Mic Valhall Olf
-
Author
david-rodrigues -
Category
Documents
-
view
9 -
download
1
Embed Size (px)
description
Transcript of Mic Valhall Olf
-
Valhall Corrosion Events and ManagementLearning Pack
EldarLarsen,HeadofOperations,BPNorway.
-
INTERNALDISTRIBUTIONONLY 2
ValhallCorrosion Events - Summary
Summary
HydrocarbonleakHIPOon6thMarch2009causedbyMicrobialInducedCorrosion(MIC)
resultedincrudeandgasleak,FirstAidIncident,emergencyplantshutdown&muster.
Valhalleventuallyshutdownfor10weeksforcorrosioninspectionandrepairs.
duringwhichthreefurtherincidencesofMICand44anomaliesidentified.
Major Lessons
Behaviours of MIC were misunderstood
AreasofhighflowratewerepreviouslythoughtunlikelytoexperienceMIC,thisassumptionfailedtoidentifyinternalpipeworkscalingcanprovideenvironmentforMICactivity.
Inadequate application of hazard Recognition, risk awareness and control of work.
TheinitialinspectionroutinewasinappropriateanddirectlyledtoexposureoftheindividualandtheresultantFAI.
15specificimprovementopportunitiesidentifiedasaresultoftheincidentandplantinvestigations(7organisational,5workprocessand3performancemanagement).
-
INTERNALDISTRIBUTIONONLY 3
Microbial Induced CorrosionWhatisMIC?
MICisMicrobialInducedCorrosion.
MICofcarbonsteeltypicallymanifestsitselfaslocalisedcorrosionorpittingattackfollowingthedevelopmentofasurfacebiofilm.
Theanaerobicenvironmentsofoilandwatertransportpipeworkoftensupportthegrowthofbiofilms,whichalmostinvariablycontainsulphate-reducingbacteria(SRB),amajorcauseofMIC.
SRBcontainingbiofilms generateH2S.
H2SresultsinformationofIronsulphidewithinthebiofilm.
Ironsulphidesarecathodictobaresteelandcanhavetheeffectofgreatlyincreasingcorrosionatanodicsites.
WhydoesMICoccur?
MICcanoccurinallsystemsthatcontainwaterwithSRBs.
PredictionofcorrosionratesattributedtoMICisunreliable
uncertaintyoftheonsetoflocalizedcorrosion/pitting,whether itproceedsataconstantrate.
ParametersthatcaninfluenceMICincludepH,temperature,nutrition,velocityoffluids,presenceofdeposits.
MICismorelikelytooccuratlocationswithlowfluidvelocity suchasindeadlegs,underdeposits,scale.
AllmetalsaresusceptibletoMIC.Carbonsteelshavegenerallybeenfoundtobemostsusceptible.
MICmitigationreliesoneffectivebiocidedosingregimes.
-
INTERNALDISTRIBUTIONONLY 4
Reference - Valhall Timeline
1982
Valhallstart
production,
Incl.Jet
washing
separators
using sea-
water.By
mid-90s
using mainly
produced
water
1998
NewMetering
Skidinstalled.
Smallbore
pipeworknot
commissioned
inWorkmate
1999RBIAnalysisperformedMICinternalcorrosionnotsufficiently
identifiedasathreat.
2000
Inspection
scheme
constructed
which
identified
external
inspectionof
Liquids
metering
packageasa
whole
2004-2006
Chemical
cleaningof
fastloopto
aid
calibration
duetoscale
buildup
Ongoing
Biocide
treatmentof
Sulphate
Reducing
Bacteria
(SRB)on
Produced
Water(PW)
system
ongoingand
working
2007
SRBs in2nd
stageseparator
0-460/ml
Sept 2007
Cor.Mngt.Health
Check:Valhall
Prod.Water
SulfateReducing
Bacteria(SRB)
contaminationas
ahighriskand
recommendsa
microbialauditby
microbial
specialist
06.Mar.2009
Leakin1
pipefast
loop
HIPO
02.Apr.2009
Upstream
skimmedoil
tank
17.Apr.2009
Leakin6
prod.water
pipe
-
INTERNALDISTRIBUTIONONLY 5
Reference - Valhall TimelineEvents and response:
6thMarch2009Meteringfastloop (F&G ESD). LimitedawarenessofMIC,deemedlowprobability.LimitedspotcheckingbyX-rayoutsidethe
fastloop.NoSDjustifiedbyresidualcorrosionrisk.Noadditionalresources.
