Daily Completion - Workover Report
Transcript of Daily Completion - Workover Report
Well Name: Date: 4/27/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,537,230.00$ Cum Cost: 3,544,630.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 1,500.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools
Tech. Super.
Trucking 1,800.00$
Tbg Rentals
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Csg/TieBack 2,300.00$
DAILY TOTAL 7,400.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
7,400.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Took delivery of 3 ½” production string and loaded
out 4 ½” tie-back string (took to Deep Well for inspection). Well has 0
psi. SWI SDFN. ESP cancelled missing part of motor. Forecast: Will run
3 ½” on 4/28/2015 in the AM.
Well Name: Date: 4/25/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,523,930.00$ Cum Cost: 3,537,230.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools
Tech. Super. 1,200.00$
Trucking 1,500.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Csg/TieBack 2,300.00$
DAILY TOTAL 13,300.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL, well has 0 psi. ND 4 ½”, Nu BOP. RU laydown
machine and casing crew. Load and haul off workstring. PU on casing,
come out of PBR at 140K, LD 229 joints of 4 ½”. RD casing crew. SWI
SDFN.
13,300.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/24/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,513,830.00$ Cum Cost: 3,523,930.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools
Tech. Super. 1,200.00$
Trucking 600.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 10,100.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. POOH w/ workstring, laying down w/ bit. SWI
SDFN 5:30pm. Forecast: Will ND liner and pull.
10,100.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/23/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,480,730.00$ Cum Cost: 3,513,830.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 10,000.00$
Reverse unit
Rig 8,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 9,000.00$
Tech. Super. 1,200.00$
Trucking 600.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 33,100.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
33,100.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
6:00am – PU 3 ¾” milltooth.
RIH to 8000’, break circulation.
RIH to 10,990’, break circulation.
RIH to 12,000’, break circulation.
RIH, tag 13,436’, wash 60’ at a time. Circulate bottoms up, fell out at
13,600’. RIH, 10 joints at a time and circulate for 30 minutes. Well
staying at 400 psi. Tagged bottom at 15,495’, circulate for 4 hours. Lost
returns; would get them back for 20 minutes at a time. Hang kill tbg, LD
swivel. POOH, laying down workstring. Forecast: LD workstring.
Well Name: Date: 4/22/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,447,630.00$ Cum Cost: 3,480,730.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 10,000.00$
Reverse unit
Rig 8,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 9,000.00$
Tech. Super. 1,200.00$
Trucking 600.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 33,100.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
33,100.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
6:00am – Crew change. Wash down to 13,405’, circulate for 3 hours,
could not make more hole. Circulation pressure – 460 psi on wellhead.
Kill tbg, POOH w/ bit. Bit had marks on inside of cones. Put on 3 ¾”
overshot w/ bumper sub and oil jars. TIH to 13,405’, caught fish, came
free at 4K over. Went down 30’ past where fish was, TOH. Got out at
08:30hrs w/ mill and bit box from coil. Forecast: RIH, wash to 15,490’,
circulate clean.
Well Name: Date: 4/21/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,418,530.00$ Cum Cost: 3,447,630.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 10,000.00$
Reverse unit
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 9,000.00$
Tech. Super. 1,200.00$
Trucking 600.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 29,100.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
29,100.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Well has 800 psi (it was shut in w/ 450 psi);
circulate for 1 hour. RIH, picking up 20 jts at a time and breaking
circulation. Tagged @ 12,711’, washed to 12,797’, lost wellhead returns
– very little circulation. Cut soap back, blew on it for 1 ½ hours. Kill tbg,
POOH, LD motor. RIH w/ 3 7/8” mill tooth and bumper sub, oil jars and
2 3/8” workstring. Got to 10,990’, started jamming; air took 5 hours to
break circulation. Go in to 11,100’ tag high; PU swivel and wash
through. Lost circulation, blow on well for 2 ½ hours, hang swivel back.
Crew change @ 0600hrs. Forecast: Wash to bottom, 15,490’.
Well Name: Date: 4/20/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,387,930.00$ Cum Cost: 3,418,530.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 10,000.00$
Reverse unit
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 9,000.00$
Tech. Super. 1,200.00$
Trucking 2,100.00$
Tbg Rentals 2,500.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 30,600.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Open well – 0 psi. Move in (2) – 1350 foam air
units and a frac tank w/ gas buster. Plumb in w/ hardline; PU 3 7/8”
sealed bearing tri-cone bit w/ motor, bumper sub, oil jars. RIH w/ 2
3/8” PH6 P110 workstring to 5000’. Unload well, no fluid. RIH to
10,026’, unload 60 bbls fluid; took 3 hours to get circulation. SWI,
SDFN.
Took delivery of 4500’ of 2 3/8” P110 workstring, now have 15,500’.
Load out 2 7/8” Hydrill and release. Forecast for tomorrow: Clean well
to 15,490’.
