NEDM Collaboration Meeting, May 19, 2008 Valve Progress Steve Williamson.
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Transcript of NEDM Collaboration Meeting, May 19, 2008 Valve Progress Steve Williamson.
nEDM Collaboration Meeting, May 19, 2008
Valve Progress
Steve Williamson
nEDM Collaboration Meeting, May 19, 2008
Goal of Valve R&D
Highest priority: the completion of a “full valve test”. Fabricate a full-sized prototype valve Use reasonable (though not necessarily final)
materials Test it under realistic conditions
LHe II inside at ~1.7 K Vacuum outside
nEDM Collaboration Meeting, May 19, 2008
Prerequisites A valve design A Facility for testing the valve
A dewar A dewar insert (for vacuum and
refrigeration) A critical parts must be tested.
Valve seat and boot Bellows assembly Valve body Plastic flange seals
nEDM Collaboration Meeting, May 19, 2008
Prototype Valve Design
Completed 2/21/08 Based on Jan’s earlier design Some features:
Uses our tested Vespel seat/boot design
Double seal (closed and open) Two sliding “linear bearings”
maintain alignment of seat/boot. Uses off-the-shelf Be-Cu
bellows Acrylic body and spool piece
nEDM Collaboration Meeting, May 19, 2008
Valve Test Apparatus Dewar (Precision Cryogenics) Received
3/12/08 Super-insulated (no LN2 shield) ~50 l “belly”
Insert (Janis) received 3/12/08 100 mW cooling power at 2K LHe throttle valve on 1K pot 6 ½” lines (1 removable) Two motion feed-thru lines Large internal vacuum volume
Combination was tested by Janis to verify 100 mW cooling power below 2 K
Should serve for pressurizer and valve testing for the project (i.e. WBS 1.4.9.6)
Internal vacuum
vessel not shown
nEDM Collaboration Meeting, May 19, 2008
Testing of Bellows Use standard Miniflex type BC-100-40-
12-1 Be-Cu bellows. Joints made with Stycast 2850FT (not
welded) Bellows was compressed 11/16” (no
extension) at a rate of about 0.8 Hz. Tests performed at 4.2 K in bucket
dewar 1000 Torr Baratron monitored vacuum
on interior of bellows. Tested on leak detector after test. Test performed twice with two different
bellows. Both bellows survived more than
500,000 cycles without failure.
nEDM Collaboration Meeting, May 19, 2008
Pressure-tested one Be-Cu Bellows (a side note) Possibly use this bellows for
hydraulic actuator Performed test at room temperature He pressure on outside, vacuum
(leak detector) inside No significant deformation/failure at
110 lbs force (~90 psi) Serious deformation at 300 lbs
(~250 psi)
Vacuum side Helium side
nEDM Collaboration Meeting, May 19, 2008
Valve Body First attempt
Machine in two parts and glue. Glued joint looked “problematic”;
technicians reject the part. Second attempt
Machine from a single block of acrylic.
Diamond machine interior Failed leak check (near blind tapped
flange holes). Holes filled and re-tapped – still leaks.
Theory: stress crack despite care Third attempt
Machine from a single block Use simplified shape Yet to be leak checked, but our best
candidate Ultimately:
Cast (expensive, long lead) Minimally machine
Machining 2nd attempt
3rd under polarized light
nEDM Collaboration Meeting, May 19, 2008
Flange Seals The design calls for “double” seals:
Acrylic-vespel-acrylic or Acrylic-copper-acrylic
Use Kapton gaskets Use silicon-bronze screws. Due differential thermal contraction,
screws end up longer than clamped flanges Leak
Strategy: use ceramic spacers and make acrylic as thin as practical. Example:
Material Length at 300 K
Length at 4K
Copper thermal contact 0.5” 0.4984”Acrylic flanges 0.35” 0.3458”
Brass screws 0.85” 0.8467”
Difference: (Brass – rest) 0” 0.0026”
1” ceramic
0.5” copper
0.35” acrylic
Acrylic-acrylic-acrylic seal
Material Integrated CTE to 4K
Ceramic (assume pyrex) -0.056%
Copper -0.325%Acrylic -1.21%
Brass -0.384%
nEDM Collaboration Meeting, May 19, 2008
Flange Seals The design calls for “double” seals:
Acrylic-vespel-acrylic or Acrylic-copper-acrylic
Use Kapton gaskets Use silicon-bronze screws. Due differential thermal contraction,
screws end up longer than clamped flanges Leak
Strategy: use ceramic spacers and make acrylic as thin as practical. Example:
Material Length at 300 K
Length at 4K
Ceramic spacers 1” 0.9994”
Copper thermal contact 0.5” 0.4984”Acrylic flanges 0.35” 0.3458”
Brass screws 1.85” 1.8429”
Difference: (Brass – rest) 0” -0.0007”
1” ceramic
0.5” copper
0.35” acrylic
Acrylic-acrylic-acrylic seal
Material Integrated CTE to 4K
Ceramic (assume pyrex) -0.056%
Copper -0.325%Acrylic -1.21%
Brass -0.384%
nEDM Collaboration Meeting, May 19, 2008
Test of flange seals Tests on smaller flanges were
successful. Test of two double seals on a
simple tube Performed in new valve test
dewar. No leaks at 77 K Leaked at 4K
nEDM Collaboration Meeting, May 19, 2008
Flange Seal Leak
Could be due to change of Kapton seal design. Holes through gasket for
better force transfer But may produce less force
per unit area Could be due to leak in
exhaust line Copper tube Stycast to
acrylic Leak check at room
temperature should answer this
Old Design
New Design
Possible leak here
nEDM Collaboration Meeting, May 19, 2008
Plans Solve double flange seal problem
Probably return to bucket dewar (lower LHe cost, faster cool-down)
Try earlier gasket design Use thin (0.2 total”) acrylic in seal region
Assemble and test with “simplified” body design and single valve seat. Body, spool piece, and bellows assembly
are already complete Finish seat and stem (when seal design
perfected) Some small adaptations of actuator
required for new dewar Success of this valve could be
considered to complete R&D project
nEDM Collaboration Meeting, May 19, 2008
Future Steps Double sealing valve
Necessary if Be-Cu proves unfriendly Requires additional alteration of actuator 2X longer travel Spring to allow force control when retracting
“Non-pressurizing” valve If no free surfaces, then closing valve will pressurize
LHe (and squirt depolarized 3He into the system) Use a second set of bellows (one set extends, the
other retracts) to maintain constant volume. In-line valve
Needed above and below IV1
nEDM Collaboration Meeting, May 19, 2008
Another Issue If bellows is not 3He friendly…
With valve closed, “top” side of valve is exposed unfriendly surface
This is not fixed by double seal action. May require “hiding” the bellows
Telescoping shield? Polyimide flexible coating inside bellows? Kapton bellows?
“Origami” Kapton bellows
We need to test more materials for 3He depolarization.