Sayantan Bhowmik Head Technology Rotary Cell Energy Manager
Transcript of Sayantan Bhowmik Head Technology Rotary Cell Energy Manager
© Reliance Industries Ltd.
Sayantan Bhowmik
Head Technology Srinivas Wuriti
Energy Manager
Jeevan Jadhav
Section Head
Rotary Cell
© Reliance Industries Ltd.
RIL Profile
RIL
Turnover Rs 4,30,731 Crore
Net Profit Rs 36,075 Crore
Contribution to national exchequer Rs
86,942 Crore
Energy saved on account of conservation
initiatives (’000 GJ): 3004
Total water recycled (’000 m3): 69364
Source: Annual Report 2017-18
RIL-NMD
Turnover of Rs 5,420
Crore.
Energy cost is 24% of
Manufacturing cost.
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RIL NMD Process
GAS CRACKER
MEG
59,000 TPA
EO
56,000TPA
POLYROPYLENE
1,20,000 TPA
LLDPE/HDPE
2,55,000 TPA
HEXENE-1
15,000 TPA
LDPE
112,000 TPA
RECYCLED PET
7,300 TPA
PROPYLENE
1,15,000TPA
ETHYLENE
4,40,000 TPA
PP
HEXENE-1
EOEG
LDPE
LLDPE/HDPE
RPET
C2C3
PROPANE
WASTE PET
Fully Integrated with value addition at each step
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Sp. Energy Consumption in last 3 years
Continuous reduction in specific energy
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Benchmarking - Gas Cracker
Solomon Benchmarking (last in 2017) (Benchmarking done with world wide Cracker plants)
Energy performance
Actual specific energy consumption in year- 2017 was 17.5 GJ /ton of HVC Vs 16.8 GJ/ton of HPP plant - 2rd quartile.
Actual specific energy consumption in year- 2015 was 17.9 GJ /ton of HVC Vs 17 GJ/ton of HPP plant - 3rd quartile.
Based on 2015 results
Gap analysis done
and closed the gap of
0.4 GJ/ton by
efficiency
improvement of CG
and C2R turbines.
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Benchmarking - PP
Spheripol Benchmarking by Lyondell Basell
NMD PP Global Average
Nameplate capacity utilization 151 % 120 %
Monomer specific consumption 1.006 t/t 1.007 t/t
Electricity specific consumption 256.4 kwh/t 311 kwh/t
Steam specific consumption 178.2 kwh/t 264 kwh/t
Nitrogen specific consumption 44.1 Nm3/t 42 Nm3/t
NMD PP is consistently better than global average in prime product %.
NMD PP continuously leverages the technology strength and focuses on
higher MFI Random Grades.
NMD PP achieved 89% Random Grade mix against the 13.4 % global
average.
PP participates in M/s Phillip Townsend benchmarking too
Europe--- 14 plants
Americas---15 plants
Far East---16 plants
Rest of world---10 plants
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Benchmarking - CPP
CPP Gas turbine units are benchmarked internationally with Fleet data by M/s SPS
Inc. USA. ORAP (Operational Reliability & Availability Program) (Jan-Jun, 2015).
Availability Reliabili
ty
Service
Factor
MS5001 Fleet,
2015
99.7 99.8 62.3
Others 89.9 98.7 22.7
Fleet 90.2 98.8 23.9
Best in Globe among Frame V fleets.
Good GTG reliability which means fewer startup/shutdowns resulting in lower energy consumption in CPP and the complex.
More than average among all registered fleets for Frame 5 international bench marking.
