149 Cooling Water treatment-a csae study_Chembond_149.pdf

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    IMPORTANCE OF COOLING WATER TREATMENT WITH RESPECT TO WATERCONSERVATION THROUGH VARIOUS TREATMENT ALTERNATIVES AVAILABLE FORLOW AND HIGHER COC(CYCLES OF CONCENTRATION) WITH COST EFFCTIVE

    PERFORMANCE,MONITORING AND CONTROLS.

    Looking into the present scenario of increasing demand of water and the

    depleting water tables we as a prudent human being really need to workextensively so that we take care of our present demand and the progenies in

    the future. As the water is the necessity of all the industries spec ially the Power

    industry. We can use water in a more cost effective manner means of output

    with lesser inputs. The higher Cycles of operation in the c irculating water which

    not only saves water but also reduces the effective cost of cooling water

    treatment and in turn water usages. A few case studies are being given

    hereunder discussing various problems and their solutions regarding the water

    chemistry with successful implementation.

    With the latest developments in the field we can operate the cooling water atvery high cycles of concentrations without any impact on performance.

    1. CASE STUDIES ON A BRACKISH WATER SYSTEM OF STATE ELECTRICITY BOARD WITH

    EFFECTIVE CONDENSER PERFORMANCE BY HIGH STRESS POLYMER TECHNOLOGY

    AND LATEST OXIDATIVE ALTERNATIVES FOR THOROUGH MICROBIOLOGICAL

    CONTROL.

    High TDS load in brackish water cooling system is a major concern in all

    industrial cooling water system, particularly in power plants where the

    condenser utilizes large quantities of such water. The performance of the

    condenser is affected by the fouling /deposition in the cooling water tubescausing reduced heat transfer rates and drop in vacuum, leading to plant

    load limitation. This has an adverse impact on the overall operating costs apart

    from adding to the damage caused by an already precarious power situation

    in the country. Appropriate mechanical design and application of advanced

    high performance polymer treatment minimizes the deposition and improves

    the condenser performance, there by reducing the cost of operation. This

    case study in a 75x3MW power plant in Western India where proper program

    selection as well as effective application, monitoring and control, helped in

    improving the condenser performance restoring power generation.

    Background

    Deposition and fouling in the condenser were major problems faced by the

    75x3MW power plant using brackish water for condenser cooling. Each unit is

    catered to by a dedicated cooling tower ie, three cooling towers for the three

    units. Improper water treatment had caused deposition in the condenser,

    leading to a drop in the vacuum and eventually affecting the plant load. This

    necessitated the use of two cooling towers with an additional pump to run one

    unit, there by increasing the cost of operation. In this arrangement, condenser

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    vacuum in a single running unit was around 0.78 kg /cm2 and the plant load

    was about 68MW.

    After evaluating the water quality, Ashland Drews computer aided program

    evaluation software On Guard TM model was used to identify the limiting

    factors and select the proper chemistry required to address the issue.

    Chembond Drewtreat Limited, a joint venture between Chembond Chemicals

    Limited (India) and Ashland Spec iality Chemicals, USA, was entrusted withpackage treatment program to improve the condenser performance and

    monitor the treatment program.

    Effectively Controlling Deposition Chemical Treatment Methods

    The traditional method of using a regular Phosphonate- compound with

    chlorine to control the deposition was found to be ineffective for the brackish

    water quality as make up to the cooling water system. Awareness about the

    importance of using advanced high- performance polymer in a total

    treatment package becomes necessary as:

    Traditional polymers with phosphate are unable to restrict the

    precipitation of dissolved solids on the heat transfer surfaces, in spite of

    the noble- metallurgies employed.

    Chlorine on its own in unable to prevent the formation of biofilm in the

    absence of a biodispersant. This results in fouling in the system and

    affects heat transfer

    Proper control and monitoring of the water parameters enhances

    system cleanliness

    Consequently, Chembond Drewtreat Limited utilized Ashlands computer

    aided program evaluation software On Guard TM to identify the limiting

    factors and select a proper treatment program to overcome them. The On

    Guard TM results indicated that the brackish water quality being used as

    make up to the cooling tower required the use of advanced high-

    performance polymers to address prec ipitation of dissolved solids, espec ially

    iron and CaC O3.

    The results are as follows:

    The formation of carbonate alkalinity leads to the deposition of calciumand magnesium carbonate in the cooling water system. This is more

    predominant in brackish water where the concentration of calcium and

    magnesium is very high. Hence, it is desirable to control the pH of the

    circulating water in the range where potential for carbonate alkalinity is

    minimized, which in this case is less than 7.8pH

    Based on the modelling, the On Guard TM, which recommends the use of

    spec ific technologies for selected water chemistry, the program identified the

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    use of advanced organophosphonate in combination with high-performance

    polymers to be used for the brackish water treatment.

    The program selected consisted of:

    Antiscalant: advanced organophosphonate based product to

    maintain residual as per the computer modelling of 0.3ppm to control

    calcium carbonate scale. High performance polymer 1: the high performance co-polymer residual

    requirement for calcium phosphate and C aSO4 dispersion/Scale

    control, as per the computerized modelling when used alone is around

    0.7.

    High performance polymer-2: the high-performance Ter-polymer residual

    requirement to control deposition of silica and iron fouling, as per the

    computerized modeling when used alone is around 0.2.

    Copper inhibitor oxidant-stable Azole- based product to maintain a

    residual of 0.7ppm is used to control copper corrosion.

    Enhancing the efficiency of chlorineA bio- dispersant should be added in combination with high performance

    polymer program to assist in penetrating the exoploymer protective coating of

    the biofilms. This allows efficient diffusion of micro bioc ides like chlorine in to the

    biomass.

