Daily Updation File OCT 2013.xlsx

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    Sr. No DATE

    STOP

    TIME

    START

    TIME

    TOTAL

    TIME

    Equipmen

    t Tag No

    withDescriptio

    n

    1

    2

    3

    4

    5

    6

    7

    89

    10 .

    11

    12

    13

    14

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    16

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    18

    19

    20

    21

    22

    23

    24

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    Type of Tripping with reason and rectification

    DAILY UPDTION FILE OF HT DRIVE MONTH: October-2013

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    Effect of

    production or Not

    Name of

    ShiftEngineer

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    Sr. No DATE STOP TIME START TIME TOTAL TIME

    1

    2

    3

    4

    5

    6

    7

    8

    9

    10

    11

    12

    13

    14

    15

    16

    17

    18

    DAILY UPDTION

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    Equipment Tag No with Description

    FILE OF LT DRIVE

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    MONTH: October2013

    Type of Tripping with reason and rectification

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    Effect of

    Productio

    n or Notfrom

    Electrical

    side

    Name of

    Shift

    Engineer

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    DE NDE

    CH9 CH10

    1 A VINOTH OFF OFF OFF OFF

    2 B Pitamber OFF OFF OFF OFF

    3 C Avinash OFF OFF OFF OFF

    4 A

    5 B

    6 C

    7 A

    8 B

    9 C

    10 A

    11 B

    12 C

    13 A

    14 B

    15 C

    16 A

    17 B

    18 C

    19 A

    20 B21 C

    22 A

    23 B

    24 C

    25 A

    26 B

    27 C

    28 A

    29 B

    30 C

    31 A

    32 B

    33 C

    34 A

    35 B

    36 C

    37 A

    38 B

    39 C

    11-Oct-13

    12-Oct-13

    13-Oct-13

    1-Oct-13

    2-Oct-13

    Sr. No. DATE SHIFT NAME

    BALL MILL 1

    KW

    BEARING RUNNING

    CURRENT

    10-Oct-13

    9-Oct-13

    3-Oct-13

    4-Oct-13

    5-Oct-13

    6-Oct-13

    7-Oct-13

    8-Oct-13

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    40 A

    41 B

    42 C

    43 A

    44 B

    45 C

    46 A47 B

    48 C

    49 A

    50 B

    51 C

    52 A

    53 B

    54 C

    55 A

    56 B

    57 C

    58 A

    59 B

    60 C

    61 A

    62 B

    63 C

    64 A

    65 B

    66 C

    67 A68 B

    69 C

    70 A

    71 B

    72 C

    73 A

    74 B

    75 C

    76 A

    77 B

    78 C

    80 B

    81 C

    82 A

    83 B

    84 C

    85 A

    86 B

    87 A

    22-Oct-13

    23-Oct-13

    16-Oct-13

    17-Oct-13

    18-Oct-13

    19-Oct-13

    20-Oct-13

    21-Oct-13

    14-Oct-13

    15-Oct-13

    24-Oct-13

    25-Oct-13

    26-Oct-13

    27-Sep-13

    28-Sep-13

    29-Sep-13

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    88 B

    89 C

    90

    30-Sep-13

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    DE NDE DE NDE DE

    CH9 CH10 CH9 CH10 CH9

    OFF OFF OFF OFF 53 40 148 1471 55

    OFF OFF OFF OFF 50 37 148 1488 47

    OFF OFF OFF OFF 50 37 140 1437 48

