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    Concrete international / FEBRUARY 2007  61

    BY MARCO ROSIGNOLI

    Even though the Reggiolo Overpass in Reggiolo, Italy, is

    a small bridge, several factors complicated its design

    and construction. The bridge, completed in 2003, spans

    the Verona-Mantua Railway that had to remain fully

    operational during construction. This made the formwork

    and shoring that would have been necessary for the

    originally designed cast-in-place bridge difficult to locate

    and construct. Its location over a working railway also led

    to the owner’s desire for minimal long-term maintenance,

    resulting in the selection of a monolithic, fully prestressedstructure instead of a steel or precast/prestressed

    girder system.

    Settling soils at the site also affected the design. The

    structure was simply-supported so that higher-than-

    expected foundation settlements could be recovered by

    Monolithic Launch

    of the ReggioloOverpass

    An example of an innovative construction method

    shimming at the abutments, and the structure was

    lightened by using high-density polystyrene blocks to fill

    voids between the top and bottom slabs. These blocks

    also eliminated empty cells that require inspection and

    can gather water, further reducing maintenance. The

    bridge also had a complex, trapezoidal plan geometry as

    a result of the entry and exit ramps that converged on

    the overpass.

    The demanding requirements were met by casting

    the superstructure on one side of the span, and thenmonolithically launching it over the railway into its final

    position. Similar construction techniques have been

    adopted for Italian railway overpasses,1 but in this case,

    the small dimensions and complex geometry suggested

    monolithic, rather than incremental, launching.

    DECK DESIGNAs shown in Fig. 1, the superstructure of the overpass

    is a multi-cellular, prestressed concrete plate spanning

    26 m (85.3 ft). The bottom surface is horizontal in the

    transverse direction and slightly inclined longitudinally,

    but the top surface is inclined in both directions toshed water, so that the total thickness of the structure

    varies from 1.28 to 1.35 m (4.2 to 4.4 ft), with a mean

    span-to-depth ratio of about 20. A varying-depth paving

    layer would have been excessively heavy on such

    a wide deck.

    In the transverse direction, the plate is stiffened by

    three 0.4 m (15.7 in.) thick internal diaphragms spaced

    at 6.5 m (21.3 ft) and two 1.0 m (3.3 ft) thick end beams

    at the abutments. A section at the midspan diaphragm

    is shown in Fig. 2. Because the launch supports were

    aligned with the three internal longitudinal webs and

    the side cantilevers ranged from 3.24 to 6.30 m (10.6 to

    Fig. 1: Plan view of the internal stiffening systems in the deck plate

    (All dimensions in meters; 1 m = 3.28 ft)

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    20.7 ft), a high level of prestress in the transverse direction

    was required during launching. In addition, the transverse

    negative moment was increased by the concentrated load

    of the edge beam.

    The prestressing level in the superstructure was

    quite high because of the railway authority’s request for

    a fully prestressed section in both the longitudinal and

    transverse directions under full design loads (dead

    and superimposed dead loads, live loads inclusive of

    dynamic amplification, and thermal gradients) and also

    during launching. In spite of the short construction

    duration, consideration of time-dependent launch

    stresses2 was required.

    The prestressing included: a) longitudinal launch

    tendons in the internal webs and edge beams; b)

    longitudinal tendons in the bottom slab, tensioned

    after launch completion; c) transverse tendons in the

    end beams and internal diaphragms, all tensioned

    before launching; and d) transverse tendons in the

    deck slab, also tensioned before launching.

    Fig. 2: Cross-section of the deck slab at the midspan diaphragm (All dimensions inmeters; 1 m = 3.28 ft)

    Fig. 3: Support points of the deck plate during launching (All dimensions in meters;

    1 m = 3.28 ft)

    DECK CONSTRUCTIONAfter casting the foundation piles and the two

    abutments, the casting yard was built on the embankment

    leading to the launch abutment. It consisted of three

    parallel 1.8 m (5.9 ft) deep foundation beams spaced5.5 m (18.0 ft) apart to match the spacing of the three

    internal webs (Fig. 3).

    The foundation beams were anchored to the launch

    abutment to minimize settlement and transfer the launch

    forces to the abutment. Figure 4 shows the deck after it

    was lifted from the foundation beams for prelaunch

    weighing and shows the wide cantilever at the rear deck

    section. Before launching, the deck was painted and

    equipped with safety fences and guard rails.