30,600.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/18/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,378,830.00$ Cum Cost: 3,387,930.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 1,500.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools
Tech. Super. 1,200.00$
Trucking
Tbg Rentals 2,100.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 9,100.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
9,100.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Open well – 0 psi. Cut and LD 892' coil (made 24
cuts), LD motor (left 3 7/8” mill and motor shaft, about 3’). Shut well in,
SD. Will resume operations 4/20/2015 w/ clean-out run. Will push bit
to bottom and leave.
Well Name: Date: 4/17/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,361,930.00$ Cum Cost: 3,378,830.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 4,800.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 4,500.00$
Tech. Super. 1,200.00$
Trucking
Tbg Rentals 2,100.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 16,900.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
16,900.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL, well on vacuum; finish POOH. Put on overshot and
jars, RIH, latch on to fish @ 10,365’. Jar for 3 hours, making 4’; jarring
up to 140K. Fish came loose; pull out fish, dragging out. Pull up, verify
fish has 6K of weight when we got to surface. Shut well in, SD.
Prepping to cut and LD coil.
Well Name: Date: 4/16/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,345,630.00$ Cum Cost: 3,361,930.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 4,800.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 2,700.00$
Tech. Super. 1,200.00$
Trucking 1,200.00$
Tbg Rentals 2,100.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 16,300.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Open well – 0 psi. Unload 1000’ of 2 7/8” Hydrill.
PU 3 ¾” shoe, 992’ of 2 7/8” Hydrill. RIH, slide over fish, wash down to
11,262’. Circulation pressure at 1200 psi at 3 bpm. Wash sand and
circulate clean. Pull up 1500’, SWI and SDFN. Forecast: Will POOH to
look at shoe to see if bottomed out – if so, will RIH w/ jars and overshot
to jar fish out.
16,300.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/15/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,326,430.00$ Cum Cost: 3,345,630.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 6,000.00$
Tech. Super. 1,200.00$
Trucking
Tbg Rentals 1,200.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 19,200.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
19,200.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
8:00am – Crew AOL. Open well – 0 psi. TIH w/ overshot and
workstring. Latch onto fish, jar on coil for 4 hours, jarring up to 140K.
Got off of fish, POOH, no damage done to grapple. SWI, SDFN. Forecast
for tomorrow: Will PU 2 7/8” CS Hydril and wash over coil.
Well Name: Date: 4/14/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,307,230.00$ Cum Cost: 3,326,430.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 6,000.00$
Tech. Super. 1,200.00$
Trucking
Tbg Rentals 1,200.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 19,200.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
19,200.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Open well – 0 psi. PU 3 ¾” shoe and 3 jts of wash
pipe. RIH, tag up at 10,365’. Wash 60’ of sand and plug parts, circulate
clean. Hang swivel back, POOH. Pick up: overshot w/ new grapple, 4’
extension, jars, collars w/ bumper sub, 6 collars w/ accelerator. SWI,
SDFN. Forecast for tomorrow: RIH and latch on and attempt to jar free.
Well Name: Date: 4/13/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,288,030.00$ Cum Cost: 3,307,230.00$
Bits
BOP/Rentals
Cementing
Coil Unit
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit 2,500.00$
Rig 4,000.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 6,000.00$
Tech. Super. 1,200.00$
Trucking
Tbg Rentals 1,200.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 19,200.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Open well, no pressure. Finish RIH, got down to
fish, PU swivel. Wash down 6’, full circulation. Latch onto fish, hang
back swivel, started jarring at 100K working up to 120K. Fish pulled off
after jarring for 2 ½ hours. Made 12’, coil still stuck. POOH w/ grapple.
Shut well in, SDFN. Forecast for tomorrow: PU 100’ wash pipe, make
wash run before latching back on.
19,200.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/12/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,267,280.00$ Cum Cost: 3,288,030.00$
Bits
BOP/Rentals 600.00$
Cementing
Coil Unit
Flowback 2,500.00$
Forklift 700.00$
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 3,800.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 9,150.00$
Tech. Super.
Trucking 1,000.00$
Tbg Rentals 1,200.00$
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane
Frac Tanks
DAILY TOTAL 20,750.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
7:00am – Pipe on location. Unload and tally 2 3/8” P110 (351 jts). NU
BOP, PU fishing tools: 3 7/8” overshot w/ 2” grapple, 3 1/8” bumper
sub, 3 1/8” hydro jars, 6 – 3 1/8” DCs, 3 1/8” energizer sub, 268 jts 2
3/8” P110. Got in w/ 8559’, shut well in at 6:30pm. Forecast for
tomorrow: Tag up, break circulation, wash down to fish, latch on and
jar free.
