US 84 MISSISSIPPI BIOGRAPHY RIVER BRIDGE TRUSS PIN AND ... · Page 1 of 14 US 84 MISSISSIPPI RIVER...
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US 84 MISSISSIPPI
RIVER BRIDGE –
TRUSS PIN AND
LINK
REPLACEMENT
JAMES GREGG
JUSTIN WALKER
MICHAEL XIN
BIOGRAPHY
James Gregg is the bridge
department manager for HNTB
Baton Rouge, LA office. He
served as the project manager
for US 84 Mississippi River
Bridge Rehabilitation project as
well as assisted with several
NBIS inspections of the bridge.
Mr. Gregg has over 10 years’
experience with design and
rehabilitation of complex
structures, design-builds, and
bridge construction inspections.
Justin Walker is the current state
bridge engineer for Mississippi
Department of Transportation
with over 15 years of experience
in bridge design. He currently
serves as a member of
AASHTO T17 Welding
Subcommittee on Bridge
structures and is a member of
the Mississippi Engineering
Society and the Structural
Engineering Association of
Mississippi.
Michael Xin is a principal
bridge engineer in HNTB
Chicago, IL office with more
than 20 years’ experience on
complex bridges. Michael
served as one of the lead
designers of the for the US 84
Mississippi River Bridge
Rehabilitation project.
SUMMARY
The US 84 Mississippi River
Bridge is a 5 span cantilever
truss bridge crossing the
Mississippi River in Natchez,
Mississippi. Two lower truss
pins on the bridge shifted
transversely and were flush
with the outside gusset. The
existing truss pins and links
were removed and replaced.
Temporary restraints were
used to bypass the load in the
truss pins and link and
instrumentation used to
evaluate stresses in the truss
during removal.
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US 84 MISSISSIPPI RIVER BRIDGE – TRUSS PIN AND
LINK REPLACEMENT
Introduction
The westbound US 84 Mississippi River Bridge
is a 5 span cantilever truss with a 7 span
approach that carries US 84 over the Mississippi
River between Natchez, Mississippi and Vidalia,
Louisiana (Figure 1). The Westbound Bridge
was designed by HNTB in 1939 and opened to
traffic in September 1940. The bridge was the
third Mississippi River Bridge built south of
Memphis, Tennessee and the first highway only
Mississippi River Bridge south of St. Louis,
Missouri. The bridge has one suspended span
located between Piers 1 and 2 and eyebar links
on Spans 2, 3, and 4. The Louisiana approaches,
Spans 6 through 11, are plate girders. A twin
structure located downstream was completed in
July 1988 and the older bridge was restriped to
two westbound lanes.
Figure 1 – Bridge Location Map
The westbound bridge has a 24’-0” clear
roadway width, 2’-0¼” wide steel curb and rail,
and a 7¼” thick deck (Figure 3). The deck is
supported by crossbeams which are supported
on 3 stringers. The stringers are framed into the
floor beams that are spaced at either 39’-10½“or
43’-9”. Eyebar links (2’-0” x 10” x 7’-6½” long)
are located at truss Joints U19, U29, U49, and
U69. The westbound bridge was originally
designed for a H15 vehicle (truck or lane).
A general elevation view is shown in Figure 2
and a section view is shown in Figure 3.
Figure 2 –General Elevation View
Figure 3 – Section View
As a border bridge between Louisiana and
Mississippi, the bridge is maintained by
Mississippi Department of Transportation
(MDOT) but cost equally shared between
MDOT and Louisiana Department of
Transportation and Development (DOTD).
Pin and Link Details
Unlike other cantilever truss bridges in which
eyebars supporting a suspended span are full
length truss member, the pins and links on the
US 84 Mississippi River Bridge are confined to
the upper joint. The suspended span and quasi-
Natchez, MS
New Orleans, LA
Page 2 of 14
suspended span loads pass through the
suspended span or quasi-suspended span upper
gusset and into the 7’-6½” long links via 101/16”
diameter lower pins (Figure 4). The load is then
transferred from the link into the cantilever span
upper gusset via 101/16” upper pins. The pins and
link also function as expansion joints for the
bridge and were designed for up to 9” of
movement between the two gussets.
