Casting manufacturing process improvement
-
Upload
abdullah-ansari -
Category
Technology
-
view
1.191 -
download
0
description
Transcript of Casting manufacturing process improvement
Abdullah Ansari
Casting Direct Pass Ratio Improvement
(Macro Report)At SUPPLIER – India
Duration Jan-2009 to Mar-2011Project Leader – Abdullah Ansari (ASQ CSSBB)
Team members – Seenivasa RagavanSenthil NathanChirag PanchalVicky Dongade
Dhaval Vyas
Background
• Involvement– In Dec-2008 CUSTOMER Supplier Quality received information that
SUPPLIER has started manufacturing castings for CUSTOMER– CUSTOMER SQM got involved for routine inspections and setting up
system for material clearance from SUPPLIER to CUSTOMER– 2 member team Abdullah Ansari & another member visited SUPPLIER
in Dec-2008 for system assessment & inspections.
Castings produced in first phase and status in nutshell
0
20
40
60
80
Qty
Produced 26 18 60 13 2 10 12
Rejected 26 18 60 13 2 10 12
Yet to be checked 0 0 0 0 0 0 0
2.1 MW Main Beam
2.1MW Main Beam
2.1MW Cross
2.1MW Hub body
2.1MW Main Frame
1.5 Main Beam
1.5 Cross Beam
Major Reasons for non-acceptance Casting Defects
DrossPorositiesBlow holesFailed in Mechanical properties
VisualPoor surfaceMismatch
Dimensions
Casting Acceptance – Pre Project Status
For castings produced in First phase prior to 31 Dec 2008
Direct Pass Ratio – ZERO 0%
Define: Project Kick-off
• Project Scope – To participate with Team of SUPPLIER in developing fully finished
casting components for CUSTOMER WTGs– Castings acceptable to global standards such as EN1563, EN12680 etc
• Team– Abdullah Ansari – Project Leader CSSBB-ASQ & SPOC from CUSTOMER– Seenivasa Ragavan – SUPPLIER QA Head– Senthil Nathan – NDT Expert– R. Subramanian – Inspection & Testing– Chirag Panchal – Analyst– Vicky Dongade – Analyst– Dhaval Vyas – Analyst
Define: Strategic Planning
• Component Prioritization– Hub body & Main Frames are heavy section castings, CUSTOMER running short
of supplies – Priority with Average weight per piece 12MT– Small castings such as main beam, cross beams analyzed thru make or buy
matrix. Found suitable to be bought from other source than SUPPLIER• Core Tool
– Plan – Do – Check – Act (PDCA) at each stage– Various tools as per applicability e.g. Pareto, trend chart, FMEA, CE matrix
• Key Measurement– Direct pass Ratio wrt to Inspected– Why Direct pass Ratio only to be measured?
• Direct indicator of acceptance/scrap• Gives indication of process & action effectiveness• Doesn’t count parts accepted under deviation• Triggers prioritization & further detailing on which part/defects actions to be
initiated.
Define: Generic Process Flow
Pattern & core box
Raw Material Receipt Molding Core making
Mold assemblyMeltingMagnesium TreatmentPouring
Knockout Fettling & Shot blasting
Destructive & Preliminary
NDT
Machining & Inspection
Non Destructive
Testing
Surface preparation &
Coating
Coating Inspection
Packing & Forwarding
Measure & analyze
• Old Casting Data– Old castings rejected for multiple defects are around 141nos– Now prioritized castings are Main Frame & hub body, amount to 13
Nos out of 141nos.– Castings were mainly rejected because of
• Failed in tensile• Failed in impact• Failed in Nodularity• Failed in visual acceptance• Failed in Ultrasonic inspection• Failed in Magnetic particle inspection• Failed in as cast dimensions• Failed in Machined dimensions
Analyze: Casting Process Control
Sr. No Process Stage Key controls Output
1 Receipt Inspection Receiving inspection of all major raw material.
Inspected and certified raw material for production.
2 Sand mixing Ratio of new/old sand, ratio of resin and catalyst
Quality sand with required bonding properties.
3 Core making Ramming to ensure fully filled core. Core without any cracks and damages.
4 Molding Ramming to ensure fully filled core. Mold without any cracks and damages.
5 Mold closing Alignment of cope and drag by locating pin. Vent provision for gases
Closed mold ready for pouring without any damage & with required cavities
6 Melting C, Si & CE and spectro analysis, Liquid metal temperature
Liquid metal with required chemistry ready for Mg treatment
7 Mg treatment Ramming of Mg alloy and covering Mg treated metal in required quantity and quality
8 Pouring Pouring should finish within prescribed time after treatment, metal temperature Poured mold
9 Knockout Cooling time to be maintained for each item Casting with runner & risers.
10 Cleaning & Fettling Manual operations Dressed casting, ready for machining.
Analyze: Cause & Effect Matrix (Casting)
10 10 10 7 10 8 8 101 2 3 4 5 6 7 8
Tens
ile
Impa
ct
Nod
ular
ity
Visu
al
Ultr
ason
ic Q
ualit
y
Mag
netic
Pa
rticle
As ca
st
dim
ensio
n
Mac
hine
d Di
m.
