mook koon BiTS 2013 Rev2 w. Taber fixes · 2013-04-04 · 2013 BiTS Workshop ~ March 3 - 6, 2013...

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Session 1 BiTS Workshop 2013 Archive STREAMLINING OPERATIONS Test operations, generally considered costly, yet necessary, add value to device manufacturing when optimized for efficiency. This session offers a variety of approaches that promise high yields, lean manufacturing, maximized performance at minimal costs, and optimized production times. The first paper discusses a method of incorporating multidimensional Monte Carlo analysis simulation with known design parameters to focus manufacturing improvement efforts and maximize alignment performance while minimizing costs. Presented next is a method for redefining test tooling design rules to gain process margin and prevent substrate chipping caused by test handler misalignment. Zero-cost, software based, virtual tool checkers that bring the whole production area towards a manufacturing LEAN direction is then discussed. Wrapping things up is a paper on a screwless socket and dual pin testing concept said to greatly enhance the robustness and efficiency of IC testing. Improving Socket Alignment Performance Using Monte Carlo Analysis Techniques and Manufacturing Controls Daniel DelVecchio, Dustin AllisonInterconnect Devices Incorporated Tooling Stack-up Process Margin Improvement Mook Koon Wong, Boon Hor PheeIntel Malaysia Zero Cost Virtual Tool Checker Seong Guan OoiIntel Technology Sdn. Bhd. Enablers for Robust & Fast Online Trouble-shooting for High Parallelism Testing Benedict LohInfineon Technologies Kohei HironakaNHK Spring Co. Ltd. Michelle NgTestPro COPYRIGHT NOTICE The paper(s) in this publication comprise the Proceedings of the 2013 BiTS Workshop. The content reflects the opinion of the authors and their respective companies. They are reproduced here as they were presented at the 2013 BiTS Workshop. This version of the papers may differ from the version that was distributed in hardcopy & softcopy form at the 2013 BiTS Workshop. The inclusion of the papers in this publication does not constitute an endorsement by BiTS Workshop, LLC or the workshop’s sponsors. There is NO copyright protection claimed on the presentation content by BiTS Workshop, LLC. (Occasionally a Tutorial and/or TechTalk may be copyrighted by the author). However, each presentation is the work of the authors and their respective companies: as such, it is strongly encouraged that any use reflect proper acknowledgement to the appropriate source. Any questions regarding the use of any materials presented should be directed to the author(s) or their companies. The BiTS logo and ‘Burn-in & Test Strategies Workshop’ are trademarks of BiTS Workshop, LLC. All rights reserved. This Paper

Transcript of mook koon BiTS 2013 Rev2 w. Taber fixes · 2013-04-04 · 2013 BiTS Workshop ~ March 3 - 6, 2013...

Page 1: mook koon BiTS 2013 Rev2 w. Taber fixes · 2013-04-04 · 2013 BiTS Workshop ~ March 3 - 6, 2013 Paper #2 1 Streamlining Operations Session 1 Tooling Stack-up Process Margin Improvement

Session 1

BiTS Workshop 2013 Archive

STREAMLINING OPERATIONS

Test operations, generally considered costly, yet necessary, add value to device manufacturing when optimized for efficiency. This session offers a variety of approaches that promise high yields, lean manufacturing, maximized performance at minimal costs, and optimized production times. The first paper discusses a method of incorporating multidimensional Monte Carlo analysis simulation with known design parameters to focus manufacturing improvement efforts and maximize alignment performance while minimizing costs. Presented next is a method for redefining test tooling design rules to gain process margin and prevent substrate chipping caused by test handler misalignment. Zero-cost, software based, virtual tool checkers that bring the whole production area towards a manufacturing LEAN direction is then discussed. Wrapping things up is a paper on a screwless socket and dual pin testing concept said to greatly enhance the robustness and efficiency of IC testing.

Improving Socket Alignment Performance Using Monte Carlo Analysis Techniques and Manufacturing Controls

Daniel DelVecchio, Dustin Allison—Interconnect Devices Incorporated

Tooling Stack-up Process Margin Improvement Mook Koon Wong, Boon Hor Phee—Intel Malaysia

Zero Cost Virtual Tool Checker Seong Guan Ooi—Intel Technology Sdn. Bhd.

Enablers for Robust & Fast Online Trouble-shooting for High Parallelism Testing

Benedict Loh—Infineon Technologies Kohei Hironaka—NHK Spring Co. Ltd.

Michelle Ng—TestPro

COPYRIGHT NOTICE The paper(s) in this publication comprise the Proceedings of the 2013 BiTS Workshop. The content reflects the opinion of the authors and their respective companies. They are reproduced here as they were presented at the 2013 BiTS Workshop. This version of the papers may differ from the version that was distributed in hardcopy & softcopy form at the 2013 BiTS Workshop. The inclusion of the papers in this publication does not constitute an endorsement by BiTS Workshop, LLC or the workshop’s  sponsors.

There is NO copyright protection claimed on the presentation content by BiTS Workshop, LLC. (Occasionally a Tutorial and/or TechTalk may be copyrighted by the author). However, each presentation is the work of the authors and their respective companies: as such, it is strongly encouraged that any use reflect proper acknowledgement to the appropriate source. Any questions regarding the use of any materials presented should be directed to the author(s) or their companies.

The  BiTS  logo  and  ‘Burn-in  &  Test  Strategies  Workshop’  are  trademarks  of  BiTS  Workshop,  LLC.  All  rights  reserved.