Monthly inter site benchmarking: First rank amongst all RIL plants in 2017-18
Equipment Performance
Site Unit PMD HMD JMD-D VMD NMD DMD JMD-Z
GT/HRSG Co-gen efficiency % 66.17% 74.12% 84.33% 83.15% 80.55% 75.09% 82.32%
STG cycle efficiency % - 26.62% 40.32% - 38.47% 31.99% 72.60%
Aux boiler thermal efficiency % 92.20% - 92.00% 87.33% - 92.67% 95.42%
Overall fuel efficiency % 76.26% 66.08% 78.45% 80.63% 67.82% 53.55% 80.48%
Fuel eff. Improvement Index % 96.37% 98.27%
102.87
% 94.35% 111.86% 65.43% 100.70%
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Implemented Projects Statistics
6
11
4
0
2
4
6
8
10
12
15-16 16-17 17-18
Implemented Projects
Savings in Rs. Million p.a
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Energy Saving Projects Implemented in
FY 2015-16
S
No
Title of Energy Saving project
implemented
Annual Electrical
Savings achieved
Annual thermal
savings
Total
Annual
Savings
Invest.
Made Payback
months Units
Million
Rs
Million
Tons of
Fuel
Rs
Million
Rs
Million
Rs
Million
1 Increasing the area of 10-E-57
(Regeneration gas feed/effluent) in Cracker --- --- 289 12.39 12.39 4.07
4
2
Stopping one cooling water pump in CT-1
tower by replacing all 6 CW pumps with
new high efficiency CW pumps in O&U
2.63 13.2 --- --- 13.2 10.2 9
3
Providing PRDS water injection by running
BFW pump & stopping one PRDS water
injection pump in CPP
0.18 1.518 --- --- 1.52 1 8
4
Direct supply of makeup water to CT1 and
CT2, hence one water makeup pump
stoppage in O&U
0.35 2.74 --- --- 2.74 1.5 7
5
Replacement of 125 W HPMV lamps with
50 W LED Lighting Fixture in PP bagging
Warehouse area (95% completed)
0.25 0.9 --- --- 0.9 1.5 20
6 Provide additional spare heat exchanger in
parallel to 10-E41D in cracker --- --- 152 6.41 6.41 4.5 9
Sub Total 3.41 18.36 441.81 18.80 37.16 22.77
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Energy Saving Projects Implemented
in FY 2016-17
S
no
Title of Energy Saving project
implemented
Annual
Electrical
Savings
achieved
Annual
thermal
savings
Total
Annual
Savings
Invest.
Made Payback
months
Units
Million
Rs
Million
Tons
of
Fuel
Rs
Million
Rs
Million
Rs
Million
1 GT3 uprate --- --- 2546 62.00 61.67 67.60 14
2 Use of available chilling capacity from
LDPE VAR to LLD AHUs 0.700 2.790 --- --- 2.79 4.60
20
3 150W HPSV street lights by 90W LED
lights 0.001 0.003 --- --- 0.001 0.003 36.0
4 Provision of HP residue gas line to HP
knock out drum for GTG fuel --- --- 5689 138.00 137.79 0.90 1
5 VAR machine temperature control in
EOEG --- --- 48 1.00 1.16 Nil --
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Energy Saving Projects Implemented in
FY 2016-17
S No Title of Energy Saving project
implemented
Annual
Electrical
Savings
achieved
Annual thermal
savings
Total
Annual
Savings
Invest.
Made Payback
months
Units
Million
Rs
Million
Tons
of Fuel
Rs
Million
Rs
Million
Rs
Million
6 Reduction in steam consumption
by derating HP steam control valve --- --- 300 7.0 7.3 0.10 1
7 Stoppage of VAR in DHC and use of
AC in laboratory --- --- 103 3.0 2.5 0.10 1
8 Increasing steam insulation
thickness based on fuel prices --- --- 80 2.0 1.93 4.0
25
9 Demo furnace convection section
dry Ice blasting --- --- 52 1.3 1.27 0.395
4
10 EOEG - BFW - END OF CYCLE - One
pump operation 0.82 2 --- --- 2 --- ---
11 Stoppage of nitrogen compressor
in ASP 3.25 4.6 --- --- 4.6 --- ---
Sub Total 4.77 9.4 8818.5 214.3 216.4 77.7
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Energy Saving Projects Implemented
in FY 2017-18
S No Title of Energy Saving project
implemented
Annual
Electrical
Savings
achieved
Annual thermal
savings
Total
Annual
Savings
Invest.
