Turbogenerators Case Studies - indianpowerstations.orgindianpowerstations.org/Presentations Made at...

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Turbogenerators Case Studies Presented by Abhilash Chandra Aron Consultant, Turbogenerators Managing Partner, Eron Services

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Turbogenerators

Case Studies

Presented by

Abhilash Chandra Aron

Consultant, Turbogenerators

Managing Partner, Eron Services

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CASES by AC ARON Feb 2012 2

Bhusawal TG Core Damage

THW-210 Bhusawal-2 TG overhauled in

1993 and then in 2002. During this o’haul,

ELCID readings were high for slots 51- 52

near 1st end packet on TE.

After removing few bars, core melt seen

between slots 51 and 52.

Tooth between 51- 52 was cut off, molten

iron removed to reach clear laminations.

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CASES by AC ARON Feb 2012 3

Bhusawal Core Damage -2 View From Turbine End

Core Melt

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CASES by AC ARON Feb 2012 4

Bhusawal Core Damage - 3

51 52

A C ARON

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CASES by AC ARON Feb 2012 5

Bhusawal Core Damage - 4

Later, after the tests, few more hot spots

near end packets detected and repaired.

A dummy tooth was made out of glass

textolite and glued in place of removed

metal position.

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CASES by AC ARON Feb 2012 6

Melting of Core Iron

Core iron melt Zone upto which

iron to be cut off

Healthy core

10 - 15 mm

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CASES by AC ARON Feb 2012 7

Core Repair - 5

Stator Core Long Wedges Dummy Tooth

Normal Wedges

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CASES by AC ARON Feb 2012 8

Slot Wedge

Core Iron

Core Repair - 6

Dummy Tooth

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CASES by AC ARON Feb 2012 9

Packet: 91 92 93

Slot 54 22 16 26

Slot 53 64 73 71

Slot 52 42 71/38

Slot 51 65 -- --

Slot 50 48 145/196 229

Slot 49 92 275/298 246

Slot 48 111 342/343 218

Slot 47 46 179/203 135

ELCID Test Results

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CASES by AC ARON Feb 2012 10

Core Loss Test

Test is done at flux density of 1 - 1.5 Tesla

for 90 - 45 min. Teeth temps. are checked

with infra red devices.

At the end, temp. rise of hottest point to

be < 25°C and difference between the

hottest and coldest be within 15°C.

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CASES by AC ARON Feb 2012 11

‘TE’:Packet: 91 92 93

Slot 54 11 12 11

Slot 53 15 19 21

Slot 52 11 -- --

Slot 51 14 16 17

Slot 50 12 13 15

Slot 49 11 13 13

Slot 48 9 11 11

Slot 47 7 7 7

Core Loss Test Temp. Rises ºC after 90 min.

Dummy Tooth

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CASES by AC ARON Feb 2012 12

Turb End: Temp Rises after 30 min. Max. rise permitted 25º C

11- 12º

16º 11º

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CASES by AC ARON Feb 2012 13

O’Haul: Dec.2004

Overheating seen

at core back near

core bars in the

repaired zone.

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CASES by AC ARON Feb 2012 14

Stator Damage

• A 760 MVA Angara-Brazil : Core repaired

after 13,400 Hrs. Hot spots repaired using

electro-chemical process.

• M/c tripped on stator faults, after another

1200 Hrs. Huge core melt seen on ExEnd.

High burrs; Insulation thickness too less.

Core was poorly clamped at two ends.

• Machine was rebuilt at site by KWU.

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CASES by AC ARON Feb 2012 15

Stator winding Leakage

• Leak in stator winding caused H2 gas to

enter into it. H2 consumed @ 25 cylinders

per day. Gas pressure reduced and water

came out at leaking point, causing flash

over between phases. Machine rewound.

• Ran for 30,000 hrs without mandatory initial overhaul. H2 leak detected in the gas trap device and in expansion tank. Leakage was in 3 bars on EE side.