Figure 4 – Upper Joint
Pin Movement
U29 Pin Movement
In 1995, MDOT observed the tie rod that holds
and restraints the pin from lateral movement was
fractured and cover plates missing on the lower
pin at U29 downstream truss. The weld that
prevents the lower pin from rotating about the
gusset was broken and the pin had rotated 2¾”
from its installed position. The lower pin was
also flush with the inside face exterior gusset on
one side and extended 1” on the outside face
exterior gusset (Figure 5 & 6).
MDOT contracted with HNTB which advised
the outside ½” gusset supported the hanger and
if the pin continued to move past the outside
gusset, there would be an adverse effect to the
factor of safety for the bridge, potentially
resulting in closure of the bridge.
Figure 5 – U29 Lower Pin Downstream Truss
Inside Face
Figure 6 – U29 Lower Pin Downstream Truss
Outside Face
Pin Rehabilitation
In 1996, MDOT awarded a contract to
temporarily remove the load off the pin and link
via temporary restraints and push the lower pin
back into place. Beneath one lane of traffic,
HNTB proposed a vertical jacking assembly that
would bypass the load on the link and pins via 4
post-tensioning bars (Figure 7).
Page 3 of 14
Figure 7 – Vertical Jacking Assembly
Prior to installing the vertical jacking assembly,
the contractor attempted to reset the pin without
removing the vertical load. The first attempt the
contractor applied 675 kips of horizontal load in
which his post-tensioning system failed resulting
in post-tensioning bars passing traffic and into
the river. The second attempt (Figure 8) the
contractor redesigned the horizontal jacks and
increased the horizontal load to 884 kips. The
third attempt the contractor redesigned the
horizontal jacks and increased the load to 1,325
kips, at which point no movement in the lower
pin was recorded.
Figure 8 – Horizontal Jacks
The fourth attempt, the contractor redesigned the
temporary restraints to include a vertical jacking
assembly in which he applied 800 kips of
vertical load to remove the theoretical dead load
in the pin and link and then applied 727 kips of
horizontal load to the pin, at which point no
movement in the lower pin was recorded.
Ultimately, MDOT and HNTB agreed any
additional attempts would be futile, potentially
cause damage to the bridge, and agreed to
regularly monitor the pin for additional
movement.
2010 In-Depth Inspection
In 2010 HNTB was contracted by MDOT to
complete an in-depth inspection of the
westbound US 84 Mississippi River Bridge in
which non-destructive testing was completed on
8 of the 16 pins. The non-destructive testing
revealed inter-component acoustic coupling
(ICAC) between the lower pin at U29
downstream truss and the link which indicated
the pin may have fused with the link. ICAC
typically occurs when the ultrasonic wave from
an ultrasonic examination is reflected from the
transverse surface of an adjacent component,
typically under high local bearing stress. The
lower pin was still flush with the exterior gusset
but an oblong hole in the gussets with a 3/8” gap
between the bottom of the lower pin and the
gusset was observed. The oblong hole was
consistent with the assumption the lower pin was
rotating about the gusset vs. the pin. It was the
intention of the original designer that the pin
would not rotate about the gusset and the
bearing stress on the gusset from the pin be 0.56
Fy. (AASHTO allows 0.4 Fy for pins subject to
rotation and 0.8 Fy for pins not subject to
rotation)
The in-depth inspection also revealed the lower
pin tie rod on U49 upstream truss had fractured,
the cover plates missing, the pin was flush with
the exterior gusset, and there was roughly ½”
gap between the bottom of the lower pin (Figure
9).
Page 4 of 14
Figure 9 – U49 Lower Pin
Pin and Link Replacement
Investigation
After the 2010 in-depth inspection, MDOT
contracted with HNTB to investigate and make
recommendations to address the lower pins at
U29 downstream truss and U49 upstream truss.
HNTB investigated four options:
1. Restrain and monitor
2. Rest pins
3. Replace lower pin
4. Replace lower and upper pins and link
Option 1 – Restrain and Monitor – This option is
similar to the “no build” option in an
environmental assessment and entails
reinstalling the cover plates on the lower pins
and continuing to monitor.
Option 2 – Reset Pins – This option would entail
reusing the concept from 1996 and attempting to
reset the lower pins
Option 3 – Replace Lower Pins – This option
would entail using the vertical jacking assembly
similar to figure 7, however, using destructive
measures to remove the lower pin, boring a new
hole in the gusset and link, and installing a new
lower pin.