Made Paybac
k
months Units
Million
Rs
Million
Tons of
Fuel
Rs
Million
Rs
Million
Rs
Million
1 LP Condensate heat recovery in
Cracker --- --- 534.4 3.7 3.7 3.00 10
2
GC furnaces Convection bank
cleaning and refractory
replacement
--- --- 4441.3 80.6 80.6 50 8
3
CG compressor turbine
efficiency improvement
--- --- 5737.8 103.3 103.3 80 10
4 C2R compressor turbine
efficiency improvement --- --- 201.5 3.6 3.6 3 10
Sub Total 10914.9 191.2 191.2 136
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CG Compressor Turbine Efficiency
improvement • Cracked Gas Compressor Train is most critical and energy intensive machine of Gas
Cracker plant. Efficiency of this machine is critical for site energy consumption.
• CG Turbine is MHI make Condensing-Extraction type turbine installed in year 1989.
• Historically the turbine was operating at lower efficiencies than Design Efficiency
for HP & LP section.
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CG Turbine Efficiency Improvement
CG Turbine: Before Revamp After Revamp
Shaft Power 19.93 MW 23.0 MW
Speed (max.) 5,794 rpm 5,580 rpm
Steam Flow 108 T/H 125 T/H
50
60
70
80
90
HP Side
Efficiency
LP Side
Efficiency
Pre Revamp 67.76 80.4
Post Revamp 72.1 89.4
67.76
80.4
72.1
89.4
CG Turbine Efficiency (%)
Pre Revamp Post Revamp
• Investment of Rs. 8 Cr. for modification
• Returns:
Energy Saving-6.5 Gcal/Hr.
Rs. 10.33 Cr. Annual savings
CG & C2R Compressor Turbine Efficiency
58
60
62
64
66
68
Efficiency
Before 62
Post Revamp 67
62
67
C2R Turbine efficiency (%)
Before Post Revamp
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Innovative Project
Skin
temperature
reduced from
5000C to 1800C Convection tubes of
5th (Dil steam +HC: 24
tubes) & 6th (Dil
steam: 6 tubes) banks
were pulled out (total
30 no. tubes) from all
5 furnaces, inspected,
cleaned and installed.
Fuel
consumption
reduced by
35Kg/hr in each
furnace
Savings: 4441
Tons of fuel p a
Gas cracker furnaces convection banks were choked but couldn’t be cleaned due to no access.
.
Challenges faced After removal of tubes, it was
observed that the insulation inside has
corbel joints at two locations. This was
not envisaged during ordering of the
insulation material. Hence Pyro bloc
insulation modules were made and
installed to form Corbel joints to suit
the site.
© Reliance Industries Ltd.
Solar panel installation of 15 MW potential identified.
Phase 1: 0.75 MW solar panel installation on water tanks is under approval
Proposed site
Typical Installation
• Site study and feasibility completed
• Site visit of EPC agency completed
• Budgetary Techno-commercial proposal
received from EPC agency.
• Financial working completed.
Renewable Energy
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Solar lamp distribution in near by villages: 34 Solar lamps of capacity to run for 4 hrs, which saves 2.8 MWH per annum conventional energy.
Solar water heaters installed in Umang Hostel
Purchasing of Renewable energy is under exploration
Rain water harvesting is being done every year @ 500 m3/day.
Renewable Energy
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S No Type of Waste Fuel used
Quantity of
waste fuel
used (Tons)
Equivalent of
Conventional energy
used (Gcal)
1 C9+ from Cracker is used in RPET burners
(earlier sent to landfill site) 270 81
2 HP residue gas to CPP
(earlier sent to flare) 10800 12866
Utilisation of Waste Material as Fuel
C9+ mixture: Generated in Cracker containing some solid particles, hence this mixture
cannot be used in main boilers considering reliable steam requirement of process plants.
It was being sent to incinerator or landfill. Later evaluated to utilize in RPET furnace for
thermic fluid heating.
Residue gas: Generated in Cracker containing mixture of Methane and Hydrogen. Normally
used in furnaces and boilers, but during high amount of Propane cracking this generation
quantity increases, hence some quantity is forced to flare. Later scheme prepared to utilize
this gas in Gas turbines for power generation.