    The three prestressed concrete launching noses

    at the front of the deck (Fig. 5) were constructed to

    control negative moments at the front of the bridge by

    shortening the cantilevered span that the deck would

    have to carry before reaching another support. They

    also limited the safety factor for deck overturning about

    the launch abutment to a minimum

    of 1.5. The noses were 3 m (9.8 ft)

    long, 0.60 m (2 ft) thick, and 1.15 m

    (3.8 ft) deep and aligned with the

    three internal webs. As shown in

    Fig. 5, each nose was anchored to

    the corresponding deck web with

    eight 36 mm (1.4 in.) prestressing

    bars. These overlapped the ends

    of the four launch tendons (Fig. 1).Shear keys on the contact surface

    between the deck and noses

    were match-cast to transfer vertical

    forces from the nose to the deck.

    Steel braces joined the three

    noses together.

    Short prestressed concrete noses

    such as these, that are detached and

    demolished after launch completion,

    are often less expensive than

    conventional steel girders, especially

    when the negative moments are toohigh to allow full-span launching of

    the prestressed deck.3 As shown in

    Fig. 6, the high negative moments

    were alleviated by cutting the launch

    span in half using a temporary, three-

    tower steel pier placed near the

    railway. Each tower was vertically

    supported by a foundation pile, and

    the tops of the towers were anchored

    to the launch abutment with rigid

    stays that resisted the horizontal

    forces from sliding friction.

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    Because of its varying width,

    the deck alignment could not be

    maintained with conventional lateral

    guides during launching.4 Instead,

    guide pins at the rear of the deck and

    at the launch abutment were used.

    These pins guided the bridge through

    a steel-lined recess in the underside

    of the deck (Fig. 2). At the temporary

    pier, the central guide was used to

    laterally stabilize the pier through

    the deck.

    After tensioning the launch

    prestressing tendons (transverse

    tendons in the end beams and the

    internal diaphragms, transverse

    slab tendons, and longitudinal launch

    tendons), the deck plate was lifted

    off the foundation beams using three

    rows of hydraulic sliding supports

    aligned with the foundation beams

    and the internal deck webs (Fig. 3).

    Because the launching tendons were

    tensioned while the structure was

    resting on the foundation beams,

    a portion of the prestressing force

    may have been lost to friction

    between the structure and the

    foundation beams. This required

    a final check of the prestressingforce after lifting the structure. The

    strands were retensioned if found to

    be at less than 98% of the design

    value. The deck was also weighed to

    confirm its theoretical weight, and

    measured deflections were compared

    to theoretical deflections for an

    indirect evaluation of the modulus of

    elasticity of the concrete.5

    With the bridge supported on 2 or

    3 rows of hydraulic sliding supports,

    hydraulic pistons acting betweenthe deck and the foundation beams

    (Fig. 7) pushed the bridge forward

    out over the span. After launching

    the desired distance, the support

    points for the bridge were changed,

    and the pistons were repositioned.

    This process was repeated in

    several stages, as illustrated in

    Fig. 8, until the bridge reached its

    final position.

    After releasing and dismantling

    the launch noses, the bottom slab

    Fig. 4: Deck weighing before launching through transducer-controlled hoisting. Thefour blockouts in the foundation beam house the hydraulic jacks at the supportpoints shown in Fig. 3

    Fig. 5: The prestressed concrete launch noses were connected with steel bracingand were used to control negative moments while the bridge was launched. Theywere removed after the bridge was in its final location

    Fig. 6: Temporary steel towers were used to cut the span of the bridge in halfduring the launch. The steel braces connected the top of the tower to the launchabutment and resisted the lateral forces at the support points

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    tendons were tensioned and grouted, the supports at the

    temporary towers were removed, and the bridge was

    placed on permanent laminated-rubber bearings at thetwo abutments.

     Additional considerations and comments

    The temporary stresses in the deck plate during

    the monolithic launch were analyzed at the beginning

    and end of each launch stage and at intermediate

    stages where necessary. A three-dimensional grillage

    model was used for this analysis because a two-

    dimensional beam model would have lead to excessively

    approximate results.6 The analyses also accounted for

    settlement of the temporary pier and the prescribed

    tolerances in the support reactions in both thelongitudinal and the transverse direction. Comparison

    of the results of launching and service load analyses

    showed that positive moments in the longitudinal webs

    were governed by service conditions, while launching

    governed negative moments (these negative moments

    would have been totally absent in the case of conventional

    deck construction on shoring). Although these temporary

    stresses increased the cost of prestressing the deck, the

    erection, dismantling, and materials for scaffold-type

    shoring on piles and the higher embankments required

    for working clearance above the railways would have

    generated about 12% higher costs.