Tota
l
1 Molding Gating system 8 10 8 8 3002 Melting & pouring Chemical composition 8 8 8 2403 Molding Sand mixing ratio 8 8 8 2004 Melting & pouring Time to pour after Mg treatment 8 10 1805 Molding Chills 6 8 6 1706 Melting & pouring Residual Mg 8 8 1607 Knockout Time to Casting cooling 8 8 1608 Melting & pouring Deslagging 10 8 1509 Melting & pouring Pouring temperature 8 8 136
10 Molding Venting 8 6 12811 Melting & pouring Inoculation 8 6 12212 Melting & pouring Treatment temperature 8 8013 Molding Refractory painting 8 56
Rating of Importance to Customer
Sr. No Process InputsProcess Step
Analyze: Cause & Effect Pareto (Casting)
Gati
ng s
yste
m
Chem
ical
com
posi
tion
Sand
mix
ing
ratio
Tim
e to
pou
r aft
er M
g tr
eatm
ent
Chill
s
Resi
dual
Mg
Tim
e to
Cas
ting
cool
ing
Des
lagg
ing
Pour
ing
tem
pera
ture
Venti
ng
Inoc
ulati
on
Trea
tmen
t tem
pera
ture
Refr
acto
ry p
ainti
ng
050
100150200250300350
Cause & Effect Matrix
Cause
Effec
t Sco
re
Improve – Actions Taken (on Casting)Improvement Need Score Actions Tool To address issue of
Gating system 300Correction in ingate size, Runners & Risers
Magma Simulations for mold filling & solidification
Visual, UT, As cast, Machined
Chemical composition 240 Establishment of charge mix DOE, Regression Tensile, Impact, nodularity
Sand mixing ratio 200 Sand mixingControl plan for mixing ratio of sand, resin & hardnere
Visual, As cast, Machined
Time to pour after Mg treatment
180Establish time range to be followed
DOE Impact, Nodularity
Chills 170 Fixing chill positions & sizesMagma Simulations for mold filling & solidification
Visual, UT, MPI
Residual Mg 160 Establishment of charge mix DOE, Regression Impact, Nodularity
Time to Casting cooling 160Establish time range to be followed
Generic recommendation & trials Tensile, Impact
Deslagging 150Establish Deslager quality & training
Supplier development & training Visual, UT
Pouring temperature 136 Establish temperature range Generic recommendation & trials Nodularity,Visual
Venting 128Correction in ingate size, Runners & Risers
Magma Simulations for mold filling & solidification
UT, MPI
Inoculation 122 Establishment of charge mix DOE, Regression Nodularity,Visual
Treatment temperature 80 Establish temperature range Generic recommendation & trials Nodularity
Refractory painting 56 Even coated film on mold Training Visual
Improve – Actions Taken Summary (Overall)
Sr Issue Actions for improvement
1 Skill enhancement Establishment of Quality System & training
2 Process Control FMEA, Control plan, Process adherence audits
3 Casting Defects Raw material combinations, Process control
HR On the job trainings, Process redesign
class room trainings on International Standards
4 Machining Explanations on drawing & specifications
5 Corrosion Protection Coating specifications, acceptance criteria, training
6 Packaging Development of specification & prototyping
7 Tracking Establishment of tracking mechanism for each castings
8 Inspection & testing Establish testing laboratory & right practices
Improvement Trend
09-10 Q1 09-10 Q2 09-10 Q3 09-10 Q4 10-11 Q1 10-11 Q2 10-11 Q3 10-11 Q4
Direct Pass %
17.6470588235294
6.66666666666667
53.757225433526
61.75 74.2603550295858
73.7430167597766
82.6887661141802
93.3649289099526
5.00
15.00
25.00
35.00
45.00
55.00
65.00
75.00
85.00
95.00
Direct Pass Ratio over 8 Quarters
Dire
ct P
ass %
Take Away of Project - Quality
Supplier ISO certified & Quality culture established Trained & Skilled human resource Control parameter establishment thru FMEA Technical Register for melting Inspection & test procedures Lessons learned for defects & causes Knowledge of errors in testing leading to flaws in acceptance Process for Corrosion protection & acceptance criteria Validated Packing guidelines Tracking mechanism of each individual component Ongoing measurement of process adherence index Ongoing measurement of Direct Pass Ratio All components PPAP completed
Take away of Project - Commercial
SUPPLIER 1st Indian Supplier to develop & supply >80% of CUSTOMER requirements of hub & main frame castings in fully finished condition
During Project at SUPPLIER, important numbers (Cummulative) [Average Casting weight considered-12MT]– Details Qty. Weight %– Castings Produced : 2653 Nos. 31836 MT 100– Castings Direct OK : 1859 Nos. 22308 MT 70– Castings Conc OK : 288 Nos. 3456 MT 11– Castings Rejected : 506 Nos. 6072 MT 19
Castings direct OK in last quarter of Project – 93.36% Development at SUPPLIER
– Main Frame & Hub for all CUSTOMER WTG models, Total 4 models
Important Numbers
During Project:Castings Produced :2653 Nos.Castings Direct OK :1859 Nos.Castings Conc OK : 288 Nos.Castings Rejected : 506 Nos.DPR % @project handover:93.3
4 quarters data after project handoverCastings Produced :1251 Nos.Castings Direct OK :1102 Nos.Castings Conc OK : 08 Nos.Castings Rejected : 42 Nos.Castings WIP: 99 Nos.DPR % @ Q4 FY11-12:97.2
Effectiveness of Project
More than 15000 Metric Ton of castings produced after project with DPR more than 93.3 consistently
Abdullah Ansari
The search for excellence is never ending…
Thank You