Quantity saved in last 3 years:
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GHG Emission Reduction
Scope 1 Emissions: Fuel combustion, Flaring
Scope 2 Emissions: Import of electricity
Excluding
shutdown
flaring
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Green Supply Chain
Capacity enhancement of trucks for material transport
• Considering base line of 2011-12 truck capacity was around 10-10.5 MT
• Current truck capacity is around 17 MT indicating an increase of 70%
in truck load
• We further target to increase truck load by 5% annually.
Increase in CO2 transport to customer
• In year 2015, NMD started selling CO2 for productive use instead of venting.
• CO2 supply to customer in 2015-16 was 1931 MT which increased to 11960 MT in 2017-18
indicating rise of over 500%. Further increase of 10% is planned for it on annual basis.
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Green Supply Chain
RORO Facility for Product Transportation to
Mangalore
Transportation of the products to Mangalore
through train to avoid road transportation resulted
ìn CO2 emissions reduction
Empty bag weight reduction
Reduction of 10 gm weight of each empty bag
resulted in reduction of polymer material by
approx. 200 MT/year
130 126 120
115 110
100
120
140
Empty Bag Weight in gm
2000 2004 2010 2012 2017
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Green Supply Chain
Elimination Inter Plant movement for product loading • Truck weighing 16-35 MT was moving from one plant to another plant consuming diesel.
By eliminating inter plant movements, diesel consumption was saved.
Before
Truck reports at one
plant
Product Bags loaded
Temp tarpaulin tying
Truck reports to second
plant
Product Bags loaded
Tarpaulin tying
Now
Truck reports at one plant
Product Bags loaded
Product bags from other
plants
brought by forklifts
Tarpaulin tying
CO2 reduction of
317 Tons
(2017-18)
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Review of Energy Performance
Oversee site Energy Performance
Networking with corporate, vendors and
academics to identify improvement areas
Measurement and Monitoring
Implementing improvements
Energy Audits
Spreading Awareness
Top to bottom, bottom to top approach
Corporate Energy Cell
Site Apex
Site Energy
Cell
Small group
Working Level
Review Energy Cons. trend
Review status of schemes
Providing resources and drive
Ideating (KAIZEN) & Mission Kurukshetra
Participation in improvement projects
Evaluate & prioritize Energy schemes
Benchmarking
Guidelines to working group
Support for Decision making
Energy & Fuel Management
Weekly energy variance review with all sites
Measurement and Monitoring
Implementing improvements
Energy Audits
Spreading Awareness
Apex : (Monthly, chaired by P-NMD)
Core : (Corporate Energy Cell)
Working Team : (Site-Energy Coordinators)
Small Group : (Site)
Energy Cell : (Site)
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Energy Monitoring
Whatever gets measured gets done
Real time monitoring of Steam & Fuel
Prosteam Optimizer
Daily Monitoring &
Reporting
Energy Review with Site Apex
Energy Professionals Networking
SMART Manufacturing_
Energy dashboard
Optimizer is used for
overall steam and fuel
balance of the site.
Real time data is taken
on hourly basis and the
software recommends
the optimized way of
running the plant
- Daily monitoring
and reporting of
the steam and
fuel balance of
the site through
Daily Energy
Report
- Plant wise daily
reporting of the
energy
consumptions
Dashboards for monitoring the hourly
average data of the plant and site
parameters (including energy)
Monthly Intersite
networking of the Energy
group done for reviewing
site Energy performance
by CoE, for new
technology updates,
EnCon ideas, suggestion
and constraints.
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Monthly steam trap monitoring
Replacing all Thermodynamic traps with Bimetallic/Inverted bucket traps
Feb’18 July’18
Steam Trap Monitoring
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Norms
• Energy & Utility Norms setting is an annual exercise.