Option 4 – Replace Lower and Upper Pins and
Link – This option would entail installing
temporary restraints so that the upper and lower
pins and link could be removed and replaced.
Risk Matrix
In order to review all four options, HNTB
prepared a risk matrix for all four options listing
the pros and cons to each option for MDOT and
DOTD to complete. The risk matrix listed risk
and probability/likelihood on a scale of 1 to 5 for
the different options and components within
each option.
Option 1 – Although MDOT had been
monitoring U29 for over 15 years, this option
represented the highest risk with moderate
probability. With the bridge at its design life of
75 years, the pins could have shifted for several
reasons such as wear or pier movement.
Unfortunately, there was minimal information to
support or dismiss theories. Ultimately, if the
pin moved further within a 12 month period or
became locked, there would be little to no
warning signs outside of complete collapse. The
probability was identified as moderate due to
fact the lower pin at U29 downstream truss had
not moved in 15 years, however, the pin at U49
upstream truss had. MDOT and DOTD decided
this option was not preferred.
Option 2 – If successful, this option would
represent the lowest risk; however, it was
assigned a low probability of being successful.
Based on the experience in 1996, the contractor
was unsuccessful at resetting the lower pin at
U29 and the non-destructive testing noted
acoustic coupling between the lower pin and link
which indicated potential fusing. If fused, the
pin was not designed to rotate about the gusset
which can be observed by the oblong hole in the
gusset from the lower pin wear. The other lesson
learned from the 1996 attempt was the fact the
pin must be rotated prior to pushing back. It is
anticipated the pin has grooves, and similar to a
key in a lock, unless the pin is rotated while
being pushed, any attempts would be futile.
MDOT and DOTD decided this option was not
preferred.
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Option 3 - HNTB completed a comprehensive
investigation of option 3 but the risk of
damaging or finding damage on the existing link
proved too high. Although the probability of
damage on the existing link was low, the links
are unable to be tested and are at their design
life. Visual inspections have been limited due to
special constraints and key sections would not
be visible until the lower pin was removed.
Contingency plans were contemplated in the
event the links needed to be replaced; however,
MDOT and DOTD decided this option was not
preferred.
Option 4 – MDOT and DOTD unanimously
agreed replacing the upper and lower pins and
the link at U29 downstream truss and U49
upstream truss was the preferred option. This
option had the highest probability of being
successful with risk that could be mitigated
through the design of HNTB’s temporary
restraints.
Pin and Link Replacement
In order to remove the pins and link, a
temporary bypass that locks the joint from
moving in all directions was developed. It was
important the temporary bypass had internal
redundancy plus alternate load paths to mitigate
the risk of any one component compromising the
bridge when the pins and link were removed. A
series of bypasses were used to lock the joint
and the Pier was expected to flex under thermal
loads.
The temporary restraints were comprised of four
main components; Upper Longitudinal Restraint,
Diagonal Bypass, Lower Longitudinal Restraint,
and Splice Plate (Figure 10).
Figure 10 – Temporary Restraints
Upper Longitudinal Restraint (Figure 11) – Due
to the fact U29 and U49 are expansion joints, the
pins and link are free to rotate. When removing
the link, the two gussets must be locked
together. The upper longitudinal restraints use
post-tensioning bars plus shim blocks to
compress the two gussets together until the
splice plate is installed. The upper longitudinal
restraints are applied to both upstream and
downstream trusses when removing the pins and
links.
Figure 11 – Upper Longitudinal Restraints
Diagonal Bypass (Figure 12 & 13) –The
majority of the load in the link is from the
diagonal truss member on the suspended span
(lower pin side of the gusset). The diagonal
bypass was designed to unload the suspended
span diagonal truss member and link. Once
installed, the suspended span would bypass the
lower pin and be transferred into the cantilever
span gusset from above.
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Figure 12 – Diagonal Bypass
Figure 13 – Diagonal Bypass
Lower Longitudinal Restraint (Figure 14) – L29
and L49 bottom chord truss members currently
are false chord members; however, they have
similar properties to the other truss members.
The Lower Longitudinal Restraint connects the
two bottom chord members allowing them to act
as an alternate load path. Shims were installed
between the two members and post-tensioned to
ensure they remained in compression.