    The launch equipment was particularly inexpensive.

    Because of the bridge’s modest weight—about 8900 kN

    (1000 ton)—a pair of small long-stroke launch pistons(Fig. 7) generated adequate operational speed at minimal

    cost.4 The use of hydraulic launch supports in the casting

    yard instead of conventional continuous low-friction

    extraction rails7 generated substantial savings in this

    bridge because three 27.6 m (90.6 ft) long steel rails

    would have been particularly expensive. In addition, deck

    lifting permitted real-time monitoring of the support

    reactions during launching, as well as compensating for

    the settlements of the support embankment.

    To further save manpower, new types of sliding supports

    were tested at the temporary pier, where Teflon® plates

    were placed directly onto the hoisting jacks and longstainless steel sheets were inserted between the hoisting

    jacks and the bridge for long-stroke continuous sliding

    (Fig. 6). The result was encouraging, although loss of the

    compensating effect of the rubber sheets of conventional

    low-friction bearing pads is acceptable only when hydraulic

    launch supports are used, and the nonpolished,

    nontensioned surface of the stainless steel sheets

    unavoidably increased sliding friction.

    Accurate load testing of the deck plate after launch

    completion confirmed the absence of any nonlinearity as

    a result of the launch process, and the prescribed

    absence of longitudinal and transverse tensile stresses

    Fig. 7: Paired launch pistons and central anti-drift guide at the rear deck end

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    Marco Rosignoli recently joined HNTB Corp.

    as Chief Bridge Engineer in the Seattle, WA,

    office after working 8 years as a Site

    Manager for bridge projects, 7 years as the

    Technical Director for a major Italian bridge

    contractor, and 9 years as a freelance

    bridge consultant. He has authored two

    books and several publications on the

    incremental-launching construction of

    bridges and also provides independent design checking of

    launching gantries and movable formwork systems.

    during launching was monitored in real time through

    hydraulic control of the support reactions and comparison

    with their theoretical values.

    SAFE AND RELIABLEThis application of the monolithic-launch construction

    method demonstrated its reliability and safety.8 Adoption

    of this method allowed a delicate and complex bridge to

    be built with extreme safety for the workers, in a short

    timeframe, and without any restriction on the railway

    traffic below. The adverse effects of soil settlement were

    completely avoided by casting the superstructure on stiff

    foundation beams with inexpensive forms,9 thus improving

    the quality of the structure.

     Acknowledgments

    The Reggiolo Overpass was built by the firm Locatelli, SpA, for

    the owner Autostrada del Brennero, represented by G. Andreani.

    The general designer of the motorway bypass was Sembenelli

    Consulting. The author designed the prestressed deck plate for both

    launch and service load stages, performed independent design

    checking of the launch equipment for the owner, and supervised the

    launch process and final load testing.

    References

    1. Rosignoli, M., “Site Restrictions Challenge Bridge Design,”

    Concrete International , V. 20, No. 8, Aug. 1998, pp. 40-43.

    2. Rosignoli, M., “Creep Effects During Launch of the Serio River

    Bridge,” Concrete International , V. 22, No. 3, Mar. 2000, pp. 53-58.

    3. Rosignoli, M., “Nose-Deck Interaction in Launched Prestressed

    Concrete Bridges,” Journal of Bridge Engineering , V. 3, No. 1, Feb.

    1998, pp. 21-27.

    4. Rosignoli, M., “Thrust and Guide Devices for Launched

    Bridges,” Journal of Bridge Engineering , V. 5, No. 1, Feb. 2000, pp. 75-83.

    5. Rosignoli, M., Launched Bridges, ASCE Press, Reston, VA, 1998,

    363 pp.

    6. Rosignoli, M., “Reduced-Transfer-Matrix Method for Analysis of

    Launched Bridges,” ACI Structural Journal , V. 94, No. 4, July-Aug.

    1999, pp. 603-608.

    7. Rosignoli, M., Bridge Launching , Thomas Telford, Ltd., London,

    2002, 342 pp.

    8. Rosignoli, M., “Incremental Bridge Launching,” Concrete

     International , V. 19, No. 2, Feb. 1997, pp. 36-40.

    9. Rosignoli, M., “Deck Segmentation and Yard Organization for

    Launched Bridges,” Concrete International , V. 23, No. 2, Feb. 2001,

    pp. 64-73.

    Selected for reader interest by the editors.

    Fig. 8: Launch sequence for the Reggiolo Overpass