    CURRENT KW

    BEARING

    CURRENT

    ROD MILL 1

    BEARING RUNNING BEA

    BALL MILL 2

    RUNNING

    KW

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    NDE DE NDE DE NDE

    92 CH9 CH10 CH9 CH10

    42 48 390 OFF OFF OFF OFF 47 37

    39 67 442 OFF OFF OFF OFF 39 35

    39 40 378 OFF OFF OFF OFF 45 35

    1

    ING

    ROD MILL 2

    CURRENT KW

    RUNNING

    BLOWER 1 BLO

    CURRENT KW

    BEARING RUNNING BEARING

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    DE NDE DE NDE

    CH9 CH10 CH9 CH10

    42 434 OFF OFF OFF OFF OFF OFF OFF

    44 445 OFF OFF OFF OFF OFF OFF OFF

    45 444 39 34 9 27 43 34 20

    ER 3 SCH MOTOR

    CURRENT KWCURRENT KW

    RUNNING

    PCH MOTOR

    BEARING

    CURRENT

    BEARING RUNRUNNING

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    DE NDE DE NDE

    CH9 CH10 CH9 CH10

    OFF OFF OFF OFF OFF OFF OFF OFF OFF

    OFF OFF OFF OFF OFF OFF OFF OFF OFF

    51 OFF OFF OFF OFF OFF OFF OFF OFF

    BLOWER 2

    RUNNING

    CURRENT KW

    BEARING

    REGRIND MILL

    KW KW

    BEARING RUNNING

    CURRENT

    ING

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    1 A VINOTH 44 44 42

    2 B pitamber 46 44 44

    3 C Avinash 42 40 42

    4 A

    5 B

    6 C

    7 A

    8 B

    9 C

    10 A

    11 B

    12 C

    13 A

    14 B

    15 C

    16 A

    17 B

    18 C

    19 A

    20 B21 C

    22 A

    23 B

    24 C

    25 A

    26 B

    27 C

    28 A

    29 B

    30 C

    31 A

    32 B

    33 C

    34 A

    35 B

    36 C

    37 A

    38 B

    39 C

    12-Oct-13

    13-Oct-13

    7-Oct-13

    8-Oct-13

    9-Oct-13

    10-Oct-13

    11-Oct-13

    2-Oct-13

    SHIFT NAMEDATE

    Oil Temp

    1-Oct-13

    Oil Temp

    Sr. No.

    Power Transformer -

    1

    Power Tra

    Winding

    Temp

    3-Oct-13

    4-Oct-13

    5-Oct-13

    6-Oct-13

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    40 A

    41 B

    42 C

    43 A

    44 B

    45 C

    46 A47 B

    48 C

    49 A

    50 B

    51 C

    52 A

    53 B

    54 C

    55 A

    56 B

    57 C

    58 A

    59 B

    60 C

    61 A

    62 B

    63 C

    64 A

    65 B

    66 C

    67 A68 B

    69 C

    70 A

    71 B

    72 C

    73 A

    74 B

    75 C

    76 A

    77 B

    78 C

    79 A

    80 B

    81 C

    82 A

    83 B

    84 c

    85 A

    86 B29-Oct-13

    28-Oct-13

    25-Oct-13

    26-Oct-13

    27-Oct-13

    20-Oct-13

    21-Oct-13

    22-Oct-13

    23-Oct-13

    24-Oct-13

    15-Oct-13

    16-Oct-13

    17-Oct-13

    18-Oct-13

    19-Oct-13

    14-Oct-13

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    87 C

    88 a

    89 b

    c

    30-Oct-13

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    44 38 42 42 44 48 52 36 38

    42 38 36 44 40 56 48 34 32

    40 36 34 38 38 50 52 52 54

    Oil TempWinding

    Temp

    Oil TempWinding

    Temp

    Dist. Transformer - 1 Dist.Transformer - 3

    Oil Temp

    Dist. Transformer - 2

    Winding

    Temp

    Oil Temp

    nsformer -

    Winding

    Temp

    Winding

    Temp

    Dist. Transformer - 4

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    38 38 36 38 36 38 38 38 42