20,750.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/11/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,200,330.00$ Cum Cost: 3,267,280.00$
Bits
BOP/Rentals
Cementing
Coil Unit 30,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 2,500.00$
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 2,500.00$
Tech. Super. 3,500.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip. 650.00$
Wellhead
Wireline Service/TCP 18,000.00$
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 66,950.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
66,950.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
7:00am – Pick up on coil w/ crane to 40K. Went to NU injector head
and coil dropped out of chains. Top of fish at ground level; get overshot
and 10’ x 2 3/8” sub. Fished coil out w/ crane. Held fish w/ BOP slips,
put on coil connector w/ TIW valve. Made gauge ring run to 10,400’,
POOH. Put on cutter 1.35. RIH, pumped 25 bbls down coil, cut coil.
POOH, RD wireline, latch onto coil w/ crank, only pull 40K and no
movement. Call out rig and rig mats; RU well service unit, latch on, pull
up to 80K and coil pulling free. Sand packed off around cut, LD 30’ coil.
Pulling free at 65K. NU injector head, tie-back to release. Pull out 130’,
pulled free. POOH w/ 10,375’ of coil. Inspected cut on fish – CLEAN.
RD coil unit. Shut well in, shut down 2:30am. Forecast for tomorrow:
PU work string w/ overshot and jars to work fish free.
Well Name: Date: 4/10/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,121,530.00$ Cum Cost: 3,200,330.00$
Bits
BOP/Rentals
Cementing
Coil Unit 61,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 8,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 78,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
78,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
6:00am – Pumping N2 at 2800 mcf, no pressure build up on casing.
Working coil up to 87K and snubbing down to 40K. Coil parted at
surface; ND coil, PU on coil. Clamped off, broke BOP down and NU over
part. Secure well and line up wireline service to cut coil, put on coil
connector, NU TIW. Shut well in, SDFN. Forecast for tomorrow: Cut
coil at 10,375’.
Well Name: Date: 4/9/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 3,048,730.00$ Cum Cost: 3,121,530.00$
Bits
BOP/Rentals
Cementing
Coil Unit 48,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 72,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
72,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
6:00am – Well shut in. N2 unit down. Parts are being flown in from
Houston. 6:30pm – N2 came back online. Pumping 2800 mcf;
circulation pressure 3350 psi, wellhead built up to 93 psi. 12:30am –
Started working coil down -30K to max pull of 87K – no movement.
Circulation pressure 3350 psi, no change and wellhead 0 psi. Well not
charging. Undress pack-off, work coil several more times, no
movement. (Greystone) to prep an AFE for cutting coil and fishing tools
and coil out from depth of 11,498’.
Well Name: Date: 4/8/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,958,430.00$ Cum Cost: 3,048,730.00$
Bits
BOP/Rentals
Cementing
Coil Unit 65,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,500.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 90,300.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
6:00am – Pumping N2 at 2800 mcf and fluid at rollover w/ foamer down
coil. 4:00pm – Started to circulate around 1 bbl out while pumping 4.5
bbls in. Moved coil to 11,498’, lost circulation again, shut casing in.
Continue to pump and work coil through the night, no movement, no
circulation. N2 pump went down at 5:45am. Well shut in. Waiting on
change out of pump. Prep to continue to try and work free. Circulation
pressure has been running around 5300 on coil
90,300.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/7/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,871,630.00$ Cum Cost: 2,958,430.00$
Bits
BOP/Rentals
Cementing
Coil Unit 62,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 86,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
6:00am – Charging on well, worked free. 2:30pm – Come up from
12,770’ to 11,505’; lost wellhead pressure again, went back to charging
well w/ 2400 psi on casing. Pumping down coil w/ 0.75 bpm fluid and
1200 mcf N2. Worked pipe several times, well still not charging. Have
not made any more hole. At midnight, dropped ball going straight
through circulation. Sub fluid w/ straight N2, 2200 mcf. Pumped 520
bbls fluid while stuck at 11,505’. Was pumping 0.25 gallons foamer per
10 bbls fluid. At 6:00am, still charging well. Prep to work coil free, then
POOH.
86,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/6/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,788,830.00$ Cum Cost: 2,871,630.00$
Bits
BOP/Rentals
Cementing
Coil Unit 58,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 82,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
6:00am – RIH w/ coil. Well has 100 psi, wellhead pumping 600 mcf N2
and ¾ bpm fluid. Got to curve, picked up N2 rate to 1000 mcf. Tag sand
at 13,211’; wash 100’ at a time. Pull 100, got through, went down,
tagged plug #4 @ 14,571’, short trip. Got sticky at 11,300’, lost
wellhead; recharge well to 2100 psi. POOH to 9700’. RIH, holding 500
psi on wellhead, tag plug #4 @ 14,571’, plug #3 @ 14,097’, plug #2 @
15,042’ and plug #1 @ 15,277’. Wellhead 480 psi, pumping 5 bbls
sweeps 100 vis. Tag bottom @ 15,490’, well drilled out. POOH, got to
13,200’, wellhead went to 0 psi, lost circulation. Pulled to 12,220’, got
tight. Stopped and started recharging well from 2:00am. At 6:00am still
charging. Pulled to 10K over and stacked down trying to snub, no
progress. Still charging. Prep to get coil free, POOH, then RDMO.
