Milford Haven Bridge Collapse Cathal Kennedy Terence Meade Sara Farivarz Padraig O’Rourke.
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Transcript of Milford Haven Bridge Collapse Cathal Kennedy Terence Meade Sara Farivarz Padraig O’Rourke.
Milford Haven Bridge Milford Haven Bridge CollapseCollapseCathal KennedyCathal KennedyTerence MeadeTerence MeadeSara FarivarzSara Farivarz
Padraig O’RourkePadraig O’Rourke
ContentsContents
IntroductionIntroduction Milford Haven Milford Haven
BridgeBridge The CollapseThe Collapse ResultsResults ConclusionConclusion
IntroductionIntroduction
Box Girders:Box Girders:
used for large 2used for large 2ndnd moment of area & moment of area & torsional resistancetorsional resistance
Hard to analyse, Hard to analyse, howeverhowever
One of 4 similar One of 4 similar bridges that failed bridges that failed from 1969 - 1971 from 1969 - 1971
Milford Haven BridgeMilford Haven Bridge
Box Girder designBox Girder design Consisted of 7 separate spans from Consisted of 7 separate spans from
77m to 312m in length77m to 312m in length Built by being cantilevered out from Built by being cantilevered out from
pierspiers Sections then welded or bolted to Sections then welded or bolted to
endend
The CollapseThe Collapse
Occurred when Occurred when launching deck launching deck section acrosssection across
Stresses during Stresses during construction are construction are very different and very different and often larger than often larger than when the bridge is when the bridge is completedcompleted
ContinuedContinued occurred during occurred during
launching a pre-launching a pre-assembled deck assembled deck section towards the section towards the second pier.second pier.
subjected tosubjected to bending bending moments and vertical moments and vertical shear forces.shear forces.
buckling of diaphragm buckling of diaphragm lead to buckling of lead to buckling of lower flange.lower flange.
Load before failure Load before failure 9700kN9700kN
ResultsResults
Committee of Inquiry concluded that Committee of Inquiry concluded that BS153 was inadequateBS153 was inadequate
Merrison committee sets rules which Merrison committee sets rules which become the basis for BS5400become the basis for BS5400
West Gate Bridge strengthened but West Gate Bridge strengthened but collapsed 2 months after killing 32.collapsed 2 months after killing 32.
ConclusionConclusion
Ultimately caused Ultimately caused by human error – by human error – failure to anticipate failure to anticipate effects during effects during constructionconstruction
Highlights need for Highlights need for engineers to fully engineers to fully understand understand principles behind principles behind constructionconstruction