    Monitoring and control parametersThe monitoring of circulation water parameters on a regular basis and control

    within the parameters guidelines generated through the On Guard TM

    modeling is important. for the c irculating water were finalized based on the

    brackish water quality being used as make up.

    ResultA baseline date was generated for monitoring the effectiveness of treatment

    performance it was decided that the plant performance in the period before

    the initial cleaning and start up would be used as the baseline.

    Parameter Unit Range

    Ph - 7.2-7.6

    Conductivity Micromhos

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    Status before implementation of treatment

    Of the three units, two units were under shutdown (R& M) and only one was

    under operation. The initial status of the unit running before implementing the

    treatment program was:

    Average vacuum = -0.78kg/ cm2

    Average load = 68MW

    Average exhaust steam temperature = 68*C Number of cooling water pumps in operation =3

    Number of cooling towers in operation =2

    Remarks

    In spite of operating an additional cooling tower and cooling water

    pump, the condenser vacuum was low and the plant was forced to

    operate at a reduced load.

    The system had adopted organophosphonate treatment and

    chlorination. However, condenser scaling was frequent and had to be

    cleaned with acid and high-pressure hydro jetting regularly. The condenser cleaning frequency was once in two months.

    Implementation of the advanced treatment programSpecially formulated dispersants were used for initial cleaning of the system

    under controlled conditions. Immediate improvement was observed in the

    plant operation after the initial cleanup. The plant performance improved and

    the key operating parameters of the running unit were as under:

    Sl.

    No.

    Before CW Treatment in

    Aug 2005

    After CW Treatment in

    Aug 2005

    Remarks

    1 Avg. Vacuum= 0.78

    kg/cm2

    Avg. vacuum= 0.84

    kg/cm2

    Improvement in

    vacuum by 0.06 kg/cm2

    2 Total unit gen = 44000 MW Total unit gen = 50000

    MW

    Improvement in gen =

    6000 MW

    3 Avg. Generation=1500MW

    /day

    Avg. Generation = 1700

    MW/day

    Improvement in gen

    =200 MW/day

    4 Aux power consumption =

    1572 MW

    Aux power

    consumption= 1073 MW

    Reduction in power

    consumption = 499 MW

    5 Aux power consumption in

    Rs. 3442000/-

    Aux power consumption

    in Rs. 2349000/-

    Aux power reduction in

    Rs. 1093000/-

    6 Heat rate =3474 Kcal/Kg. Heat rate= 3175

    kcal/Kg.

    Reduction in heat

    rate=299 Kcal/Kg.7 Lignite consumption=

    1.17MT/MW

    Lignite consumption =

    1.05 MT/ MW

    Reduction in lignite

    consumed 0.12 MT/MW

    8 Turbine efficiency =24.755% Turbine efficiency

    =27.086%

    Improvement in Turbine

    Efficiency =2.33 %

    a)Vacuum = 0.84kg/cm2

    b) Load =75MW

    c) Exhaust steam temp.=

    61*C

    d) Number of cooling towers

    in operation = 1

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    These parameters were maintained with the continuous treatment program.

    After the other two units were brought online they operated at their rated

    output with optimum vacuum in the condenser generating rated power on a

    continuous basis.

    2. CASE STUDY FOR IMPROVEMENT ON PERFORMANCE OF COOLING TOWERFILLS THROUGH CHLORINE-DI-OXIDE TECHNOLOGY IN A NORTH INDIA

    POWER PLANT.

    Background

    In one of the power plant in North India the tower fills were getting chocked and

    hence causing difficulty in the cooling tower operations be way of low cooling effect

    and causing fills to fall due to weight.

    Cause and the sequence of choking

    This was due to the reason that the tower was induced counter flow type and fills

    were used to enhance the cooling by increasing the surface area of the droplets

    dripping down. Various steps of the development of chocking were observed to be:

    1. Sucking air, dirt and dust from the bottom

    2. Water was traveling from the top to bottom through the fills.

    3. The thin tubular structures of fills were causing the dust /dust ac cumulation.

    4. This was giving rise to bacterial muck/sludge causing fills to be heavy.

    5. Water was getting dried up on the upper portion of these fills

    causing CaC O3 deposition.

    Based on the detailes of the analysis of the deposit and thickness on the upper layer

    the cause for this was attributed to no treatment in the cooling towers and

    concluded that this accumulation was there since the period of no treatment in the

    system.

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    Non functioning of Oxidizing biocide

    The cooling water treatment was implemented in the tower in a later stage but still the

    chocking in the tower was the cause of worry, however the condenser performance

    improved.

    Chlorine was not working well due to its limitation on the Biofilm penetration and

    efficiency reduction in the high pH operation.

    Hence Chlorine Di-Oxide was used alongwith the biodispersant to enhance the

    efficacy of the microbiological control programme. As analysis for the C hlorine di-

    Oxide measurement on hourly basis was not feasible alternate method of ORP

    (Oxidation and reduction potential) measurement was selected.

    1. HOCl- + H++2e- - Cl- +H2O with 1.48 volts53.5 gms

    2. HOBr- + H++2e- - Br- +H2O with 1.48 volts97 gms3. 2Cl2 +2e- - 2ClO2 with 0.95 volts135 Gms.

    By successful implementation of C hlorine Di-Oxide and the biodispersant really

    worked and an improvement in the tower efficiency was visible.

    Case studies by

    ChembondDrewtreat Limited

    EL 71, MIDC Mahape

    Navi Mumbai

    706050403020100--

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    Refinery Fouling versus ORP

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    Time

    ORP

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    ORP

    FOULING