Success Indicators
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Transcript of Success Indicators
SUCCESS INDICATORS
JOHN CHANDLER, JR
CEO | COO | General Manager | Multisite, Multifaceted
Company President | Optimizing Performance
5S Training / Process Improvements Increase Production By
200%, Generating Gross Profit of 24.39%
Company operation was not generating run rate required to meet financial objectives.
Efficient product flow was nonexistent. Challenge was to develop a suitable lean
continuous improvement model that met the needs of the customer, business, and
culture.
Put plant leadership through extensive training in 5S and value stream mapping in
support of plant transformation starting with machine shop. Machine shop went from a
large batch and queue process to a one-piece flow, reducing welding lead time from
three hours to 87 minutes.
Production increased to 200%, generating a gross profit of 24.39% and line failures
dropped to under 6% almost overnight.
Newly Restructured Manufacturing and Quality Assurance
Departments Improve Gross Profits By 10.1%+
Recognized opportunity to drive higher gross profit margins by restructuring
manufacturing and quality assurance departments. Batch and queue process was
outdated and teams did not understand the value of new process and were hesitant to
see a change that would require new learning.
Restructured manufacturing and quality assurance departments. Transitioned plant to a
cellular manufacturing process that consisted of implementing lean enterprise
workplace organization and inspection / maintenance systems.
Improved gross profit from 26.7% to 36.8% and increased production from 86 units per
year to 254 units per year in less than three years.
One-Piece Flow Pull System Increases Productivity By 49.6%
Company was paying more than it should have for the proper level of output; i.e.,
producing far more than downstream customer demand required, resulting in inventory
overruns, costly large batch movements, and higher damaged goods.
Developed process for staging transition from batch and queue to one-piece flow pull
system. Implemented steps necessary to convert manufacturing plant without loss of
production. Established use/hr, FTT, and PIA metrics to determine effectiveness and
efficiency of lean manufacturing processes.
Increased productivity 49.6% resulting in a 65.7% increase in unit/hr production.
Achieved FTT scores in excess of 97% from ~85%.
Multidepartmental and Facility Task Force Delivers $4.7+ Million In
Cost Savings
Company was paying more than it should have for the proper level of output; i.e.,
producing far more than downstream customer demand required, resulting in inventory
overruns, costly large batch movements, and higher damaged goods.
Developed process for staging transition from batch and queue to one-piece flow pull
system. Implemented steps necessary to convert manufacturing plant without loss of
production. Established use/hr, FTT, and PIA metrics to determine effectiveness and
efficiency of lean manufacturing processes.
Increased productivity 49.6% resulting in a 65.7% increase in unit/hr production.
Achieved FTT scores in excess of 97% from ~85%.
Operational Processes / Strategies Cut Costs By 47%+, Boost Sales By
11%, and Doubles Profitability
Company had two consecutive years at 5% loss position, a nonsustainable condition.
Firm’s entrenched way of doing things for the past 10 years had left operation stuck in
a rut with little guidance or motivation to change.
Closely assessed improvement areas and rolled out strategies supporting inventory
management, changes to operating procedures, financial controls, and
communications. Defined clear change objectives and worked closely with team
leaders to achieve buy-in from team members.
Turned around operations in one year, lowered operational costs by 47%+, increased
sales by 11%, and doubled profitability.
Lean Manufacturing Process Reduces Task Time By 2.5 Days And Work-
In-Process By 50%
Outdated “batch and queue” process inherently lends itself to excessive waiting,
overproduction, increased inventory/work-in-process (WIP), additional
transport/handling/motion, and damage/defeats.
Transitioned plant from “batch and queue” process to “one-piece flow pull system” and
implemented lean enterprise inspection and maintenance systems with each
department 5S’ed and shadow boarded.
Reduced task time from 5.5 days to 3 days and work-in-process by 50%, while
increasing units per hour from 67 to 111.
Change Management Practices Improve Material Yields By 20% and
Production Yield By 11%
Needed to find a way to reduce inventories while diminishing material shortages.
Warehouses were organized in part-number sequence without regard to location and
usage with excess raw materials and work-in-process (WIP). Traditional inventory
control system created excessive transport, motion, inventory, and work-in-process,
therefore increasing costs unnecessarily.
Produced value stream map to determine present state and identified future state
objectives. Replaced traditional inventory control system with Just-in-Time (JIT) lean
systems.
Improved material yields by 20% and production yield by 11% over standard costs.
Sales Structure and Compensation Plans Boost Part Sales By 50%
Small parts sales costs were excessive at 26% of sales. There was great resistance to
change in both the company and the industry because things had always been done
the same way.
Revamped small parts sales compensation plans to more directly reflect company
goals. Narrowed target niches to those with greatest current success and future
potential. Drove market share increases as a result of more targeted market approach.
Boosted company-part sales by 50% in three years, cutting costs by 14% of sales.
Cross-Functional Task Force Turns Around and Salvages $50 Million in
Sales
Company lost three large customers and two major customers had placed the
company on notice for product, packaging, and service quality issues. Customer order
fulfillment rate was 85%, generating 15% loss in sales on a daily basis. Sales force
morale was low and sales personnel were in customer maintenance mode.
Established cross-functional task force to ensure retail store display requirements and
rotations were followed across operations and that plant production was aligned with
customer demand.
Improved customer order fulfillment rate to 99% in less than 30 days, salvaging $50
million in sales.
Forecasting, Scheduling, & Process Controls Reduce Labor / Overhead
Variance By Under 3%
Labor variances were outside desired limitations and needed to be brought back under
control. There was a clear lack of focus and direction on leadership teams across the
organization, with limited understanding of process controls.
Collaborated with team leads to create and implement forecasting, scheduling and
process controls that allowed more transparency in business operations, including
manpower availability and utilization. Created visual tools for tracking key indicators
and trained personnel on their application.
Achieved outstanding labor and overhead variances of under 3%.
New Warehouse Management and Procurement Procedures Slash Inventory By
53.4%, Material Handling Labor By 58.2%, and Material Touches By 60%
Needed to establish control over increasing inventory assets and reduce amount of
cash tied up in product inventory. Raw material inventory growth was outpacing sales
growth, diminishing margins and restricting cash flow / profitability.
Revised warehouse management and procurement procedures to establish control and
timely reporting over inventory network / POs. Transitioned firm from traditional
warehousing system to a point-of-use methodology.
Slashed inventory by 53.4%, material handling labor by 58.2% and material touches by
60%.