    38 36 40 38 38 36 40 38 44

    40 38 36 34 38 38 40 38 40

    Oil TempWinding

    Temp

    Dist.Transformer - 5

    Winding

    Temp

    Oil Temp

    4 MVA Tr

    Oil Temp

    Dist. Transformer - 8

    Winding

    Temp

    Dist. Transformer - 6 Dist. Transformer - 7

    Oil TempOil TempWinding

    Temp

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    44

    42

    40

    nsformer

    Winding

    Temp

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    18-8-12

    19-8-12

    22-8-12

    29-8-12

    6/9/2012

    13-9-2012

    2/10/2012

    12/10/2012

    3/11/2012

    6/11/2012

    13/11/12

    23/11/2012

    28-11-12

    29-11-12

    30-11-12

    4/11/2012

    26-12-12

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    27-12-12

    4/1/2013

    5/1/2013

    12/1/2013

    13-1-13

    20-1-13

    21-1-13

    24-1-13

    31-1-2013

    31-1-13, 1-2-13

    1 & 2-2-2013

    3/2/2013

    4/2/2013

    7,8,9,10-2-13,

    11/2/2013

    15-2-2013

    21-2-2013

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    23-2-13

    24-2-2013

    25-2-2013

    6/3/2013

    15-3-2013

    31-3-2013

    2,3-4-2013

    4/4/2013

    6/4/2013

    9/4/2013

    10/4/2013

    16-4-2013

    17-4-2013

    17-4-2013

    17-4-2013

    17-4-2013

    3/5/2013

    10/5/2013

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    11/5/2013

    12/5/2013

    13-5-13

    14-May-13

    17-5-13

    18-5-13

    19-5-13

    20-5-13

    27-5-2013

    28-5-2013

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    29-May-13

    30-May-13

    8-Jun-13

    8-Jun-13

    9-Jun-13

    11-Jun-13

    6/16/2013

    24-Jun-13

    27-Jun-13

    3-Jul-13

    4-Jul-13

    13-Jul-13

    18-Jul-13

    20-Jul-13

    21-Jul-13

    24-Jul-13

    4-Aug-13

    28-Aug-13

    18-Sep-13

    23-Sep-13

    18-Jun-13

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    25-Sep-13

    26-Sep-13

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    Ball mill 1 LRS insulator support damaged. Flash over. Total 9 nos were defective and replaced by new insulators.

    Ball mill 2 LRS insulator support damaged. Flash over. Total 9 nos were defective and replaced by new insulators.

    Rod mill 1 LRS checked. Insulation value was less. All the six insulators were replaced with good one.

    Ball mill 1, 2 water level in LRS was lowered by 30mm to increase the gap between the insulators and water

    level. For this one no 10mm hole was drilled in LRS tank.

    Ball mill 1 NDE side bearing NU 230 M was replaced as the old bearing was giving scratching sound. Grease

    SCH motor NDE bearing replaced.6320 C3.

    Motor fan replaced with the fabricated fan brought through Adarsh

    5AG-01, 5AG-02 lead agitator motor non drive end bearings were replaced with 6209-2RS bearing.

    Ohline shifting work completed near SKM gate through M/s Navdurga electrical jaipur

    11KV/440V 1500KVA trafo 440V side cables were removed and connected to 11KV/6.6KV/440V transformer .

    Raise borer M/c power supply given .

    Main V.fan greasing done. With Temp Gun. Motor DE Cover= 68 deg C , Motor body= 77degC, NDE cover=

    Masibus Scanner: Channel 1=36degC, 7= 110degC, 8=78degC.

    Raise borer m/c connections removed from the back of the techno office room.

    Power given to raise borer m/c at south ramp.

    The 33KV no 1 feeder tripped at early morning 1AM. One no 33KV PT fuse blown out at the SKM incomer feeder.

    The tripping was cause due to one cable bursting and eathing at the DSC side cable tray near yard. 33KV No 2 ckt

    Raise borer m/c pump connections removed in the evening as the pilot hole drilling is over.

    33KV no 2 feeder cable jointing done

    33KV no 2 feeder line charged after cable jointing work.

    Raise borer M/c is taking 490A @ the boring of 3.5 mtr dia .

    Hydro fill plant 6.6KV trafo power supply energized on 6.0PM.

    Important Breakdown list

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    SCH was giving problem. 3 core cable was laid out from oil cooling panel to float switch so that relay R1 can be

    energized directly. R2 elay is kept charged through permanent short ckt.

    The mill was switched off in 4PM due to the union after the accident in lead plant.

    33kv no1, no 2 circuits were taken in to ckt and 6.6KV no1, 2 feeders switched on and the bus coupler is kept off.

    Ball mill 1 DE side grease cover opened. The cup was not in exact position. Grease is coming out. Ball mill 1

    motor needs to be opened to rectify this fault. Fixed back as it is greasing done.

    11KV/6.6KV/440V 1500KVA transformer was energized from 6.6kv mill side power. Power given from 6.6KV

    Greasing done on Main V.fan 630KW

    Ball mill no 1 drive end side grease which was lying inside motor approximately 7KG was removed.

    Greasing done on V.fan

    Capacitor reforming done in the spare inverter module

    KTSelvan & Ravi went to Udaipur on official tour.

    CVR ventilation fan started. It is taking 150A load.

    Sh Sukhmayan was deputed for 33KV yard work at DSC

    Ball mill 1 : NDE side bearing NU230E ( Fag) changed, DE side bearing NU236E( NSK japan make ) & 6320

    changed.( Grease ring(oil ring in NDE side is AJ180 & this is damaged. ).

