Simulation of Free Chlorine Decay and Adaptive Chlorine Dosing
Chlorine Emission Presentation-New
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Transcript of Chlorine Emission Presentation-New
7/30/2019 Chlorine Emission Presentation-New
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IPCLGandhar Petrochemicals Complex
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Location of Chlorine Vent
Wind Directi
NE to SW
Wind Spee
9 Km/Hr
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GANDHAR COMPLEX - PRODUCT FLOW DIAGRAM
Salt
Semi-RichGas
(from GAIL)
C2 C3
SeparationPlant
C2 C3
Mixture
GasCracker
Plant Ethylene
EDC / VCMPlant
Chlorine
Chlor-Alkali
Plant
VCM
PVC
Plant
HDPE
Plant
HCL
CausticSoda Flakes
Caustic
Soda Lye
Caustic Soda
Prill
Lean Gas EO/EG
Plant
PVC
EthyleneOxide
Ethylene
Glycol
HDPE
Raw Material ProductsIntermediate
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IPCL - CHLOR ALKALI PLANT
Capacity
Caustic : 460.00 TPD Chlorine : 400..00 TPD
Major Sections :
Primary Brine : Preparation of Brine
Secondary Brine : Purification of Brine
Cell House : Electrolysis of Brine
Chlorine : Compression and Liquifaction of Chlorine
CEU / CCU : Concentration of Caustic Soda
M/s UHDE Membrane Cell TechnologyDate of Commissioning : 01 Apr 1997
On line Use.
Licensed Storage Capacity - 460.00 MT
At no Time stored More than 40.00 T
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Salt
DM Water
BrinePreparation
BrinePurification
Electrolsysis
Power
Chlorine Treatment :
Drying, Compression,
Liquifaction
Chlorine Gas to
VCM
Chlorine
Evaporation
HydrogenChlorine
Caustic Soda
Schematic Diagram Of Process
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Function Of Hypo Section :
To Neutralize The Waste Chlorine Gases From The Plant
Areas With Caustic Soda And Make Sodium Hypo
Chlorite
Hypo Section : Part of Chlorine Section
Normal Capacity :750 Kg/Hr of Chlorine
Emergency Handling Capacity:3.00 Tons of Chlorine in
10 min - Neutralizing Capacity for Plant full Load
Design Capacity – Hypo Section
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Schematic of Hypo System
Waste
Chlorine
18 mHeight
Vent
Caustic
Over Head
Tank
Suction
Tank I
Suction
Tank II
Pump Pump
Chlorine Emission
Faulty RedoxMeter
Final Scrubber
Estimated Chlorine
Release : 26.00 Kg
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Date of Occurrence
of Incident : 20 – 12 - 2002
Time : 21:05 Hr
First Information of Leak :
Report of Chlorine Smell By Other Plants And
By People From Jageshwar Village - Due to
Wind Direction
Immediate Action TakenThe plant was Stopped Immediately within 8
minutes. All The Chlorine System Was Isolated
And Thorough Check Of All Pressurized
Chlorine System was done by Ammonia
Plant Was Under Shut Down Since Morning For Routine
Maintenance. Restarted at 19:00 Hr. Under Stabilization at
The Time Of Incidence
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Chronology Of Events
Plant Re-Start Up : 17:00 Hr
HCl Furnace Start up : 19:40 Hr
First Report Of Smell : 21:05 Hr
Plant Load Reduction : 21:05 Hr
Complete Check Up Of All Areas Of The Plant. No identifiable leak could be
found
Plant Shut Down Was Taken At 21:29 Hr
Senior People Of IPCL Visited The Site Along With Fire And Safety Personnel
No Chlorine Smell Could Be Found
Thorough Checking Of Pressurized Chlorine Equipment With Ammonia For
Any Leaks
Follow Up Actoins
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Ambulance / Fire Services / Security people visited Plant at 21:30 HrVillagers Arrived and Treatment Given At OHC. Doctors From Nearby
Industries Called For Help
Transport Section Was Alerted To Keep Vehicles Ready If Evacuation
Is Required
RGSS Personnel Were Posted At OHC To Help The Villagers Coming
For Treatment
Since Dahej Telephone Exchange Was Down, Angareshwar Pump
Station Was Contacted To Give Messages to ED -GC and GM -O At
