mook koon BiTS 2013 Rev2 w. Taber fixes2013 BiTS Workshop ~ March 3 - 6, 2013 Paper #2 1...

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Session 1 BiTS Workshop 2013 Archive STREAMLINING OPERATIONS Test operations, generally considered costly, yet necessary, add value to device manufacturing when optimized for efficiency. This session offers a variety of approaches that promise high yields, lean manufacturing, maximized performance at minimal costs, and optimized production times. The first paper discusses a method of incorporating multidimensional Monte Carlo analysis simulation with known design parameters to focus manufacturing improvement efforts and maximize alignment performance while minimizing costs. Presented next is a method for redefining test tooling design rules to gain process margin and prevent substrate chipping caused by test handler misalignment. Zero-cost, software based, virtual tool checkers that bring the whole production area towards a manufacturing LEAN direction is then discussed. Wrapping things up is a paper on a screwless socket and dual pin testing concept said to greatly enhance the robustness and efficiency of IC testing. Improving Socket Alignment Performance Using Monte Carlo Analysis Techniques and Manufacturing Controls Daniel DelVecchio, Dustin AllisonInterconnect Devices Incorporated Tooling Stack-up Process Margin Improvement Mook Koon Wong, Boon Hor PheeIntel Malaysia Zero Cost Virtual Tool Checker Seong Guan OoiIntel Technology Sdn. Bhd. Enablers for Robust & Fast Online Trouble-shooting for High Parallelism Testing Benedict LohInfineon Technologies Kohei HironakaNHK Spring Co. Ltd. Michelle NgTestPro COPYRIGHT NOTICE The paper(s) in this publication comprise the Proceedings of the 2013 BiTS Workshop. The content reflects the opinion of the authors and their respective companies. They are reproduced here as they were presented at the 2013 BiTS Workshop. This version of the papers may differ from the version that was distributed in hardcopy & softcopy form at the 2013 BiTS Workshop. The inclusion of the papers in this publication does not constitute an endorsement by BiTS Workshop, LLC or the workshop’s sponsors. There is NO copyright protection claimed on the presentation content by BiTS Workshop, LLC. (Occasionally a Tutorial and/or TechTalk may be copyrighted by the author). However, each presentation is the work of the authors and their respective companies: as such, it is strongly encouraged that any use reflect proper acknowledgement to the appropriate source. Any questions regarding the use of any materials presented should be directed to the author(s) or their companies. The BiTS logo and ‘Burn-in & Test Strategies Workshop’ are trademarks of BiTS Workshop, LLC. All rights reserved. This Paper

Transcript of mook koon BiTS 2013 Rev2 w. Taber fixes2013 BiTS Workshop ~ March 3 - 6, 2013 Paper #2 1...

  • Session 1

    BiTS Workshop 2013 Archive

    STREAMLINING OPERATIONS

    Test operations, generally considered costly, yet necessary, add value to device manufacturing when optimized for efficiency. This session offers a variety of approaches that promise high yields, lean manufacturing, maximized performance at minimal costs, and optimized production times. The first paper discusses a method of incorporating multidimensional Monte Carlo analysis simulation with known design parameters to focus manufacturing improvement efforts and maximize alignment performance while minimizing costs. Presented next is a method for redefining test tooling design rules to gain process margin and prevent substrate chipping caused by test handler misalignment. Zero-cost, software based, virtual tool checkers that bring the whole production area towards a manufacturing LEAN direction is then discussed. Wrapping things up is a paper on a screwless socket and dual pin testing concept said to greatly enhance the robustness and efficiency of IC testing.

    Improving Socket Alignment Performance Using Monte Carlo Analysis Techniques and Manufacturing Controls

    Daniel DelVecchio, Dustin Allison—Interconnect Devices Incorporated

    Tooling Stack-up Process Margin Improvement Mook Koon Wong, Boon Hor Phee—Intel Malaysia

    Zero Cost Virtual Tool Checker Seong Guan Ooi—Intel Technology Sdn. Bhd.