ACA - OH - 2 / 50 HO

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CASES by AC ARON Feb 2012 16

Radial Vibrations THW: Stator Winding Vibrations

Teflon Tubes

A. C. ARON 1999

Tangential Vibrations

Upper Bar

Lower Bar

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CASES by AC ARON Feb 2012 17

Chandrapur 500 MW U-7

• TG having clocked 63,734 hours, running

with gas cooler leak, tripped on electrical

faults. Melting of copper lugs,Teflon tubes

water headers seen on turbine side.

• Mostly,replaceable lug ends got damaged

but in one joint, 4 hollow strips melted.

• A copper chamber was made in this lug

by brazing in situ, to restore water flow.

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CASES by AC ARON Feb 2012 18

Damage at 7 O’Clock

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CASES by AC ARON Feb 2012 19

Upper half box removed

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CASES by AC ARON Feb 2012 20

Brazed jacket

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CASES by AC ARON Feb 2012 21

Brazed top box cover

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CASES by AC ARON Feb 2012 22

High Cold Gas Temps.

• CW temp. remains high in summer and

machine operated at maximum MVAR.

• 2 RTDs were defective due to cold solder

• Hot gas leaks bypassed

H2 cooler inside stator.

Rubber seals in coolers

were corrected.

NEYVALI THW - 210 MW TG

Core

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CASES by AC ARON Feb 2012 23

210 MW: Motoring

• 2 ph steady state asynchronous motoring

for 6 minutes without excitation.

• Generator: 12.9, 12.8,12.3 kV stator volts

and load: 2.8, 4.4, 3.0 kAmp; 0.5 MW.

• Calculations showed: ‘I2’ was 5110 Amp

(56.5% FL) duration 3 sec., So, I2² t ~ 3,

which was permissible

• Rotor was cleared without any inspection.

North Chennai

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CASES by AC ARON Feb 2012 24

TG Motoring - 2

• A 200 MW Mitsubishi generator

motored in asynchronous mode for

almost 34 minutes due to GCB fault.

• I2² • t value was computed by OEM

as more than 110.

• Retaining rings were removed but no

physical damage seen.

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CASES by AC ARON Feb 2012 25

TG Motoring - 3

• Machines started as induction motor

from standstill..

• Rotor barrel ends got overheated and

winding insulation got damaged.

• In Wanakbori ‘GT’ also got damaged.

• Stator windings were damaged.

BOKARO, KAKINADA, OBRA, WANAKBORI-7

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CASES by AC ARON Feb 2012 26

Local Repair of a Lower Bar

• After rewinding works, during final HV

lower bar failed at 70 mm from core end

in overhang.

• Puncture point was filled with epoxy. On

top, a ’Π’ shape 4 mm thick insulation

125 mm long was tightly glued and tied.

Passed 21 KV. In operation for >25 yrs.

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CASES by AC ARON Feb 2012 27

Puncture Point

Cap

Glue

Cord

Repair of Lower Bar - 2

70 Core

WANAKBORI - 1

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CASES by AC ARON Feb 2012 28

Repair of Upper Bar

=2Lb

Db Thick

Fault Point

Upper Bar

Lower Bar

Barrier Core Iron Wedge

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CASES by AC ARON Feb 2012 29

THRI-210: Rotor Damage

Set started without water in gas coolers

and loaded to 77 MW.

High gas pressure alarm comes. H2 gas

pressure seen 2.6 against 2 atg normal.

It was estimated that gas temp.went up

to about 129°C and rotor hot spot temp.

went up to 200° C.

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CASES by AC ARON Feb 2012 30

THRI Rotor Damage - 2

Set resynchronized. Rotor current higher by about 20%, confirming rotor inter-turn insulation damage.

Advised to increase H2 pressure from 2

to 3 atg & restrict rotor current to rated,

giving 170 MW and 20 MVAR.

Rotor ran for 18 months in this condition.

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CASES by AC ARON Feb 2012 31

Creepage Path*

THW TG – Rotor Winding – Low IR

*About 2800 creepage paths in rotor cause creepage resistance to fall.

