
TO
TA
L
Wh
eel u
nlo
ad
ing
un
it
mo
dif
icati
on
Recip
e c
han
ge
acti
vit
y
Cen
tre p
in
mo
dif
icati
onSL.NO
To
olin
g k
it p
rovis
ion
Assem
bly
tab
le
pro
vis
ion
Racker
arm
un
it
mo
dif
icati
on
Plu
ng
er
ho
lder
un
it
mo
dif
icati
on
Mo
uld
co
mp
on
en
ts
han
dlin
g e
qu
ipm
en
t
O
S
KF
KE
KM
SLIDE NO : 40
SLIDE NO : 41
Implementation of new Mould design
The effectiveness of improvements.
Setup time reduction to 3hrs.
changeover – 5 occurrence to 8 occurrence
/ month
Fatigue reduction by eliminating removal of
moulds during changeover.
O
S
KF
KE
KM
No of Activities Before & After
Gradual decrease in diameter
90
°
45
°
Angular connection
Different duct
diameters
Gradual decrease in
diameters
SLIDE NO : 42
Machine Before After
CNC Machine 6.7mps 10.3mps
ID/OD Vertical
Machine
7.1mps 18.9mps
ID/OD Horizontal
Machine
7.5mps 13.3mps
Alex R50 5.7mps 12.3mps
Conical Edger 3.7mps 7.2mps
Dry Disc Machine 5.7mps 8.7mps
Boring Machine 7.5mps 14.3mps
Suction Velocity
Kaizen the Equipment - Duct
O
S
KF
KE
KM
SLIDE NO : 43
Mould• Telescopic
Moulding
Molding machine
• Reducing setup change over time
Duct Engineering
• Increasing suction velocity by reengineering
O
S
KF
KE
KM
Kaizen the Equipment – Key Learnings - Summary
44
Snagging Finishing line
Negligible risk
15
Low risk
22
Medium risk
16
High risk
12
Very high risk
2
Total – 67
activities
Kaizen the Man
O
S
KF
KE
KM
45
Kaizen the Man
O
S
KF
KE
KM
46
Snagging Finishing line
Negligible risk
15
26
Low risk
22
25
Medium risk
16
16
High risk
12
0
Very high risk
2
0
Before
After
Kaizen the Man
O
S
KF
KE
KM
SLIDE NO : 47
Ergonomics• Improving work
conditions
REBA Study
• Implemented Kaizens to eliminate high risk activities
Training
• Training for new way of doing work.
O
S
KF
KE
KM
Kaizen the Man – Key Learnings - Summary
Results- Overall
Productivity
Delivery
Quality
SLIDE NO : 48
Before Target After
Deliverytime(mins)
270 8 15
0
50
100
150
200
250
300
Qua
ntity
/shift
Delivery time(mins)
BETTER
Results- Overall
Before Target After
Distancetravelled
638 282 282
0
100
200
300
400
500
600
700
Dis
tance /m
onth
Distance travelled
BETTER
Before Target After
Lead time inFinishing
3 1 1
0
0.5
1
1.5
2
2.5
3
3.5
Da
ys
Lead time in Finishing
BETTER
SLIDE NO : 49
Business
captured over 3
months- 8Cr
Losses reduced by duct engineering.
Optimum/desired velocity achieved at
hood/duct.
Suction velocity increased at hood.
3 unit dust collectors eliminated
There by saving energy 30 HP motor
Space saving 3000 Sq. feet
Environmental Impact
Machine Before After
CNC Machine 6.7mps 10.3mps
ID/OD Vertical
Machine
7.1mps 18.9mps
ID/OD Horizontal
Machine
7.5mps 13.3mps
Alex R50 5.7mps 12.3mps
Conical Edger 3.7mps 7.2mps
Dry Disc Machine 5.7mps 8.7mps
Boring Machine 7.5mps 14.3mps
SLIDE NO : 50
Scope for Horizontal Deployment
Horizontal deployment Internal and External Plants
Capex Cleared for Russia and Hosur Plant based on these
Concepts for newer Lines
Any other merits
• Due to Space Creation – New Building for Precision Grinding
was whipped off to a tune of 2 Crs.
• The initial investment of 7cr for the new machine has been
stopped after getting the result of this project.
SLIDE NO : 51
SLIDE NO : 52
Life is Short,
Time is Fast,
No Replay,
No Rewind,
So Enjoy Every
moment
As it Comes
If you are not making mistakes, you are not experimenting