Compressor Vibration Problems Due to Changed Gas ...

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Purdue University Purdue e-Pubs International Compressor Engineering Conference School of Mechanical Engineering 1986 Compressor Vibration Problems Due to Changed Gas Composition - A Case Study S. N. Dwivedi Follow this and additional works at: hps://docs.lib.purdue.edu/icec is document has been made available through Purdue e-Pubs, a service of the Purdue University Libraries. Please contact [email protected] for additional information. Complete proceedings may be acquired in print and on CD-ROM directly from the Ray W. Herrick Laboratories at hps://engineering.purdue.edu/ Herrick/Events/orderlit.html Dwivedi, S. N., "Compressor Vibration Problems Due to Changed Gas Composition - A Case Study" (1986). International Compressor Engineering Conference. Paper 579. hps://docs.lib.purdue.edu/icec/579

Transcript of Compressor Vibration Problems Due to Changed Gas ...

Page 1: Compressor Vibration Problems Due to Changed Gas ...

Purdue UniversityPurdue e-Pubs

International Compressor Engineering Conference School of Mechanical Engineering

1986

Compressor Vibration Problems Due to ChangedGas Composition - A Case StudyS. N. Dwivedi

Follow this and additional works at: https://docs.lib.purdue.edu/icec

This document has been made available through Purdue e-Pubs, a service of the Purdue University Libraries. Please contact [email protected] foradditional information.Complete proceedings may be acquired in print and on CD-ROM directly from the Ray W. Herrick Laboratories at https://engineering.purdue.edu/Herrick/Events/orderlit.html

Dwivedi, S. N., "Compressor Vibration Problems Due to Changed Gas Composition - A Case Study" (1986). International CompressorEngineering Conference. Paper 579.https://docs.lib.purdue.edu/icec/579

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C<J.IPRESS0a VIBRATION PRCI3LEh6 DUE TO Cl!ANGEJ G,\S CCillPCSITION 1\ 'CASE STIJ!JY

S.N. DlfiVEDI

DY • MAllAGER - COL'IPRESSOR DESIG:~ Bi-IARAT PUI.IPS & COMPR2SSOl15 LTD. llAINI'- ALlAHABAD 211010 {INDIA)

AB~~f'CT ~ •'.';'," ·1, >'h•

The importance of specifying the exact range of gas composition that a·· cor:lpressor is required to handle is sometimes under­eitima ted. This situation often leads to severe problems, particular! y if the variation happens to be wide enough.'

The present paper discusses a case study of vibration problems faced on a multi-stage neciprocating compressor handling a · complex mixture of hydrocarbons. The vibrations were so severe that the compress-or could not be run continuously.

Thorough investigations into the causes of such severe vibrations led to the conclusion ti1at the problems were due to changed gas composition. The ,.,etnodology of investigations~· analysis and further solution of the problem resulting into· successful running of these compressors are presented in this paper.-

The paper concludes with an appeal to all compressor users and'consultants to specify as far as possible a realistic gas c·o171position and in case there is any change later to inform the compressor manufacturer for carrying out an analysis of the changed gas composition so as to enable them incorporate nece­ssary changes to ensure trouble-free running of c~ressor •

.mJRODUGTICN

Reciprocating coi.!pressors· generate flow pulsations which in turn give rise to press-ure pulsations. The reciprocating motion of the compressor piston·generates the basic fundamental pulsation frequency corresponding to the compressor speed and passage of the gas through compressor valves gives rise to higher· pulsation frequencies or harmonics corresponding to multiples of compressor ·speed;'

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The final build-up of amplitudes of individual pulsation compo­nents is controlled by the effects of the manifold and the piping system attached to the compressor. These pulsations sometirres get coupled to the mechanical system at points such as closed ends of vessels or pipes, bends, orifices, reducers, etc. to produce acoustic shaking forces. These acoustical shaking forces excite vibrations, the magnitude of which depends upon the location of mechanical natural frequencies relative to the frequencies of acoustical shaking forces and the amount of damping in the mechanical system.

The level of pulsations generated by a compressor, is related to a number of parameters which include compressor operating pressures, compression ratio, cylinder clearance volumes, phasing between cylinders, thermodynamic gas properties and COJ!llressor cylinder and valve design. These pulsations are further anpli­fied by the attached piping systems. The consequant vibrations depends upon the acoustical and mechanical characteristics of the vessels and piping systems.

Gas composition is one of the most important parameters that must be exactly specified by the cOQpress-or user. Severe problems may arise in case the actual gas composition is widely different from that specified. The present paper discusses a case s"b.I dy of viliration prdJ lems faced on a r:~ulti-stage Recipro­cating compressor handling a complex mixture of hydrocarbons.