82,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 4/2/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,713,030.00$ Cum Cost: 2,788,830.00$
Bits
BOP/Rentals
Cementing
Coil Unit 51,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 75,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
75,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Art Linthicum
Activity: Expense Breakdown:
5:00am – Moved coil 200’, lock down again. Charge up 2500 psi on
casing. Pump-down coil until well charged up. Open casing through gut
line, pull up 80K and coil pulled free. POOH w/ coil, change bit nipple,
clean out plug catcher. Ready to run back in and finish last 4 plugs first
thing in the AM on 04/06/15. Shut well in shut down 7:30pm.
Well Name: Date: 4/1/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,639,730.00$ Cum Cost: 2,713,030.00$
Bits
BOP/Rentals
Cementing
Coil Unit 51,000.00$
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 73,300.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Art Linthicum
Activity: Expense Breakdown:
5:00am – Finish POOH; no cutting in basket. Put on bit, RIH, tag plug #8
@ 13,604’, plug #7 @ 13,838’ and plug #6 @ 14,084’. Circulation
pressure on wellhead 245 psi. Pumping 1 bbl, 1000 N2. Tag plug #5 @
14,328’. Pumping 5 bbls sweeps; drill out plug #5 and well goes on
vacuum. POOH to short trip to 13,337’, still no circulation. Started
getting sticky; shut down, start to charge well. On casing pumping 1200
N2 @ 2000 psi; back on coil, pumping 0.75 fluid 1000 N2. Drag up hole
to 13,100’ pulling 65K to 80K. Recharge well, start trying to work free.
Moved a couple of feet, let coil set. Pumping down coil to charge up
well. Will continue to try and work free and drill out remaining 4 plugs
in the AM. Well shut in to charge.
73,300.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Clean out well
15,490'
Well Name: Date: 3/31/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,563,930.00$ Cum Cost: 2,639,730.00$
Bits
BOP/Rentals
Cementing
Coil Unit 51,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 75,800.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
75,800.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RD Frac Equipment / Move off location
15,490'
Art Linthicum
Activity: Expense Breakdown:
5:00am – Charging well up, 30 psi on casing. Switch off coil, pump
down casing w/ N2. Pressure up to 2400 psi, book back to coil, started
pumping 0.75 fluid and 1200 N2. Work coil at negative 20K and pull to
85K. Rip casing open to pit while working coil; continue same steps.
7:30pm – Coil came free, circulate @ 280 psi, send 2 sweeps at 5 bbls
each and 110 vis. POOH, change out motor, put on Venturi basket. First
run, tag @ 13,365’. Come out w/ 0.25 full basket. RIH again, set down
mill down 4’ of basket cavity. POOH. Prep to drill out remaining 9
plugs.
Well Name: Date: 3/30/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,482,630.00$ Cum Cost: 2,563,930.00$
Bits
BOP/Rentals 3,500.00$
Cementing
Coil Unit 51,000.00$
Flowback 2,500.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Downhole Tools 15,000.00$
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks 2,000.00$
Well Equip.
Wellhead
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks
DAILY TOTAL 81,300.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
81,300.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RD Frac Equipment / Move off location
15,490'
Art Linthicum
Activity: Expense Breakdown:
5:00am – Open well, RIH w/ coil tbg @ 5000’. Start N2 @ 1.5 fluid and
600 N2. Tag plug #1 @ 11,261, plug #2 @ 11,497’, plug #3 @ 11,728’.
Short trip to wellhead, 70 psi sweeps. Pumped 5 bbls w/ 5 bbls spacer,
110 visc. Plug #4 @ 11,966’, #5 @ 12,174’, 6 @ 12,296’. Short trip, tag
plug #7 @ 12,451’, plug #8 @ 12,690’, plug #9 @ 12,927, plug #10 @
13,178’. Tag #11 @ 13,400’, do not drill, short trip. Wellhead 45 to 75
psi, pumping 1 bbls fluid, 1000 N2. Pulled to 12,305’, well goes on
vacuum. 10:00pm – Coil stuck. Work coil until 1:00am. Max pulled,
used 75K snub down, max 20K. Made 10’. No circulation. 5:00am –
Start at 1200 and fluid 0.75. Still charging wellbore. Wellhead 30 psi,
casing still shut. Prep to continue charging well to work coil free.
Well Name: Date: 3/29/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,467,580.00$ Cum Cost: 2,482,630.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,800.00$
Tbg Testing
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
DAILY TOTAL 15,050.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
15,050.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RD Frac Equipment / Move off location
15,490'
Bob Dimit
Activity: Expense Breakdown:
MIRU coiled tbg and clean-out tools.