    Enablers for Robust & Fast Online Trouble-shooting for High Parallelism Testing

    Benedict Loh—Infineon Technologies Kohei Hironaka—NHK Spring Co. Ltd.

    Michelle Ng—TestPro

    COPYRIGHT NOTICE The paper(s) in this publication comprise the Proceedings of the 2013 BiTS Workshop. The content reflects the opinion of the authors and their respective companies. They are reproduced here as they were presented at the 2013 BiTS Workshop. This version of the papers may differ from the version that was distributed in hardcopy & softcopy form at the 2013 BiTS Workshop. The inclusion of the papers in this publication does not constitute an endorsement by BiTS Workshop, LLC or the workshop’s  sponsors.

    There is NO copyright protection claimed on the presentation content by BiTS Workshop, LLC. (Occasionally a Tutorial and/or TechTalk may be copyrighted by the author). However, each presentation is the work of the authors and their respective companies: as such, it is strongly encouraged that any use reflect proper acknowledgement to the appropriate source. Any questions regarding the use of any materials presented should be directed to the author(s) or their companies.

    The  BiTS  logo  and  ‘Burn-in  &  Test  Strategies  Workshop’  are  trademarks  of  BiTS  Workshop,  LLC.  All  rights  reserved.

    This Paper

  • 2013 BiTS Workshop ~ March 3 - 6, 2013

    Paper #21

    Streamlining Operations

    Session 1

    Tooling Stack-up Process Margin Improvement

    2013 BiTS WorkshopMarch 3 - 6, 2013

    Wong Mook KoonPhee Boon HorIntel Malaysia

    Conference Ready 2/10/2013

    3/2013 Tooling Stack-up Process Margin Improvement

    Agenda

    • Background• Problem statement • Current Status and Technical Challenges• Solution• Check Result• Summary• Acknowledgement

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    3/2013 Tooling Stack-up Process Margin Improvement

    Background

    • IC transistor size reducing ~12% per year• Number of transistors increasing, ~39% per year• Package IO increasing

    • Land/Ball Pitch need to be reduced to control package

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    Figure 1: IC transistor feature size has decreased and number of transistors per chip has gone up, but in relatively higher proportion. (Source www.ieee.org)

    3/2013 Tooling Stack-up Process Margin Improvement

    Problem statement• Semiconductor process challenges: Number of IO

    increased and Ball Pitch reduced Impacts:1. Unit handling method inside handler at final test

    • Thermal contact resistance challenges at different M/C• Substrate real estate & Keep out Zone challenges (top

    and bottom side)2. Test tooling stack up process margin and test interface

    challenges• Low yield issue (Fail open test)• Quality issue (mechanical defects )• Tooling wear out

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  • 2013 BiTS Workshop ~ March 3 - 6, 2013

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    3/2013 Tooling Stack-up Process Margin Improvement

    Current Status & Technical Challenge• Unit handling method inside handler at final test -

    Substrate edge handling

    Nozzle pick up unit Place unit on carrier

    Test ChuckPick up unit on

    carrier

    Test chuckPush unit on

    carrier against load board

    Load Board

    Test ChuckPick up Unit on

    carrier

    Test Chuck

    Heater

    Substrate edge rest on carrier

    Nozzle

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    3/2013 Tooling Stack-up Process Margin Improvement

    Current Status & Technical Challenge• Inefficiency of substrate edge handling methodology

    – Substrate size, land & ball pitch to substrate edge reduced– Impact: space constrain at unit holding edge

    Substrate edge rest on carrier

    Bottom View Substrate edge rest on carrier

    SRO/Solder Ball distance to substrate perimeter decreased

    Solder Ball/Land Pad hit on Carrier edge

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  • 2013 BiTS Workshop ~ March 3 - 6, 2013

    Paper #24

    Streamlining Operations

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    3/2013 Tooling Stack-up Process Margin Improvement 7TS Side view

    PKG

    • Test tooling stack up process margin and test interface challenges- Chuck Z-motion inside handler may cause package bottom

    surface to hit test socket’s Anvil Surface under worst case condition

    Current Status & Technical Challenge

    3/2013 Tooling Stack-up Process Margin Improvement 8

    – Test tooling stack up process margin and test interface challenges (cont’d)

    – Guide plate opening too loose, Test results fail open due to Pogo pin not contacting SRO

    .