Figure 14 – Lower Longitudinal Restraints
Temporary Splice Plate (Figure 15) – As a
means to control displacement and provide an
alternate load path, a splice plate was designed
to connect the suspended span gusset to the
cantilever span gusset. The temporary splice
plate required over 350 A490 bolts per truss
which entailed removing existing rivets in the
gusset or field drilling new holes. Because only
one rivet could be removed at a time, each bolt
was installed with a custom nut between the
gusset and splice plate to ensure the splice plate
bore uniformly on the middle nuts and middle
nuts on the gussets. The force in the each bolt
was calculated and bending in the bolt checked.
Cheek or shim plates were installed between the
gussets and splice plate to provide additional
friction force, however, the friction force was
not included in the design of the splice plate or
bolts.
Figure 15 – Temporary Splice Plate
Redundant Load Path
In order to mitigate risk while the pin and link
are removed, the temporary restraints were
designed so that they had internal redundancy as
well as additional load paths in the event one
system is lost. Figure 16 and 17 & 18 illustrate
the three load paths.
Figure 16 – Temporary Load Path A – Diagonal
Bypass
Page 7 of 14
Figure 17 – Temporary Load Path B – Splice
Plate and Lower Longitudinal Restraint
Figure 18 – Temporary Load Path C – Splice
Plate
Construction
Overview
Typically MDOT projects are either design-bid-
build or design-build. In the design-bid-build
option, MDOT or its consultant prepares a set of
plans and the project is advertised and any
contractor may place a bid with the low bid
winning. MDOT and FHWA agreed that due to
unique nature of the work, plus the risk of a
mistake or carelessness could result in collapse
or severe damage to the bridge, MDOT decided
to advertise a design-bid-build with a two-step
process. Step one consisted of a request for
qualification from contractors with a short list of
qualified contractors. Two qualified contractors
were shortlisted with both submitting bids based
on plans developed by HNTB. C.E.C. out of
Lafayette, Louisiana was the low bidder at $3.8
million and awarded the project.
Traffic Control
It was decided that because of the risk associated
with removing the pin and link, the traveling
public should not be on the bridge during the
replacement. MDOT wisely decided to install
crossovers and put traffic head to head on the
eastbound bridge as well as re-synchronize
traffic lights. Minimal to no queue was
observed throughout the duration of the project.
U29 Misalignment
During installation of temporary restraints, it
was observed that U29 upper pin gusset
(cantilever span gusset) and lower pin gusset
(suspended span gusset) near the lower pin were
shifted inboard by 1.875” where they should
have been centered with each other (Figure 19).
The cantilever span gusset near the upper pin
was shifted by ¾” and the cantilever span gusset
appeared to have a slight rotation. Truss
member U29-L30 also was kinked near the
connection point at L30 (Figure 20). Based on
review of the 1940 construction and erection
records of the bridge, the suspended span from
L22 was cantilevered out with the final tie-in
between the suspended and the cantilever span at
U29 (Figure 21). The misalignment was
indicative of a geometric misalignment during
erection of the bridge and the two spans were
pulled together laterally in order to install the
pins and link. It was speculated that U29 had
locked-up lateral erection force which was being
restrained by the existing pins and link.
In order to mitigate the locked-up erection
forces, the anticipated load was calculated based
on the observed deflection and checked against
the top strut lateral restraints and found to be
satisfactory. 200 plus additional A490 bolts
were required at U29 splice plate to mitigate the
additional bending plus an interior plate that
engaged the entire bolt group installed. (Figure
22)
Page 8 of 14
Figure 19 – U29 Offset
Figure 20 – U29-L30 Kink
Figure 21 – 1940 Construction
Figure 22 – U29 Middle Plate
Instrumentation
In order to ensure the temporary restraints were
properly transferring the load off the pin and
link as well as to evaluate any unforeseen losses
in the restraints, strain gauges were installed on
multiple truss members and the post-tensioning
bars. The splice plates were also instrumented
to evaluate stresses once the pins were removed.
Because the temporary restraints would change
the boundary conditions of the bridge to fixed-
fixed, adding additional load in the truss and
forcing the Piers to flex, the Piers were inspected
prior to and after locking each joint.
The initial inspection of the Piers revealed
numerous cracks, as is expected for a mildly
reinforced Pier at 75 years of age. No crack
growth was observed in the post-inspection.