    All the three new bearings are SKF make.Ravikant Baipai sent to Udaipur for grease seal.

    U/G 11KV cable joint near hoist room opened, cable re-routed through cable trench and straight through jointing

    made. 8AM to 4PM. Cable charged back.

    Ball mill-1: Motor DE side oil seal 200*180*15 mm fixed with juggad fittings and trial taken.

    Total Mill power was taken through 33KV ckt2 @ 10AM. 33kv CKT 1is in no load.

    SCH crusher complete set replaced with new crusher, new oil cooling system, new overpressure fan.

    Sukmayan was deputed to DSC 33KV yard work

    DGMS electrical inspector visited SKM for inspection

    KTselvan Went to (DGMS ) Udaipur for submitting HT file. File was rejected as it was not in stipulated New

    VVIP visit took place at SKM.

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    Compressor house power shutdown taken from 3.0PM to 6.30 PM for jointing the VCB panels.

    High mast light work completed

    Went to DGMS Udaipur office on personal taxi to submit the compr house substation application.

    By train on 6-7-13 went to delhi. Came back on 8-3-13 by flight. V.fan motor inspection work.

    Power to south ramp given from mill side through cable. 11KV/440V transformer switched off and 440V cable

    connection removed from PCC side.

    BC-3 magnet coil insulation failure at bottom. Removed , repaird and brought back on 6-4-2013 for fixing. It was

    tested at Udaipur and found ok.

    M/s Zitron visited the SKM for additional fan requirement study.

    Went to Udaipur for magnet inspection @ Sakthi elect

    Mine shaft supply given from mill via feeder ie no 14 & 38

    Ball mill no 2 shaft sheared off near motor coupling.

    The BC-3 Magnet was put in to operation. Working OK.

    SCH motor (removed from use) DE side NU320 (SKF) bearing was changed with new bearing ( SKF). The bearingwas damaged due to low grease.

    ABB engr Raj kumar was attending the problem of UMC 22 for the past 4 days. MOM signed today. There is a

    small problem in the UMC 22 which needs to be resolved.

    Setting for trafo 3, 4 HT feeders changed from 0.7, 1.0 to 0.7, 0.4( I>0.7, t>0.4). Setting for trafo 440V incomer in

    all 1 to 8 no trafo changed to ( t> 0.65 from t>4.0)

    V.fan setting for 1 no channel changed from 70 to 75 deg for tripping. No1 channel temp reading jumped from

    V.fan AC indoor card damaged & sent to Udaipur. Now the AC is not working.

    Hydro fill plant 30VDC battery charger batteries failed in B shift end. Battery ircuit opened and the system

    started with 30VDC rectifier ckt without battery.

    Trafo-5 was tripped due to high set over current while the CT changing work is going on. MCC 5 Both front and

    Back side cleaned and checked.

    Both Mill stopped at 5 pm due to water shortage.

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    Both mill kept shut. PMCC2 complete blowering done on backside, front side . MCC5,6,7 complete blowering

    done. PMCC2 side all Breakers removed and cleaned. MCC5,6,7,8 ACB cleaned and checked.

    Both mill kept shut. MCC4 complete blowerng done. PMCC1 side front , back side complete blowering done.

    PMCC1 side all ACB opened and cleaned and checked. MCC4 checked. MCC1,2,3 opened and cleaned and

    checked. EMER MCCB ACB ( both ) not checked and cleaned.Both Mill started at 5 PM. Trafo 1,2,3,4,5,6 VCB Cleaned and checked.

    DSC power tripped at 5PM. 33KV 1,2 power not available. 11KV power not available. CPP is down. Power is

    through RSEB. Total load on mill 33KV feeder 2 is 2.3 MW.

    33KV no 1 feeder PT fuse blown at SKM side.

    Mill is off from 5PM.

    Both mills started at 12:30 AM.

    Shutdown taken from MRS for Incomer 1 (33KV) inorder to change the Line PT fuses ( R phase and Y phase).

    Incomer - 1 and Trafo 1 back panel cleaning done. Incomer 1 GO switch in 33KV Switch yard maintenance

    New reservoir pump started with VFD panel after cable laying work from hydro fill plant.( job went for a week).

    850 mtr cable 95 sqmm laid out. 45kw motor taking 33A at full speed.