• Unit performance is assessed in detail on monthly basis with agreed norms
Intent
• Optimize the consumption of Energy & Utilities of the complex
• Establish the baseline norms for assessing plant performance throughout the year
Principle
• Setting SMART goals
• Setting stretch goals based upon benchmarks & best achieved figures considering technology and type
Standard
• Corporate standard available for setting norms for the financial year
Average of two lowest process entitlements in last three years
Adjustments done to take care of any abnormalities in technology, equipment performance, plant load, etc.,
Efficiencies of major energy intensive equipment consideration
Improvement measures under implementation & planned in financial year
CoE review & Site CTS chief approval
Benchmarking with intra-site & internationally by CoE
Quarterly review of actual norms against the target
EnCon Target Setting and Monitoring
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Capability Building Training Programs
Training Need Identification (TNI) is done at the start of the year
Other than TNI, training/awareness programs are conducted as below:
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EnCon Week
EnCon quiz
EnCon token gift
distribution
EnCon Suggestion
EnCon Crossword in School
EnCon awareness sessions in township
Involvement of all stake holders
EnCon Programs
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Involvement of School
Children
Energy awarene
ss Posters
Energy awareness Program
Mission Kurukshetra Portal
Energy Saving tips
through mail
Involvement of Family members
Involvement of
community members
Energy training
Participation in External trainings
Engagement of all stakeholders
Awareness & Involvement
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Implementation of ISO 50001:2011
ISO 50001:2011:
Energy Management
system implemented in
year 2014 and
recertified in year 2017
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GreenCo Rating
NMD Site rated as a GreenCo Gold u it as pe fulfill e t of the e ui e e ts in accordance with Gold level of GreenCo Rating System in year 2017
Attained the distinction of being the 1st Petro Chemical Complex to be rated
ith the p estigious GreenCo Rati g i the country
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Site Awards & Accolades
• Won Ce tifi ate of E elle e i 12th State Level Awards for Excellence i E e g Co se atio a d Ma age e t fo 6-17.
• Won GreenCo Gold Rating-CII in Petrochemical Sector – 2017.
• Won Natio al a a d fo E elle t E e g Effi ie t U it CII fo ea 14-15 for consecutive 3rd time.
• Won BEE National Energy Conservation Award –First prize in Petrochemical sector for the year 13-14.
• MEDA State Award for Best Energy Efficient Unit – First prize for 2013, 2014 and 2015
Energy
• Golden Peacock National Quality Award - 2012 & 2015
• RBNQA 2012 – Commendation Certificate
• RBNQA 2016 – Performance Excellence
Quality
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Site Awards & Accolades
•APEX India Afforestation Excellence Award 2017 under Platinum category
•Golden Peacock Occupational Health & Safety Award - 2013 & 2015
•Green tech Safety Award - 2013
•ICC award for Management in Health, Safety & Environment for the year 2012
•National Safety Award - Ministry of Labor, Government of India for Meritorious
Performance
•Five star accreditation from British safety Council – 2003 & 2008
•Award for Meritorious Performance from Council of Industrial Safety
•Certificate of Merit from FPA-UK for High Standards in the Mgt. of Fire Systems &
procedures
•Longest Accident Free Period from NSC – Maharashtra Chapter
• Maha asht a State Vanshree A a d - First rank
• Best Environmental & Ecological Implementation, from International Greenland
Society
• Indo-German Green-Tech Environment Excellence Award 2000-2001 & 2002-2003
Safety & Environment
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ENCON Road Map
Aggressive plan to reduce 5% Energy consumption by 2020-21.
High Energy prices, aggressive ENCON schemes
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ENCON Road Map
Plan 2018-19:
1. Steam trap replacement in GC/EOEG/CPP/O&U/LDPE/PP.
2. Engineering of SVH-SM back pressure turbine generator.
3. Engineering of GT inlet air path modification.
Plan 2019-20:
1. Installation of SVH to SM Back pressure Turbine with Synchronous Generator at CPP.
2. GT inlet air path modification to reduce pressure drop.
3. Installation of Solar panels for 0.75 MW power generation.
4. Restoration of 10-P-41A QW pump turbine to minimize steam letdown.
5. Cooling Tower-2 cooling water system augmentation.
6. Installation of new Air compressor to reduce operating costs.