    Pogo pin Socket Guide plate opening

    TS Side view

    PKG

    SRO

    Current Status & Technical Challenge

  • 2013 BiTS Workshop ~ March 3 - 6, 2013

    Paper #25

    Streamlining Operations

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    3/2013 Tooling Stack-up Process Margin Improvement

    Current Status & Technical Challenge

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    – Test tooling stack up process margin and test interface challenges

    – Carrier guide hole deterioration due to occasional crash by guide pin and wear out

    – Need to physically measure carrier guide hole dimensions to avoid substrate hit on Test Socket’s top plate

    Worn Out

    3/2013 Tooling Stack-up Process Margin Improvement

    Unit handling method inside handler at final test 1. Combine Nozzle assembly with Test chuck 2. Change substrate rest at edge to Substrate corner

    Solution- Problem 1

    Nozzle pick up unit

    Nozzle Assembly

    Test Chuck pick up Unit on carrier

    Test Chuck

    Heater

    Test Chuck

    Test Chuck with nozzle to pick unit

    Substrate edge rest on carrier Substrate corner rest on carrier 10

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    3/2013 Tooling Stack-up Process Margin Improvement 11

    Solution- Problem 1

    • 1st Substrate edge handling– High land/ball pad depopulate – Not cost effective due to increase in substrate real estate

    • 2nd Combine Nozzle with Test Chuck– Thermal resistance not met, need longer soak time to start of test– Change equipment handler handling method, cost concern

    • 3rd Substrate corner handling– Cost effective– Minimum solder ball depopulate– Maintain current thermal performance and run rate

    Unit handling method inside handler at final test

    3/2013 Tooling Stack-up Process Margin Improvement

    Solution- problem 2• Test tooling stack up process margin and test interface

    challenges• Re-design the Guide Plate to gain tooling stack up process margin

    • Optimize socket total height - Increase Z-height Gap from negative to positive during unit to test socket pre engagement

    • Optimize Lead In chamfer depth - Increase the X-directional allowance

    Before After12

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    Solution- problem 2

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    • Test tooling stack up process margin and test interface challenges• Strengthen Seal plate guide hole of carrier with metal sheet

    reinforcement• Carrier condition indication line to eliminate measurement

    3/2013 Tooling Stack-up Process Margin Improvement

    Check results

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    • Results Summary– Under worst case Test Check misalignment condition, substrate

    damage will occur except if carrier is in good condition + with optimized socket guide

    – Minor misalignment will not cause substrate damage if the carrier is in good condition, regardless of POR or optimized socket guide

    • Conclusion– Controlling the carrier guide hole condition is crucial in

    determining the substrate damage risk – Optimized socket guide will definitely buy additional process

    margin to prevent substrate damage

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    Streamlining Operations

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    Conclusion

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    • Summary– Optimized Test Socket Guide plate vertical wall

    and chamfer lead in depth demonstrated process margin improvement

    – Carrier guide hole condition is key factor to ensure good quality tooling stack up

    – Substrate Corner handling method is solution for Thermal concern, Substrate real estate and land pad/Ball depopulation issue

    3/2013 Tooling Stack-up Process Margin Improvement

    Acknowledgement

    • LT Yew (Test Engineering Manager)• TS Yeoh (Principal Engineer)• Jensen, Morten S. (Committee member)

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