Well Name: Date: 3/28/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 2,452,830.00$ Cum Cost: 2,467,580.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
DAILY TOTAL 14,750.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
14,750.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RD Frac Equipment / Move off location
15,490'
Bob Dimit
Activity: Expense Breakdown:
Move frac equipment off location.
Well Name: Date: 3/27/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 1,920,140.00$ Cum Cost: 2,452,830.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 1,950.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP 18,600.00$
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
Pressure Control 15,860.00$
Frac Pumping (4 Stages) 406,955.00$
Frac Plugs 6,945.00$
Water (12,546 bbls) 8,785.00$
Acid/Chems 54,845.00$
DAILY TOTAL 532,690.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
532,690.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Pump Stages 15 - 18
15,490'
Perf Stage #16 11,851', 11,771', 11,691, Stage #17 11,611',
11,531', 11,458', Stage #18 11,373', 11,291', 11,211'
Bob Dimit
Activity: Expense Breakdown:
Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500
psi.
Pumped Stage #15 with 4,200 gal 15% HCl, 122,262 gal linear & cross-
linked gel, 151,538# of 20/40 RC sand @ 60 BPM. Set Magnum Snub
Nose flow-thru plug at 11,891'. Perforated Devonian @ 11,851',
11,771', 11,691' with 19 shots (.35" holes). Pressure tested lines. Drop
frac plug ball ahead of acid.
Pumped Stage #16 with 3,990 gal 15% HCl, 120,162 gal linear & cross-
linked gel, 148,225# of 20/40 RC sand @ 60 BPM. Set frac plug at
11,651'. Perforated @ 11,611', 11,531', 11,458'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #17 with 3,822 gal 15% HCl, 118,860 gal linear & cross-
linked gel, 145,413# of 20/40 RC sand @ 60 BPM. Set frac plug at
11,417'. Perforated @ 11,373', 11,291', 11,211'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #18 with 3,990 gal 15% HCl, 125,390 gal linear & cross-
linked gel, 144,215# of 20/40 RC sand @ 60 BPM. Job Complete
Well Name: Date: 3/26/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 1,543,535.00$ Cum Cost: 1,920,140.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 1,950.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP 18,600.00$
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
Pressure Control 18,860.00$
Frac Pumping (3 Stages) 305,220.00$
Frac Plugs 6,945.00$
Water (12,546 bbls) 6,280.00$
DAILY TOTAL 376,605.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
376,605.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Pump Stages 12 - 14
15,490'
Perf Stage #13 12,569', 12,495', 12,411, Stage #14 12,331',
12,251', 12,171', Stage #15 12,091', 12,008', 11,934'
Bob Dimit
Activity: Expense Breakdown:
Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500
psi.
Pumped Stage #12 with 5,208 gal 15% HCl, 117,684 gal linear & cross-
linked gel, 141,088# of 20/40 RC sand @ 60 BPM. Set Magnum Snub
Nose flow-thru plug at 12,611'. Perforated Devonian @ 12,569',
12,495', 12,411' with 19 shots (.35" holes). Pressure tested lines. Drop
frac plug ball ahead of acid.
Pumped Stage #13 with 3,822 gal 15% HCl, 119,826 gal linear & cross-
linked gel, 141,201# of 20/40 RC sand @ 60 BPM. Set frac plug at
12,371'. Perforated @ 12,331', 12,251', 12,171'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #14 with 4,074 gal 15% HCl, 116,886 gal linear & cross-
linked gel, 149,321# of 20/40 RC sand @ 60 BPM. Set frac plug at
12,131'. Perforated @ 12,091', 12,008', 11,934'. SDFN.
Well Name: Date: 3/25/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 1,056,978.00$ Cum Cost: 1,543,535.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 1,950.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP 24,800.00$
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
Pressure Control 16,060.00$
Frac Pumping (4 Stages) 406,952.00$
Frac Plugs 9,260.00$
Water (12,546 bbls) 8,785.00$
DAILY TOTAL 486,557.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
486,557.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Pump Stages 8 - 11
15,490'
Perf Stage #9 13,531', 13,451', 13,371, Stage #10 13,291',
13,211', 13,137', Stage #11 13,053', 12,971', 12,891', Stage # 12
12,811', 12,731, 12,651
Bob Dimit
Activity: Expense Breakdown:
Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500
psi.
Pumped Stage #8 with 3,780 gal 15% HCl, 111,342 gal linear & cross-
linked gel, 92,200# of 20/40 RC sand @ 60 BPM. Set Magnum Snub
Nose flow-thru plug at 13,571'. Perforated Devonian @ 13,531',
13,451', 13,371' with 19 shots (.35" holes). Pressure tested lines. Drop
frac plug ball ahead of acid.