THE COMPfi.ESSOR

The compressor involved was a three-stage Il.eciprocating Compressor cO!ilpressing associated gas having composition as per Table 1 (as indicated by client in their order) from a suction pressure of 1.068 Kg/em'" absolute to a discharge pressure of 51.533 Kg./cml'. abs. The scteroo of compression is shown in Fig 1.

Tm compressor was designed to handle specified gas and the design was also checked by Analog study as per design approach 3 of API 618 - 1974, and modifications as required during study were incorporated in the final design. It was expected that this design should result in a trouble-free performance of the subject co~ressor.

THE VIBRATIOn PHCBLEJ,\

When the stbject co::tprossor was installed and corru:lissioned on 9roccss gas, it n<ls observeJ that there were heavy vibrations on 2nd stage cylinders and related suction and discharge danp­ners. These vilirations resulted into frequent failu:ms of cooling I'Jat.Gr piping connected to 2nd stage cylinders.

A thorough investigation was carried out to establish the causes of these severe vibrations. Vibration rneasu:rements were taken at various locations with the help of B&K and IRD rnech­analysis instrumentation.

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A typical vibration measurement record is sham in table 2 and typical "vibration spectra aro shown in figs. 3, 4 and 5. (Fig. 2 shons locations of measurer:ent points).'

The vibration readings and also the vibration spectrum sugg­ested a pre-dominance of 6th harr:1onic {i.e. around 2000 rpm -the compressor speed being 333 rpm). Dased on these observations it was concluded that the underlying cause of these vibrations "is ;rela~ed to some sort of acoustic rosonance and the consequently high shal-.ing forces inside 2nd stage suction and discharge dampners.'

THE GAS COMPCS IT ION

At this stage of investigations the actual gas co~position of the gas being handled by the compressor was checked. It was oi?served that there I'Jas a wide v;nriation in tha actual gas composition from that specified by client at the time of order, wpi9h was used for design.

Thus it was concluded that the real reason for the sUbject vibration probler.Js was the dange in the co::1position of gas being handled, which resulted into generation of high frequency s_haki~g for'ces with consequent forced vibrations of the compressor cylinders, and vess.:Jls, particularly of the sac·ond stage. \lith the initial gas co:~positi.on the shal:ing farces on various v:ol~ b9ti;les were having ver}' lo1·J values {refer to table 3 ) which were not expected to cause any undue vibrations and as such no internals weJ.·e anticipated for force balancing in these vessels.

However, due to the changed gas composition and the resulting changes in the acoustic behaviour of the gas :aixture, the · subject dampners of 2nd stage suction and discharge respectively were subjected to high unbalanced forces of 6th harr.1onic and this was the reason of vibrations of the second stage cylinders and -vessals.

THE SOLi.JTIOl!

As a first step towar::ls solution of the prohlems, the clients 1·1ere convinced about the role of gas composition in this vibration problem. The client as a result ~ade detailed investigations into the ac-:;ual ilnd possible gas cor~:;.osition at this site. Ultimately, the client specified a \'tide range of gas C03position that could possibl"f be involved during the running of stbject comp1·ess-ors over years. · (Ref. table 4)

The manufacturers, than endeavoured to rnke suitable modifica­tions in the design of the st.bject compressors so as to take care of this nel•tly specified ranga of gas composition. It was bpractical to have a detail-ed anal1tical study inclusive of Analog study, botl;l because of the huge variety of possibilities of different combinations of gas mixtUJ:e.s being involved in the wide rq_nge of gas composition sp~cified by cliGnt all:l as well because of the prohibitive costs and time required for such an

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analytical stlldy.

In view of above it was decided to adopt a qualitative solu­tion, that was well proven by manufactur·:'!r's experience and as such :lnte:~.·nals •acre dcdgned and introduce:J in suction and discharge vassals of 2nd stage and also suction vessel of 3rd stage, for force balancing of these vessels over a wide range of gas composition as specified by the client. This solution involves shifting pulsation origination ~oint insiJ:! a d<J.npno:r, approldrni..lbly to the central location so that the !JUlsations travel path to both ends of tho vessels equalize and conseque­ntly ti-e shaking forces are reduced to a minimum. This solution is equally useful at all possible aas conposition.

The compressors \'Jere run successfully after these vibrations and the overall vibration level was reduced to safe limits. (Refer Table 5) These compressors have alraady ragistered more than 8000 hrs. of cur.unulative wn without any further probleos.

CONCLUSia·l

The author wish:ls to r.n:<e an appeal to all compressors users to appreciate the iiif!ortance of ~cifying exact gas composition range for the service involved. This allons tlw conpressor desisner to take care oi the whole range while maintaining opti­mum perfo:cr:ance of the compress-or. Any inaccurate specificat­ion of the range of gas compos:.tion, r;~a:r lead to troubles and costly do:mtirre, as in the case illustrated here.