    15kw submersible pump and starter fixed in the main reservoir sump and started.

    PB& ZN floculant drawing traced and changed as in the panel.

    MLDB 4 at PCH fixed with digital ELR.

    On trafo 4, oil leakage was found. And in there LT side bushings of Y and B phases were found loose. So it was

    630kw vfan motor received with duct assembly at SKM site.

    Plant - Both the streams are stopped due to the fatal accident in Mines at 4:00AM

    Plant didn't run for the whole day .

    Power Readings:

    33KV I/C 2 : 1.36MV

    Mines Shaft 2 : 362 W

    Surface VF : 320.2KW

    Mines 300MRI : 172KW

    Mines Fdr-4 : 51.5KW

    TR-7 : 24.5KW

    TR-6 : 132KW

    TR-5 : 115.5KW

    TR-4 : 2KW

    TR-3 : 93KW

    TR-2 : 165KW

    TR-1 : 2.4KW

    Shaft Fdr-1 : 67KW

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    Hydrofill Plant : 60KW

    Plant was Restarted at 10:30am after that incident.

    4P-01C, motor windings burnt and DE side bearing was damaged. e/f was shown in vfd. New 180kw(287A) motor

    was installed and ID run test was successful. Old motor details: Serial No: NAD2X 10507 TOP, Frame size:ND3152X New motor Details: Serial No: NAD2X 11876 TOP, Frame size: ND3152X. Old motor bearing -SKF

    NU319C3, This bearing was completely dry, inner race cracked, oil seal burned, motor rotor rubbed at drive end

    33kv black-out at 3pm from CPP. Entire plant was taken in load at 6:30 pm

    BM-1 energy meter was replaced with spare motor feeder (panel no 2)

    5AG-03G motor was replaced with newer one. Abnormal sound was noticed in motor.

    Regrind Mill motor was tripped due to False alarm in Temperature scanner. Problem due to loose connection in

    On rod mill-1 new 500kw motor was fixed. And no load trial was taken.

    Report of no load trial KW = 24, CURRENT = 22A, WINDING TEMP = 33, DE SIDE = 33, NDE SIDE = 31 , KVA =

    BC-2 tripper cable dressing done properly.Its clips got out from wire.It was fixed properly

    Ball Mill-1 ( channel 5 in Scanner was showing "undr' .While checking from motor side it was found that 1 cable g

    On mines shaft feeder-1 (feeder no 14) CT was changed by 400/1 A. Earlier it was 250/1 A.

    Hydro fill plant Transformer (6.6KV/440V) - NGR to Earthis not proper. It was rectified and started. Transformer b

    Feeder No 31 Charged by Mines Electrical for 212 mrl substation(mines). Micom 220 was found faulty andreplaced from spare feeder.Shutdown given.

    11KV Overhead Line was tripped due to earth fault. It was checked from Mines side by Mr. Bhanu. No problem

    was found. After that it was started again.

    7P-02 (1.1KW/2.35A) motor was replaced. Old motor was having bearing problem.

    33kV Incomer-1 shutdown was taken from MRS end. Incomer-1 & Transformer-1 breaker were turned OFF from

    SKM side. Bus Coupler is Racked Out

    Since new ventilation fan motor connection was to be done in Raise Borer M/C panel, P-22 in PMCC-2 so

    Shutdown was taken for trafo-5. This ventilation fan motor was installed in Mines area. Also ELR+CBCT was

    change in P-22, PMCC-2. After termination of Motor connection from feeder side its shutdown was cleared.

    3BC-03 ventilation fan trial taken. Taking 8.6A. ( Rating:5.5KW/9.9A, MPCB Setting:9A). Motor is runnig fine.

    Tripped from temp. scaner. While check it was found that its channel no-4 showing false reading. It was skiped

    and started again. Channel no 4 need to be check in ROD mill shutdown.

    5AG-03G (22KW/40A) has been changed with the spare one due to some abnormal sound in the motor. Load curr

    Trafo-3 was tripped without any indication in SPAJ-140C Relay. It was started again and no further tripping occur

    mcc 4 Tripped on Io>> fault. Fault has come from from ball mill 2 inching drive winding termination weak

    insulation. Also loose bolts were also found inside that terminal box. Trial was taken for that motor after

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    otor side RTD terminal.

    t cut .It was joined again.

    dy earthing also done.

    ent 27A. Running fine now

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    E PROBLEM.