Martin Brown GE19 Bridge Displacement Director, Health, Safety and Environment London Rail.
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Transcript of Martin Brown GE19 Bridge Displacement Director, Health, Safety and Environment London Rail.
Martin BrownGE19 Bridge Displacement
Director, Health, Safety and Environment
London Rail
Outline
• Some Background• GE 19 and the incident • Why it occurred• Lessons for Design, Construction and
Constructability and Site monitoring• Some conclusions and suggested next steps
East London Railway Extension
The East London Line Extension, connects the old London Underground East London Line (running from New Cross to Shoreditch, including Marc Brunel’s Thames Tunnel), part of the existing suburban line to Crystal Palace and Croydon, and some new Infrastructure. Phase 2 is a proposal to link to Clapham Junction
GE19
Bridge GE19
• Bridge set at 1:30 gradient, falling from west to east
• Situated near the Broadgate Tower, near to the Liverpool Street Station throat
Bridge GE19 : Plan View
• Set at 60 degrees to the Great Eastern Main Line, which is a six track • Lying almost due West to East
GE19 in numbers
• Spans 84 metres, with 8 metres deep truss• Made from steel weighing 812 tonnes• Bridge decked out with 417 Omnia planks,
each weighing approximately 100k • Approximately 500 tonnes of concrete was
cast as counterweight (45% of total length) pre-launch, at the East end
• The bridge sits on four bearings
What Occurred• Launch successfully completed during a possession
weekend 3 – 5th May 2008, landing within 1 mm of design• Between 5th and 21st May preparation and lowering work
was undertaken• Mid-May it was realised the bridge had moved, and needed
to be plan jacked approximately 38 mm (East to West), against lateral restraints
• Thermal expansion was about 20mm during day• With the plan jack completed, final lowering was scheduled
to be completed on 29th – 30th May• On 28th May, at 19.15, Bridge dropped 200mm at East End
onto the permanent bearing
Bearings Layout• At launch, the base of the
bridge was 650mm above the East bearing, and 400mm above the West
• The bridge sat on steel plates on top of the final bearings
• The bearing set up, provides constrained movement as shown. The West end is fixed
• The bearing have transport restraints
• The bearings have smooth finish stainless steel contact surfaces
Movement is fixed
Lateral movement North-South
Longtitudinal movement East-West
Free movement
500 tonne Hydraulic Jack,
with security collars
Top cap of abutment
Permanent bearing
Lower Member of Bridge GE19
Temporary spacer plates
Temporary PTFE
Covered plates
3 degree temporary
wedge
Note the inclination of the bridge has been enhanced for clarity
Some load assumptions
• The load on the eastern end bearings was about 450 tonnes• With the slope about 3.5 degrees, simple assumptions give a
resolved horizontal down slope load of about 18 tonnes• Again with some assumptions, the breakout friction at the PTFE
plate would be 3% to 4%, giving a stable position over some time • Cooling temperature change could lead to movement of 2 to 3 mm,
converting static to dynamic levels• Dynamic friction would be 1% or less• The transit bolts would have provided maybe 2 tonnes each• However once movement began, the spacers would begin to be
squeezed out, and the transit bolts bent. This is what we think happened
Omnia Planks
Note this plank shows signs of damage from the bridge displacement
Note the lacing in both directions tosecure the planks in position,
fitted post incident
Omnia planks issues• The Omnia planks were held in place by ‘contraband’
tape, with a filler material in the gaps between planks• Shear pins were fitted between the planks, to take up the
loads when concreted• The planks were not laced, following a value engineering
and pre-launch review. There was no secondary means of preventing the planks dropping onto the live railway
• When the bridge was displaced the planks were subject to a significant movement in some places; 5 fell onto the track, and several others were dislodged
• The method was based on previous successful installations
Bridge drops (causing disruption of service)
PTFE pad inserted in the wrong position
Inadequate understanding of risks
by supervision
Unsecured Omnia planks falls onto track
Risk assessment discounted possibility
of planks falling
Risks not adequately identified and analysed in assessment
MS short time change procedure not
followed
Design of temporary works does not
consider realignment during jack down
Unexpected movement down
slope dislodges plates
Initiating Event
Immediate cause
Contributory Causes
Root Causes
GE19 Bridge Incident – Root cause map
No secondary means of securing planks
Temporary support bearings fail
Unsecured planks dislodged by
movement of Bridge
Design did not fully encompass the
practicability of the temporary works for lowering the bridge
Cumulative design checks reinforce expected success of
planned works, hence reducing perceived risks
Inadequate dynamic risk assessment
undertaken
Wrong instruction given
No written instructions in place or suitable
briefing
Method statement requiring interlacing
was discounted
Inadequate controls over change of
methods
Deviation from method
Statement
No evidence of explicit standards and procedures in place for management of temporary works
Once launch complete there was a reduced focus on the lowering and temporary works
controls
Lessons from the Displacementof the Bridge
• Design of the Temporary Works• Lack of explicit standard or work instruction for
placement of the PTFE• Reduced focus, once launch was complete• Design of bridge did not fully encompass
constructability of all elements• Failure to understand the high consequence/ low
probability risks involved
High load sliding elastomeric bearings have been specified for concrete box girders.Preformed fabric is bonded to a steel plate that is recessed to receive a PTFE sliding surface.The top is stainless steel on a steel backing plate. Anchorage to the upper and lower concretesurfaces is with end welded studs. Under these conditions, the following controls arerecommended:
♦ The preformed fabric should be 2.0 in. thick. ♦ The average bearing pressure on the preformed fabric due to dead load and live
loadwithout impact should not exceed 2,000 psi.
♦ The average bearing pressure on the PTFE surface should not exceed 3,000 psi. ♦ Top and bottom surfaces should be level. Concrete or epoxy grout should be cast
against the in-place bearing.
Bridge Design ManualDecember 2001© by Texas Department of Transportation(512)
Conclusions
• These circumstances were (as far as we can tell) unique• If our analysis is right, the potential for failure had not
been fully considered before, why was this ? • Once explained, everyone felt the risks were obvious. If
our analysis is wrong what did happen ?• The management of the design, in parcels of work, may
have assisted in the lack of design integration• Greater use should be made to ‘what if’ analysis where
high potential risk exists, especially where there can be further consequential risk
Next Steps• If we are right, we need to change the guidance on how,
where (and when) PTFE plates are used in structures
• For those who ‘sit behind the desk’ planning and designing, we need to ensure production of the information for ‘those on the tools’ to act correctly, this is an educational issue
• We need to reinforce an approach that questions design at a fundamental level, looking at the ‘what if’. This is also an educational issue
• We need to understand more how Human Factors impact on undertaking fundamental and proactive analysis, design checking and site inspection, this may be a research issue
Questions to :[email protected]
Full Report can be found at :
http://www.tfl.gov.uk/corporate/projectsandschemes/networkandservices/eastlondonrailway/2111.aspx
orhttp://www.tfl.gov.uk/assets/downloads/GE19-Incident-Main-
Report.pdf