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.lliJTIAL GA5 CWPCSITIOH

The conpre3s-ors shall haQlle Gas 1 from 1st to 3rd stg and Gas 2 from 2nd to 3rd stage. Tho gas compositions (f.lol ;;) of Gas 1 and 3as 2 are as follows:

Case I casa II ---Coq:> o_':= nt Gas l Gas 2 Gas 1 Gas 2

C02 2.71 3.01 2.81 3.01

C1 14.74 54.20 15.11 54.20

C2 21.52 20.74 22.10 20.74

C3 31.76 13.79 31.19 13.79

IC4 6.30 2.14 6.50 2.14

NC4 10.90 3.16 10.46 3.16

IC5 2.99 o.7s 2.91 o.1s NC5 o.7o o.19 0.70 0.19

C6 + 7.89 1.99 8.22 1.90

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TABLE 2 VIBRATICl'l lviE.ASUHEMENTS BY B&K INSTRUMENIS (mcnms PEAK TO PEAK)

LCCA- 1ST STG CYL 1ST STG CYL II ZIG CYL II STG CYL III STG C'll TIO!l {PUt.iP SIDE) (MOTOR SIDE) (PUMP SIDE) (MOTOR SIDE)

Overall Major Peaks Overall Major Peaks Olrerall Major Peaks Cbserved Cbserved Ci>served

A 'A 100 100 220 70 at1xRPM 180 70 atlxRPM 230 160 at lxRPM. 110 atlxRPM 80 at6x!FM 40 at 6xRPM

BJ< - - 180 50 atlxRPM 140 - 120 65 at6xRPM

Cz 45 40 360 65 atlxRPM 340 75 at1xRPM 220 70 at 1xRPM 280 at6xRPM 280 at6xRPM 80 at 6xRPM

'-0 130 at 9xRPM tv co

D,z; - - 260 - 240 - 160

Ey 180 185 280 220 at lxRPM 240 - 340 300 at 1xRP!.I 80 at 6xRPM 43 at BxflPf,!

Fy 240 240 550 95 at 1xRPM 500 - 400 85 at lxRPM 360 at 6xRPM 50 at 3xRPM

300 at 8xRPM

!:!QI[: lf.ea sure~nt locations as shown in fig. 2 • RPM = 333.

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TABLe 3_

SHAKING HRCES m CO.:P~SSCR DA.'.1PEN!!f!S ( BASED ON It!ITIAL GAS CO!.IPCBITION )

I STG. SUCTION DAMPHER {Dl) II STI;. DISCHAaJE DAMPNER (02) III STG. SUCTICl-l DAMPNER {03) II STG DISCHARGE DAUPNER (D4) III STG SUCTION DAMPNER (05) III STG DISCHARGE DAMPNl:!R {06)

; ± 510 lit : .± 300 ~ I .± 56Dfi. I .± 520li I .± 595 \ 1 .±Negligible.

TABLE 4

FINAL RAi'K;E CF GAS CCl:lPCSITIOH (MOLE PERCENT)

COMPO- FIRST SUCTI Olt SEGCND SUCTim THIRD sucrrrn NENT (Press. 1.068 (Press. 4.013 (Press. 15

,Ycrniabs.) J¢/cm'-a) lfj/cm2- a)

C02 2.51 - 3.71 2.81 - 3.63 3.21 - 4.03 Cl 20.04 - 44.11 34.06 - 48.62 38.83 - 50.10 C2 13~:.W - 23.00 15.45 - 21.59 16.87 - 23.70 C3 18.70 - 28.20 17.20 - 22.60 17.20 - 22.65 IC4 3.70 - 4.47 2.62 - 3.57 2.54 - 3.01 NC4 3.24 - 5.04 2.30 - 4.:31 2.63 - 3.33 IQ) 0.39 - 0.74 o.33 - 0.54 0.27 - 0.33 NQ) 0.30 - o.63 0.26 - 0.49 0.19 - o.24 NC6 0.12 - Q.28 0.10 - 0.17 o.b4 - o.o7 NC7 o.o1 - o.o3 o.o1 - o.o1 o.oo - o.oo2 CB + 6.33 - 18.98 5.72 - 12.58 3.85 4.97

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I STG CYL. I STG CYL. II STG CYL. II STG CYL. (PU~'.iP 3IDS) (hlOTCR SIDE) {PUI.JP SIDE) (/J!OTOR SIDE)

X 110 lC) 180 150

y 180 185 300 330

z 45 40 360 340

" 140 110 110 100 ,,

y 220 200 220 200

z 60 60 80 100

X axis is along crank-shaft axis. Y axis is along cylinder axis. z axis is along vertical axis.

III STI3 CYL.

230

340

220

100

340

130