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CASES by AC ARON Feb 2012 32

Fire Around Slip Rings

• In a 210 MW generator, slip rings had

depressions due to non uniform wear

They were not machined as required

and machine continued to run.

• Fire broke out on brushes around the

rings. All the holders+brushes melted

causing a forced and long shut down.

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CASES by AC ARON Feb 2012 33

Slip Rings • Brushgear centering, stagger of brushes,

mounting of brush holders, & alignment

and clearances, brush pressure & grade

are important.

• Dust + oil vapours, give high sparking.

• HM-100 grade, though softer had better

performance. Slightly higher pressure

reduces sparking and brush jumping.

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CASES by AC ARON Feb 2012 34

Oil Starvation

• 210 MW set reached 570 rpm. Sound

heard from rear bearing. Coast down

was quick. Babbit had melted, shaft

journal dia 400 mm developed cracks.

• Shaft had hardened to 315 BHN from

246, because of rubbing. Cracks upto

200 mm length and 1.75 mm depth

had developed.

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CASES by AC ARON Feb 2012 35

• Rotor was reused after machining.

Oil Starvation - 2 Damage To Bearing Journal

175

200

115

160

Ø400

Machined to Ø 320 mm, till all cracks disappeared & normal BHN achieved.

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CASES by AC ARON Feb 2012 36

Damage to a THW-210 TG

• During overhaul, old strip type cracked

lock washers were reused. As a result

during operation, M24 bolts came out,

releasing a 5 kg steel segment inside.

• Plate fell on stator overhang and was

sucked by magnetic pull into the airgap

hammering stator and rotor surfaces &

damaging them.

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CASES by AC ARON Feb 2012 37

THW-210 Damage - 2

A. C. ARON 3MAY 2002

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CASES by AC ARON Feb 2012 38

THW-210: Thrust Seal Failure

• At 120 MW, abnormal sound is heard near

TS bearing. Press falls by 0.3 Kg.

• TS seal-oil drain high. Hydraulic seal oil

level high. Overflow of oil from the damper

tank to hydraulic seal occurs. Babbit RTD

on TE not working.

• Smoke comes out of Turb S seal area

momentarily. Mating surfaces of hole and

locking pin were damaged.

Kolaghat-4, Bokaro-1

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CASES by AC ARON Feb 2012 39

Thrust Seal Failure - 2 • TS seal collar face damaged & was cut by

13 mm. Seal liner babbit was worn out,

parent metal damaged 5 mm deep. Pins

were loose and found shifted.

• Collar face was machined to get 36.7 mm

collar thickness.

• Seal body flange thickness increased by

13.5mm. Long bolts and new seal liners

used.

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CASES by AC ARON Feb 2012 40

Brass Bush

Locking Pin

A

A

With Bush

Without Bush

Damage Here

A-A

A-A

B B

Sec B-B

THW-210: Thrust Seals

Seal Liner

A. C. ARON

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CASES by AC ARON Feb 2012 41

Fire in a 500 MW TG Six LP last stage blades towards IP

side failed at roots in quick succession after 11 years service. All bearings, H2 shaft seals damaged; H2 escaped.

Oil and leaking H2 catch fire. H2 fire extinguished promptly by venting H2 out and CO2 feed. Oil fire stopped by extinguishers. No damages due to fire.

PMG,exciter armature, generator rotor compressor blades were damaged.

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CASES by AC ARON Feb 2012 42

Explosion in Generator

• 110 MW TG fed O2 instead of H2 for make

up. Explosion occurred after 8 hours. Ten

cylinders of O2 were fed upto explosion.

• Purity-meter having 90% low range, was

not working,purity unknown. TG end walls

welding broke, gas coolers axially pushed

• A stator coil had flashover marks in its

overhang portion, copper had melted. Set

tripped on its protections. ACA - OH - 2 / 50 HO

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CASES by AC ARON Feb 2012 43 AFSHA CLASS 5

Best Wishes !