Pumped Stage #9 with 4,620 gal 15% HCl, 125,370 gal linear & cross-
linked gel, 141,576# of 20/40 RC sand @ 60 BPM. Set frac plug at
13,331'. Perforated @ 13,291', 13,211', 13,137'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #10 with 4,536 gal 15% HCl, 126,252 gal linear & cross-
linked gel, 148,889# of 20/40 RC sand @ 60 BPM. Set frac plug at
13,098'. Perforated @ 13,053', 12,971', 12,891'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #11 with 4,200 gal 15% HCl, 119,994 gal linear & cross-
linked gel, 141,499# of 20/40 RC sand @ 60 BPM. Set frac plug at
12,851'. Perforated @ 12,811', 12,731', 12,651' SDFN.
Well Name: Date: 3/24/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 562,724.00$ Cum Cost: 1,056,978.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 9,547.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP 24,800.00$
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
Pressure Control 16,140.00$
Frac Pumping (4 Stages) 406,952.00$
Frac Plugs 9,260.00$
Water (12,575 bbls) 8,805.00$
DAILY TOTAL 494,254.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
494,254.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Pump Stages 5 - 7
15,490'
Perf Stage #5 14,491', 14,411', 14,325, Stage #6
14,251',14,171',14,091', Stage #7 14,011', 13,931', 13,851',
Stage # 8 13,766', 13,691, 13,611
Bob Dimit
Activity: Expense Breakdown:
Pressure tested lines to 9400 psi. Pressured 4 ½” – 7” annulus to 2500
psi.
Pumped Stage #4 with 3,990 gal 15% HCl, 120,876 gal linear & cross-
linked gel, 143,638# of 20/40 RC sand @ 60 BPM. Set Magnum Snub
Nose flow-thru plug at 14,531'. Perforated Devonian @ 14,491',
14,411', 14,325' with 19 shots (.35" holes). Pressure tested lines. Drop
frac plug ball ahead of acid.
Pumped Stage #5 with 4,116 gal 15% HCl, 142,800 gal linear & cross-
linked gel, 141,987# of 20/40 RC sand @ 60 BPM. Set frac plug at
14,295'. Perforated @ 14,971', 14,896', 14,811'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #6 with 4,242 gal 15% HCl, 130,116 gal linear & cross-
linked gel, 140,403# of 20/40 RC sand @ 60 BPM. Set frac plug at
14,051'. Perforated @ 14,011', 13,931', 13,851'. Pressure tested lines.
Drop frac plug ball ahead of acid.
Pumped Stage #7 with 4,116 gal 15% HCl, 120,078 gal linear & cross-
linked gel, 139,726# of 20/40 RC sand @ 60 BPM. Set frac plug at
13,806'. Perforated @ 13,766', 13,691', 13,611' SDFN.
Well Name: Date: 3/23/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 187,674.00$ Cum Cost: 562,724.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 1,950.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP 18,600.00$
WO Fluids
Crane 5,500.00$
Frac Tanks 450.00$
Pressure Control 15,800.00$
Frac Pumping (3 Stages) 305,220.00$
Frac Plugs 6,945.00$
Water (11,119 bbls) 7,785.00$
DAILY TOTAL 375,050.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
375,050.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Pump Stages 1 - 3
15,490'
Stage #2 15,211',15,131',15,051', Stage #3 14,971', 14,896',
14,811', Stage # 4 14,731', 14,651', 14,571'
Bob Dimit
Activity: Expense Breakdown:
Pressure tested lines to 9483 psi. Pressured 4 ½” – 7” annulus to 2500
psi.
Pumped Stage #1: 630 gal 15% HCl, 153,888 gal linear & cross-linked
gel, 183,966# of 20/40 RC sand @ 60 BPM. Set Magnum Snub Nose
flow-thru plug at 15,251'. Perforated Devonian @ 15,211', 15,131',
15,051' with 19 shots (.35" holes). Pressure tested lines. Drop frac plug
ball ahead of acid.
Pumped Stage #2: 6,720 gal 15% HCl, 142,800 gal linear & cross-linked
gel, 141,987# of 20/40 RC sand @ 64BPM. Set frac plug at 15,011'.
Perforated @ 14,971', 14,896', 14,811'. Pressure tested lines. Drop frac
plug ball ahead of acid.
Pumped Stage #3: 5,460 gal 15% HCl, 161,379 gal linear & cross-linked
gel, 131,712# of 20/40 RC sand @ 64 BPM. Set frac plug at 14,771'.
Perforated @ 14,731', 14,651', 14,571'. Pressure tested lines. SDFN
Well Name: Date: 3/22/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 148,474.00$ Cum Cost: 187,674.00$
Bits
BOP/Rentals 2,500.00$
Cementing
Coil Unit
Flowback 1,800.00$
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumps 4,000.00$
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super. 1,950.00$
Trucking
Tbg 3 Days
Vacuum Trucks
Well Equip.
Wellhead 3,000.00$
Wireline Service/TCP
WO Fluids
Pick Up Machine
Sfc Rentals 5,500.00$
Frac Tanks 2,700.00$
Pressure Control 16,250.00$
DAILY TOTAL 39,200.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Jody Linthicum
Activity: Expense Breakdown:
Move in frac stack, crane, wireline, pump-down, flowback, lights/lifts
and sanitation. RU and ready for frac.