2ndApril2009T-337pressureincrease (NoESD).
StartupafteracompressorincidentincreasedflarebackpressurewhichburstaMICinthe
producedwatersystem.
15days(6+9)shutdownlookingforMICwithEddycurrentandX-rayw.crewof3.
17thApril20096 producedwaterpipe (NoESD).
RestartattemptfailedwhenaMICburstintheprod.watersystem.Hadbeeninspectedinvery
closevicinity.Increasingrealizationofthecriticalityofadequateinspectionrigour.
10daysshutdown,100%inspectionofprod.watersystembyEddy currentandX-ray,extended
riskbasedapproach.Increasedoffshoreresources.
27thApril2009Condensatereturntoprod.watersystem.(F&G ESD).
Pipeburstduringstartupattempt.Containedhighlyvolatilecondensate.
Realizedtechnologygap.ChangedtoSLOFECscanningsuccessfully.
30+teamoffshore.Taskforceonshore.True100%inspectionbeyondproducedwater.RIB
revision.
1stJune2009Successfulrestart.
10weeksofproductionlossandseriousHSEincidents.
-
INTERNALDISTRIBUTIONONLY 6
Valhall Corrosion Event (March 6th 2009)Summary of first event.
Aseep orsweatingleakobservedcomingfromaninsulated1 carbonsteelpipewaspreparedforinspectionfollowingremovaloftheinsulation.
Thepipewasonthecrudeexportmeteringskidandcontainedamixtureofcrudeoilandgasat25barpressure.
Onremovalofinsulation,theleakwasobservednottooriginatefromtheflangeasoriginallyexpected.
Aninspectorexaminingthepipeinitiallyusedabladetoscrapeoffpaintattheleaksite.
Duringalatervisit,theinspectortouchedtheleaksitewithhisfingerandwassprayedinthefacewithoilunderpressure.
Duringhydrocarbonrelease,theholeenlargedto10mmdiameter.
ValhallwenttofullEmergencyShutdownandmuster.
Hydrocarbon leak on metering skid First Aid Incident Emergency Plant Shutdown
-
INTERNALDISTRIBUTIONONLY 7
Inherent Design
Plant Layout
Control, Alarm &
Shutdown system
Inspection (RBI) and Corrosion Management practices failed to identify and mitigate the internal corrosion threat/risk that led to the failureRBI assessment not updated to reflect changes to operating and/or process conditions
Maintenance
& Inspection
Learning from
the Past
Actions from 2007/2008 Health Checks to improve Biocide treatment and to conduct Microbial survey not completed
Force Inspection procedures inconsistent with requirements of HSE Directive for visual inspection
Operations
Procedures
Inspection Engineer delegated inspection task to NDT Technician.
Effective
Supervision /
Leadership
Training &
Competency
Failure to follow CoWand RBI procedures
Work Control
Inadequate Hazard Recognition and Risk Awareness job treated as routine and Level 2 work permit.CoW - Failure to isolate energy source prior to workCoW - Failure to comply with requirements for Visual Inspection
Support to Next
of Kin & Injured
Relief and
Blowdown
system
Audit & Self
Regulation
No apparent MoC for chemical treatment of Fast Loop line.1 line not identified on risk-based inspection schedule
Management
of Change
Active & Passive
Fire Protection
Escape /
Access
Rescue &
Recovery
HAZARDHydrocarbon Inventory at
25bar in Fast Loop line
Investigation &
Lessons Learned
HAZARDREALISATION
Loss of containment
First Aid injury & HiPo
Hazard Barrier Diagram
Heirarchy of control Bias towards hardware/inherent safety & reducing the scope for human error multi barrier defence
Four Point Check not used.