Based on the instrumentation output from the 8
links over a two week period it was obvious the
bridge was behaving in a fixed-fixed condition.
The existing link and pins would build up as
much as 3.0 ksi of stress before breaking free
and equalizing back to zero.
Sequence of Construction
As part of the contract plans, the contractor was
required to submit a detailed sequence of
construction demonstrating means and methods
for removing the pin and link. The contract
plans provided a suggested sequence of
construction in which the contractor adopted
with minor modifications. The contractor chose
to remove the pins and link at U49 first, and
Page 9 of 14
based on lessons learned, some adjustments
were made at U29. The following are the key
steps to the sequence of construction with
lessons learned from construction:
Step 1 – Tension Diagonal Bypass (Figure 23
and 24). L48 – U49 diagonal bypass was
tensioned to remove the load in the existing truss
diagonal member, link and pin. Stressing
operation were conducted in increments and
member stresses observed to ensure the bypass
was functioning as anticipated. U49 existing
link change in force was monitored and U49
diagonal bypass was tensioned to 10% over the
anticipated force, resulting in the change in force
in the link to be within 1% of the anticipated
load (Table 1). Although the entire load would
not be released until the pins were removed, it
was preferred to minimize the load in the
existing link to avoid the pins from binding and
prevent sudden movement resulting from pin
removal.
Figure 23 – Tensioning of Diagonal Bypass
Figure 24 – Tensioning of diagonal bypass
Table 1 – Diagonal Bypass
Member Load Anticipated
Load
U49 Diagonal
Bypass
836 kips 760 kips
L48-U49 580 kips 761 kips
U49 Link 660 kips 655 kips
U29 Diagonal
Bypass
782 kips 740 kips
L28-U29 699 kips 740 kips
U29 Link 634 kips 640 kips
Prior to tensioning U49 diagonal restraint, upper
and lower shims were installed. The upper
shims would transfer any horizontal force in the
diagonal restraint. The lower shims would not
be required until Step 2 but were chosen to be
installed during Step 1 (Figure 25 and 26).
During the stressing of the diagonal bypass, the
lower shim shifted transversely by ¼”. As the
diagonal restraints became fully engaged, it
became clear that one of the post-tensioning bars
was conflicting with the truss lateral bracing,
potentially causing the shift at the lower shims.
The portion of truss lateral bracing that was in
conflict was cut further allowing the diagonal
post-tensioning bars to adjust; however, because
the upper bypass was engaged, the horizontal
Page 10 of 14
load from the upper bypass did not allow the
shims between the two gussets to shift back
horizontally.
Once the existing pin was removed and the new
one installed, it was observed that the inboard
and outboard lower gusset had walked out by
½”. Fortunately the new lower pin was made
longer and the pin bore directly on the gussets;
however, the pin extension beyond the gusset
was minimal. Although the gussets did not
appear to walk when engaging the diagonal
restraints, the existing pins may have been
restraining them, and once removed, the gussets
were free to walk.
For U29, the lower shims were not installed until
after the diagonal bypass was engaged and prior
to tensioning the upper longitudinal restraint.
An additional stiffener plate was also installed
and as a result, U29 outboard and inboard gusset
did not walk.
Figure 25 – Upper Shims
Figure 26 – Lower Shims
Step 2 – Tension Upper Longitudinal Restraint
(Figure 27 and 28). Both upstream truss and
downstream truss upper longitudinal restraints
were tensioned to prevent the joint from moving
longitudinally. The upper longitudinal restraints
were designed for a 60 degree temperature drop
but stressed to accommodate a 40 degree
temperature drop based on the 10 day weather
forecast.
Figure 27- Upper Longitudinal Restraint
Page 11 of 14
Figure 28- Upper Longitudinal Restraint
Step 3 – Weld Templates and Field Drill Splice
Plate (Figure 29 and 30). Once the bridge was
locked from moving, the splice plate templates
were welded together and used to field drill the
splice plates. Field drilling and installing the
splice plates was challenging due to the 100 plus
A490 bolts per face of gusset, but was
completed with minimal to no incident.
Figure 29 – Splice Plate Template
Figure 30 – Field Drill Splice Plate
Step 4 – Install Top Strut Plates (Figure 31).