39,200.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Prep for Frac
15,490'
15,441' , 15,366', 15,291'
Well Name: Date: 3/12/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 137,304.00$ Cum Cost: 148,474.00$
Bits
BOP/Rentals 1,500.00$
Cementing
Coil Unit
Flowback
Forklift 750.00$
Hot Oilier
Kill Truck
PKR Service
Pumps
Reverse unit
Rig 3,000.00$
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking 1,500.00$
Tbg 3 Days 1,920.00$
Vacuum Trucks
Well Equip.
Wellhead 1,000.00$
Wireline Service/TCP
WO Fluids
Pick Up Machine
DAILY TOTAL 11,170.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
11,170.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RU coil tubing unit / Toe Prep
15,490'
15,441' , 15,366', 15,291'
Jody Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. Well on slight vacuum. Release hanger and POOH,
laying down tbg. POOH w/ gauges and contact Precision Pressure Data
to pick up. ND BOP, NU master valve, RD and release rentals and move
off. Will have remainder of frac stack NU and move in support rentals
on 3/21/2015.
-------Standby for Frac Date---------------
Well Name: Date: 3/9/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 121,940.00$ Cum Cost: 137,304.00$
Bits
BOP/Rentals 500.00$
Cementing
Coil Unit
Flowback
Forklift 750.00$
Hot Oilier
Kill Truck
PKR Service
Pumps 4,064.00$
Reverse unit
Rig 3,000.00$
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking 1,000.00$
Tbg Rental/Day 640.00$
Vacuum Trucks
Well Equip.
Wellhead 1,000.00$
Wireline Service/TCP
WO FluidsPick Up/Lay Down
Machine 2,910.00$
DAILY TOTAL 15,364.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Jody Linthicum
Activity: Expense Breakdown:
7:00am – Crew AOL. RU, rack 335 jts 2 3/8” L80 rental. ND master valve
and NU BOP. PU SN w/ 2 3/8” x 6’ perforated gauge carrier and tally in.
TIH w/ 331 jts, PU hanger and land tbg @ 10,593'. RU pump, load w/ 37
bbls, shut in tbg and establish rate of 8 bpm @ 3630 psi.
25 bbls in, 8 bpm @ 3650 psi
50 bbls in, 7.75 bpm @ 3800 psi
71 bbls in, 7.6 bpm @ 3900 psi and SD
ISIP – 1300 psi / 5 minutes – 475 psi / 8 minutes – 0 psi
Shut in and RD pump. Will POOH w/ gauges on 3/12/2015. Basic
elected to leave rig over hole w/ no standby charges. SISDFTD 5:30pm.
15,364.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RU coil tubing unit / Toe Prep
15,490'
15,441' , 15,366', 15,291'
Well Name: Date: 3/8/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 42,365.00$ Cum Cost: 121,940.00$
Bits
BOP/Rentals
CementingCoil Unit w/ Chemical
& Mixing Plant 40,000.00$
Flowback
Forklift
Hot Oilier
Kill Truck
PKR Service
Pumping Unit
Reverse unit
Rig
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking
Tubing
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service/TCP 11,942.00$
WO Fluids
Acid/Chems 12,085.00$
Motor w/ Mill 14,048.00$
DAILY TOTAL 79,575.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Jody Linthicum
Activity: Expense Breakdown:
5:00am – Move in coil tubing unit/mixing plant, RU. PU motor w/ 3 7/8”
mill; test motor, NU, test stack to 10K and casing to 6K, RIH. Baker TCP
and acid on location. Tag 15,490' w/ mill, send sweep, drop ball and lay
71 bbls of 15% Acetic acid in lateral. POOH to 9500', pump soda ash
through coil and chase sweep out of hole. LD motor/mill, PU guns and
RIH to 15,490'. Perforate:
7 shots/6spf/60deg/.35 entry hole diameter (ehd) @ 15,441'
6 shots/6spf/.35ehd @ 15,366'
6 shots/6spf/.35ehd @ 15,291'
POOH to 9500’. Establish rate through coil of 5 bpm @ 3600 psi, pump
29 bbls, SD. Pressure @ 0 psi and resume POOH. POOH w/ guns, all
shots fired. Start RDMO at 10:00pm. Will move in rig, tbg and gauges
for DFIT in the AM.
79,575.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
RU coil tubing unit / Toe Prep
Well Name: Date: 3/7/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: 6,250.00$ Cum Cost: 42,365.00$
Bits
BOP/Rentals 1,000.00$
Cementing
Coil Unit
Flowback
Forklift
Hot Oilier
Kill Truck 500.00$
PKR Service
Pumping Unit
Reverse unit
Rig 4,200.00$
Rods
Roustabout 500.00$
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking 500.00$
Tubing
Vacuum Trucks 1,600.00$
Well Equip.