This Paper

Page 2: mook koon BiTS 2013 Rev2 w. Taber fixes · 2013-04-04 · 2013 BiTS Workshop ~ March 3 - 6, 2013 Paper #2 1 Streamlining Operations Session 1 Tooling Stack-up Process Margin Improvement

2013 BiTS Workshop ~ March 3 - 6, 2013

Paper #21

Streamlining Operations

Session 1

Tooling Stack-up Process Margin Improvement

2013 BiTS WorkshopMarch 3 - 6, 2013

Wong Mook KoonPhee Boon HorIntel Malaysia

Conference Ready 2/10/2013

3/2013 Tooling Stack-up Process Margin Improvement

Agenda

• Background• Problem statement • Current Status and Technical Challenges• Solution• Check Result• Summary• Acknowledgement

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2013 BiTS Workshop ~ March 3 - 6, 2013

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Background

• IC transistor size reducing ~12% per year• Number of transistors increasing, ~39% per year• Package IO increasing

• Land/Ball Pitch need to be reduced to control package

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Figure 1: IC transistor feature size has decreased and number of transistors per chip has gone up, but in relatively higher proportion. (Source www.ieee.org)

3/2013 Tooling Stack-up Process Margin Improvement

Problem statement• Semiconductor process challenges: Number of IO

increased and Ball Pitch reduced Impacts:1. Unit handling method inside handler at final test

• Thermal contact resistance challenges at different M/C• Substrate real estate & Keep out Zone challenges (top

and bottom side)2. Test tooling stack up process margin and test interface

challenges• Low yield issue (Fail open test)• Quality issue (mechanical defects )• Tooling wear out

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Current Status & Technical Challenge• Unit handling method inside handler at final test -

Substrate edge handling

Nozzle pick up unit Place unit on carrier

Test ChuckPick up unit on

carrier

Test chuckPush unit on

carrier against load board

Load Board

Test ChuckPick up Unit on

carrier

Test Chuck

Heater

Substrate edge rest on carrier

Nozzle

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3/2013 Tooling Stack-up Process Margin Improvement

Current Status & Technical Challenge• Inefficiency of substrate edge handling methodology

– Substrate size, land & ball pitch to substrate edge reduced– Impact: space constrain at unit holding edge

Substrate edge rest on carrier

Bottom View Substrate edge rest on carrier

SRO/Solder Ball distance to substrate perimeter decreased

Solder Ball/Land Pad hit on Carrier edge

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Paper #24

Streamlining Operations

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3/2013 Tooling Stack-up Process Margin Improvement 7TS Side view

PKG

• Test tooling stack up process margin and test interface challenges- Chuck Z-motion inside handler may cause package bottom

surface to hit test socket’s Anvil Surface under worst case condition

Current Status & Technical Challenge

3/2013 Tooling Stack-up Process Margin Improvement 8

– Test tooling stack up process margin and test interface challenges (cont’d)

– Guide plate opening too loose, Test results fail open due to Pogo pin not contacting SRO

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Pogo pin Socket Guide plate opening

TS Side view

PKG

SRO

Current Status & Technical Challenge

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Current Status & Technical Challenge

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– Test tooling stack up process margin and test interface challenges

– Carrier guide hole deterioration due to occasional crash by guide pin and wear out

– Need to physically measure carrier guide hole dimensions to avoid substrate hit on Test Socket’s top plate

Worn Out

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Unit handling method inside handler at final test 1. Combine Nozzle assembly with Test chuck 2. Change substrate rest at edge to Substrate corner

Solution- Problem 1

Nozzle pick up unit

Nozzle Assembly

Test Chuck pick up Unit on carrier

Test Chuck

Heater

Test Chuck

Test Chuck with nozzle to pick unit

Substrate edge rest on carrier Substrate corner rest on carrier 10

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Solution- Problem 1

• 1st Substrate edge handling– High land/ball pad depopulate – Not cost effective due to increase in substrate real estate

• 2nd Combine Nozzle with Test Chuck– Thermal resistance not met, need longer soak time to start of test– Change equipment handler handling method, cost concern

• 3rd Substrate corner handling– Cost effective– Minimum solder ball depopulate– Maintain current thermal performance and run rate

Unit handling method inside handler at final test

3/2013 Tooling Stack-up Process Margin Improvement

Solution- problem 2• Test tooling stack up process margin and test interface

challenges• Re-design the Guide Plate to gain tooling stack up process margin

• Optimize socket total height - Increase Z-height Gap from negative to positive during unit to test socket pre engagement

• Optimize Lead In chamfer depth - Increase the X-directional allowance

Before After12

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Solution- problem 2

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• Test tooling stack up process margin and test interface challenges• Strengthen Seal plate guide hole of carrier with metal sheet

reinforcement• Carrier condition indication line to eliminate measurement

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Check results

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• Results Summary– Under worst case Test Check misalignment condition, substrate

damage will occur except if carrier is in good condition + with optimized socket guide

– Minor misalignment will not cause substrate damage if the carrier is in good condition, regardless of POR or optimized socket guide

• Conclusion– Controlling the carrier guide hole condition is crucial in

determining the substrate damage risk – Optimized socket guide will definitely buy additional process

margin to prevent substrate damage

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Conclusion

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• Summary– Optimized Test Socket Guide plate vertical wall

and chamfer lead in depth demonstrated process margin improvement

– Carrier guide hole condition is key factor to ensure good quality tooling stack up

– Substrate Corner handling method is solution for Thermal concern, Substrate real estate and land pad/Ball depopulation issue

3/2013 Tooling Stack-up Process Margin Improvement

Acknowledgement

• LT Yew (Test Engineering Manager)• TS Yeoh (Principal Engineer)• Jensen, Morten S. (Committee member)

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