-
INTERNALDISTRIBUTIONONLY 8
Valhall Corrosion Event (April 2nd 2009)Summary of second event.
AleakintheProducedWaterSystemfollowed
agascompressionupset.Areaisolated&
upstreamvesseldrained.
25mmholefoundindrainline.
Areasoflowflowanddead-legswereidentified
andinspected.6furtherMICincidents
observed.
Investigationinitiatedtoensureappropriate
analysisandresponsepriortorestart.
Managementverificationofprocessmitigations
andcorrosionmapping&repaireffort.
Targeted inspected discovers further incidence of MIC
-
INTERNALDISTRIBUTIONONLY 9
Valhall MIC Response The third event: Defining the Scope of Work
ProducedWateridentifiedasbeingthemain
hostofSulphate ReducingBacterias (SRBs)
Consideredpotentialcontaminationofother
systemsvsHCleakrisks.
ScopeagreedbyOps,ProcessTA,Corrosion
MgmtTA,Inspection&CMContractor.
ProducedWaterSystemwas100%inspected.
RiskBasedHotspot Execution Waterwetted
surfaceseg Lowspots,Sumps,Deadlegs etc.
Wasteinjectionondrillingplatform(DP).
Wellsystems,confinedtoslurrylines.
CrudeOilprocessingincludingthe
meteringsystem.
ClosedDrainsSystem.
Oil Return from PW Flash Drum to Oil Return tankOrientation of defect; 9 oclock position on vertical pipe
Unpredicted nature and location of corrosion required a new approach to
immediate reaction inspection.
-
INTERNALDISTRIBUTIONONLY 10
Leakin6producedwaterhighflowpipework
A8mmholewasdiscoveredduringpreparationforplantrestartfollowinginspectionprogramtriggeredtwogasdetectors&ESD.
Critical Factor1
MicrobialinducedCorrosion(MiC)mechanismintheproducedwatersystem
CriticalFactor2
Inspection(RBI)andCorrosionManagementpracticesfailedtoidentifythecorrosionriskinhighlevel,highflowpipework
Targeted inspected discovers further incidence of MIC in high flow pipework
ValhallCorrosionEvent.Summaryofforthevent.
-
INTERNALDISTRIBUTIONONLY 11
Valhall MIC project Inspection
Extensiveinspectioneffortrequiredtoexecute
identifiedscope 30+strongteam.
SLOFECtechnologyused
Priority1scopeIdentified44anomalies
23MICRelated
21Non-MIC-related
19spoolsreplaced,5temporarilyrepaired&20
scheduledforongoinginspectionfollowingstart-up
AssuranceprocessesfollowedbyNogo/Go
verificationreviews
Priority2inspectionscopeidentifiedforpoststartup
inspection.
No.10 T-337Flangecorrosion
Following fresh focussed risk assessment an intense and prioritised
inspection programme was initiated.
-
INTERNALDISTRIBUTIONONLY 12
Lessons Learnt
Direct cause
CrosscontaminationofoilproductionsystemwithSRBviatheproducedwater
system.
Inadequateawareness,inspectionandmitigationasanalysisdidnotidentifyoil
systemasatriskfromSRBcorrosion.
Insufficientchemicalinjection(suchasbiocideandcorrosioninhibitor)and
samplingandanalysistocontrolmicrobialactivity.
AsaresultMICoccurredwithinoilsystems.
Underlying causes
Improvementopportunitiesidentifiedwithin:
Organization (7subcategorieswithrecommendations)
Work Processes (5subcategorieswithrecommendations)
Performance Management (3subcategorieswithrecommendations)