Management Presentation V2

16
Jamie Hopkins Swansea University Year In Industry Review

Transcript of Management Presentation V2

Page 2: Management Presentation V2

Agenda• Projects Overview

Fuel Stock & Thermal Performance Manual & LP Development

Station Efficiency Losses Oil Optimisation Air Heaters Performance Analysis Works Power Analysis HP Heater Replacement Validity Biomass Throughput Tracking Additional Tasks

• Personal Development At Aberthaw• Further Questions

Page 3: Management Presentation V2

Fuel Stock & Thermal Performance Accounting

• Response to failing to close off monthly heat account

• Heat account run by one source• No procedure for heat accounting• Trailed and tested• EUETS support• Deliverables;

Document of manualsLocal procedure

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Fuel Stock & Thermal Performance Accounting

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Station Efficiency Analysis• Already evaluating of CPI losses and TEMP raw data

• Administrating heat account• Quantify losses• Required;

TEMP losses reportAnalysis tool

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0100000200000300000400000500000

Station

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GJ

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Station Efficiency Analysis

M01W01

M01W04

M02W03

M03W02

M04W01

M04W04

M05W03

M06W

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Unit Leakage

Unit 7Unit 8Unit 9

GJ

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M08W1

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M08W4

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M09W3

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M10W2

2015

M11W1

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M11W4

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M12W3

2016

M01W2

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M02W1

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Unit Leakage

Unit 7Unit 8Unit 9

GJ

• Improvement demonstration.

• Actions from losses• Surveys (on/off load)• Reduction in water

leakage as an example.

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Oil Optimisation• Over usage on starts identified• On-load usage analysed to asses opportunity for tech

data changes• Target areas for further reductions

• U7 & 9 ashing• U8 PF temps• Established tech data

change

2016

M01

2016

M02

2016

M03

2016

M04

2016

M05

2016

M06

2016

M070.00%0.20%0.40%0.60%0.80%1.00%1.20%1.40%1.60%1.80%

Station Oil Usage

Station Oil UseTarget Onload Usage

Fire Change

Furnace Stability

Low Mill Temps

Ashing Load Support

Other0.0%5.0%

10.0%15.0%20.0%25.0%30.0%35.0%40.0%45.0%50.0%

Percentage Of Total Oil Burn

Unit 7Unit 8Unit 9

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Oil Optimisation• Temperature difference analysis carried out on unit 9• No real value in pursuing• Identification of further work• Revisit post Hi-Vol

 

Average Temp. Diff.

CA Mill 2B Mill 2C Mill 3D Mill 3E Mill 5F Mill 5

Overall Average 3

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Energy World Air Heater Performance

• Instrumentation route not viable• Testing strategy was reactive not

proactive• Requiring pre planned programme

10/25

/2002

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/2003

10/25

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/2005

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10/25

/2015

0.0%

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40.0%

60.0%

80.0%

100.0%

120.0%

140.0%

Mill A/H A LeakageMill A/H B LeakageMain A/H A LeakageMain A/H B LeakageNormal MainNormal MillRepair MainRepair Mill

Lea

kage

(% O

2)

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Energy World Air Heater Performance

• Weekly monitoring; o Cold side efficiencyo Hot air to mills o Main air heater outlet temperatureo Mill and main air heater diff. pressureso FD, ID & PA fan amps

Air Heater Ingress Assessment

Boiler Air Ingress

Assessment

Air Heater Leakage

Assessment

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Imported Works Power• Assessment of station usage against business

plan

• 2016 consumption 11.7 MW

• FGD matrix control to be assessed

• 0.5 MW worth ~£600k[1] [2]

[1] Based on current works power prices of £35/MWh[2] Using 2017 – 2023 business plan running

1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 25 26 27 280.0

5.0

10.0

15.0

20.0

25.0 Adjusted Works Power Usage 2016

Adjusted Total Works Power (MW) Adjusted TX 3 & 4 Usage (MW)FGD Usage (MW) Target (MW)

TEMP Week

MW

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HP Heater Replacement Validity• Stations most common reliability issue• 2016 losses estimated at £300k• Approx. £800k losses from 2017 to 2023• Approx. £3.6 million for units heater replacement

  2017 2018 2019 2020 2021 2022 2023

Efficiency (£)Unit 7 £34,000 £38,000 £42,000 £7,000 £7,000 £7,000 £8,000Unit 8 £32,000 £32,000 £35,000 £6,000 £6,000 £6,000 £7,000Unit 9 £32,000 £36,000 £39,000 £6,000 £6,000 £7,000 £7,000

Reliability Cost (£)

Unit 7 £36,000 £40,000 £45,000 £7,000 £8,000 £8,000 £8,000Unit 8 £30,000 £23,000 £37,000 £6,000 £6,000 £6,000 £7,000Unit 9 £33,000 £28,000 £41,000 £6,000 £7,000 £7,000 £8,000

Total Annual Cost Station £197,000 £197,000 £239,000 £38,000 £40,000 £41,000 £45,000

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Biomass Throughput Tracking

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0.0%10.0%20.0%30.0%40.0%50.0%60.0%70.0%80.0%90.0%100.0%

Actual Burn Target Burn % Of Target Burn

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0.0%10.0%20.0%30.0%40.0%50.0%60.0%70.0%80.0%90.0%100.0%

Actual Burn Target Burn % Of Target Burn

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• Budget constraints overtaken progression• Fuel availability issues going forward

Phase 1

Phase 2

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Additional Tasks• TEMP data QA tool• Quarterly & annual weighbridge report.• Taking meeting minutes (Combustion CIG,

P&C Bi Weekly)• Damper checks (BSOD’s, SAD’s, TAD’s etc.)• Air heater cross leakage• Unit water leakage• Flowrate’s (CW to quick starts)• Unit 9 low NOx commissioning• 1 month secondment to operations• 2 weeks at Pembroke

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My Personal Development At Aberthaw• Confidence & character building• Development of safety awareness• Improvement in presentation skills• Enhancement in computational skills• Exposure to commercial operations • Integration into problem solving

tasks• Handover process

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Further Questions?