Although there was a wind shear device at U29
and U49, the two top strut were connected
together to provide lateral additional rigidity in
the event there were any unexpected lateral
forces when the link was removed.
Figure 31 – Top Strut Plate
Step 5 – Install Lower Longitudinal Restraints
(Figure 32 and 33). Shims were installed
between the two false chord members and post-
tensioned together to ensure continuous bearing
between members.
Figure 32 – Lower Longitudinal Restraint Shims
Page 12 of 14
Figure 33 – Lower Longitudinal Restraints
Step 6 – Remove Pins (Figure 34 and 35).
Because of the difficulty the previous contractor
had with trying to reset the pins in 1997, the
contractor elected to cut the pin with a diamond
tipped wire saw. After cutting U49 upper pin,
minimal change in force was observed in the
link, and U49 and U29 splice plates saw about 1
ksi and 7.5 ksi of stress respectively (Table 2).
It was speculated the higher stress in U29 was
attributed to the misalignment of the truss. No
movement was observed in either joint during
removal of the pins.
The contractor attempted to push out U49 lower
pin with hydraulics jacks after the upper pin was
cut, but after applying 1,000 kips, minimal to no
movement was observed. Ultimately, both faces
of all pins required cutting and after the lower
pins were removed, it became clear from the
observed amount of grooving, the pins would
not been able to be pushed out (Figure 36).
Figure 34 – Wire Saw
Figure 35 – Wire Saw Inside Truss
Figure 36 – U49 Lower Pin Drop Cut
Table 2 - U29 Splice Plate Maximum Stress
Page 13 of 14
Step 7 – Line Bore (Figure 37). The contractor
line bored a 10½” to 10¾” hole through the
existing gusset and new eyebars to ensure the
new pins would bear properly and fit. With the
existing link and pins removed, it was found that
the existing upper pins at U29 and U49 were not
plumb whereas the lower pins were. It is
speculated this may have been part of the cause
of the walking observed at the existing lower
pins. It was also noted that U29 inboard and
outboard gussets were not plumb and this was
attributed to the locked-up erection forces in the
gusset. New pins were bored plumb and in line
with each other.
Figure 37 – Line Bore of Upper Pin
Step 8 – Install New Pins (Figure 38). Once the
line bore was complete, the new pins were able
to be installed with little difficulty. For the first
location, U49, all four pins were machined and
on site. However with the existing upper pin
hole not being plumb and new hole required to
be plumb, the existing upper original diameter of
10¼” was inadequate. The contractor sent U29
lower pin, which was 10¾” diameter, back to the
machine shop to have it turned down to the
needed diameter of 10½”.
New pins were ordered for U29, however, they
were not turned down until after the line boring
was 50% complete.
Figure 38 – Installation of New Pins
Conclusion
After the new pins were installed, the temporary
restraints were disengaged and load transferred
to the new pins and eyebars. Table 3 includes
the results from U29 and U49 eyebars. U49
eyebar loads appeared to be symmetric and
behaved as a deep beam governed by Euler-
Bernoulli. The inside eybar was 15% greater
than the outside eyebar and it is thought that the
inside gusset may carry more load due to the fact
that the weight of roadway is transferred through
the floor system which favors the inside gusset.
U29 loads were not as symmetric as U49 and
heavily favor the outside gusset. The outboard
eyebar was 44% greater than the inboard eyebar
and it is thought that the misalignment in U29
was the primary culprit for the imbalance.
When comparing the total loads in Table 3, both
U29 and U49 were within 3% of the dead loads
shown on the 1940 contract plans.
Page 14 of 14
Table 3 – U29 and U49 Eyebar loads
Location U29 U49
Bar 1 (inboard) 70.9 kips 135.3 kips
Bar 2 105.4 kips 115.9 kips
Bar 3 119.9 kips 100.2 kips
Bar 4 115.6 kips 102.0 kips
Bar5 125.6 kips 104.1 kips
Bar 6 (outboard) 127.0 kips 115.7 kips
Total 656.5 kips 673 kips
DL in 1940 Plans 638 kips 655 kips
MDOT, HNTB and CEC all felt the project was
a success and MDOT is anticipating replacing
the remaining 12 pins and 6 links on a future
project. The primary key to success was the
partnership and determination between all the
parties involved to make the project successful.