22:00 Hr
WTD At Baroda Was Informed Using M/s Dodsal Communication
System At 22:00 Hr
At 23:00 Hr Senior Executives Of IPCL Visited The Complex And
Jageshwar And No Chlorine Smell Could Be Found
On-Site Emergency Actions
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Message Was Conveyed To Senior Factory Inspector, Bharuch And
Officer Of GPCB At Bharuch By 23:00 Hr. They Arrive At 01:30 Hr
Police Authorities From Dahej Police Station Also Arrive To AssessThe Situation
Between 01:30 Hr and 03:30 Hr GPCB Officials Vistied The Complex
And Jageshwar Village. No Chlorine Smell Found. Nil Reading on
Detection Tube
Total Of 335 Villagers Were Given Treatment For Cough And Throat
Irritation And Released The Same Night
Eight People Were Sent To Bharuch For Close Observation
Doctors Visited Jageshwar Village Daily For 7 Days For PreventiveHealth Check UP
No Fatal Injury In The Incident
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Limitations Which Influenced the Occurrence
of the incident :
Low Concentration Of Caustic in The
Suction Tank -Scrubbing Tank
Effective Low Volume of the Over Head Tank
Off-Line of Suction Tank I due to Maintenance
Faulty Indication Of Redox Meter
Gas Detector In the Opposite Direction Of Wind
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Actions Taken Before Re-start of the Plant
All the instruments of Hypo System Were Checked
And Calibrated
Concentration Of Caustic in The Over Head Tank
Increased to Increase the Caustic Concentration
Dosed to Suction Tanks
Taking in line Of Hypo Suction Tank I Also
Installation of One Gas Detector Near to The HypoVent Stack
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Actions Taken to Prevent Recurrence of the
Incident :
SOP of Hypo System Was Revised To Meet TheIncreased Safety in Operation
To Keep Both The Suction Tanks Always in Line
Additional Two Chlorine Sensors -Total 3
With Hooter in DCS And Recording Provided Near The
Chlorine Vent
Replacement of Caustic Head Tank
Regular Sampling of Gas Coming Out of The Vent
Installation of additional Redox Meters in The Suction
Tank
Provision of Chlorine Gas Sensors in Other Locations inthe Vicinity - Complex Boundary Near Village
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Actions Taken to Increase Awareness and Integrity
Additional Siren Installed On Complex Boundary Near
Village Jageshwar
Regular Ambient Air Monitoring is Carried Out In theVillage
Windsocks Provided in The Surrounding Village
Review / Rehearsal Of Onsite Emergency Plan
Interaction With Nearby Industries At Working Level
Improving External Communication System
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Actions Taken to Increase Awareness and Integrity
Safety Audits by Internal And External Agencies At
Regular Intervals
Discussions with Chlor – Alkali Industries to reach the root
cause for this Incidence
Discussions with UIL – Mumbai our Technology Licencors
to Review our SOPs for the Plant Operations
Plant Audit done by RIL- Safety Team to review our
Infrastructure Requirements for safe Plant Operations so as
to avoid Reoccurrence of such incidence
Safety Audit done by Euro – Chlor Belgium to review our
Infrastructure Requirements for safe Plant Operations so as
to avoid Reoccurrence of such incidence
Meeting with Neighboring industries as a confidenceBuilding Measure in Our Safety Management System.
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We are confident from the Lessons learnt from
the accident and the follow up action we have
undertaken.We are sure that the chances of reoccurrence of such Incidence are non - Existent
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We are confident from the Lessons learnt from
the accident and the follow up action we have
undertaken.We are sure that the chances of reoccurrence of such Incidence are non - Existent