Wellhead 7,500.00$
Wireline Service
WO Fluids
Csg/TieBack 6,015.00$
Torque Turn 5,750.00$
Casing Crew 7,050.00$
DAILY TOTAL 36,115.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Jody Linthicum
Activity: Expense Breakdown:
7:00am – Crews AOL. RU casing equipment, PU seal assembly, set
torque turn and tally in w/ csg. Seat seals, test to 2000 psi. Pull seal,
sub out and land hanger w/ 90K compression. ND BOP, NU tbg head
and master valve. Test annulus to 2000 psi, RD casing crews and
release. RD pulling unit, move off and ready for CTU toe prep in the
AM. SISDFTD 10:00pm
36,115.00$
Daily Completion - Workover Report
University 31 #1H - Greystone Oil & Gas
Triple N - Devonian
CB-1408
Original Completion of Well
Basic Energy
Rig to run Casing
Well Name: Date: 3/6/15
Field: Safety Mtg: Yes
AFE No: AFE Amount: WI %
Purpose:
Rig Contractor: Operator: Jose Pusher:
Present Operation:
Comp Days: Workover Days: Testing Days:
Original PBTD: New PBTD: BOPD:
Orig. Open Perfs: BWPD:
New Perfs: MCFPD:
Daily Costs: Prior Cum Cost: -$ Cum Cost: 6,250.00$
Bits
BOP/Rentals 1,000.00$
Cementing
Coil Unit
Flowback
Forklift 750.00$
Hot Oilier
Kill Truck
PKR Service
Pumping Unit
Reverse unit
Rig 1,000.00$
Rods
Roustabout
Stimulation
Supervision 1,500.00$
Tbg Testing
Tech. Super.
Trucking 2,000.00$
Tubing
Vacuum Trucks
Well Equip.
Wellhead
Wireline Service
WO Fluids
Workstring
Rentals Surface
Safety Anchors
DAILY TOTAL 6,250.00$
Total Load (bbls): Swab (hrs):
Load to Recover: Daily Recovery (bbls):
Rig Supervisor: Total Recover (bbls):
BO:
Daily Completion - Workover Report
Original Completion of Well
Basic Energy
6,250.00$
Expense Breakdown:Activity:
University 31 #1H - Greystone Oil & Gas
CB-1408
Triple N - Devonian
10:00am – Move in rig, racks/mats, BOP and RU. Also, set light plants
and rack 231 jts 4 ½” 11.6# P110 LTC. Will move in Baker seal assembly,
subs, casing crew and pick-up machine in the AM. SDFTD 2:00pm
MIRU
Jody Linthicum
Fail Date AFE #: CB-1408
Start Date 3/6/2015 AFE $:
End Date Foreman: Jody Linthicum
Service Co. Basic Energy Bob Dimit
Use Drop Down: Art Linthicum
WS Reason
Type of Failure
Cause of Failure 1
Cause of Failure 2
Failed Item
Failed Part
Type In Data:
Size/Grade
Brand
Coating
Area Failed
Failure Depth
Description
Well Service Report
Original Completion of Well
Orig Completion
fluid type fluid type fluid type fluid type Proppant Name Proppant Name
Show amount
used in barrels
Gallons -
Autocalculated
Show amount
used in barrels
Gallons -
Autocalculated
Show amount
used in lbs
Show amount
used in lbs
1 0 0 0 - 676
2 0 0 0 - 608
3 0 0 0 - 582
4 0 0 0 - 523
5 0 0 0 - 320
6 0 0 0 -
7 0 0 0 -
8 0 0 0 -
9 0 0 0 -
10 0 0 0 -
11 0 0 0 -
12 0 0 0 -
13 0 0 0 -
14 0 0 0 -
Avg.
Rate
(bpm)
Stage # Formation NamePerfs - Each Interval /
Display in feet
Plug Set
depth /
Display
depth in
feet
Openin
g WHP
(psi)
Break
Down
(psi)
ISIP
(psi)
15 Min.
SIP
(psi)
Max
Press
(psi)
Avg.
Press
(psi)
Max
Rate
(bpm)
Break
Rate
(bpm)
FG
psi/ft
Total Acid
(bbls)
Total Acid
(gallons -
autocalc)
Propp
.
Concn
. Min
(ppg)
Propp
.
Concn
. Max
(ppg)
TOTAL Load to
Recover (bbls)10# Linear 10# Linear 20# Xlinked 20# Xlinked
20/40
Ottowa
20/40 Super
LCTotal Proppant
(lbs - autocalc)
15 0 0 0 -
16 0 0 0 -
17 0 0 0 -
18 0 0 0 -
19 0 0 0 -
20 0 0 0 -
21 0 0 0 -
22 0 0 0 -
0 0 0 2,709
Tally Length Depth
Tally Length Depth
Tally Length DepthCasing Tally
Rod Description
Tubing Description