Linac Marx Modulator Update Trevor Butler & Howie Pfeffer 2/25/2015.

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Linac Marx Modulator Update Trevor Butler & Howie Pfeffer 2/25/2015

Transcript of Linac Marx Modulator Update Trevor Butler & Howie Pfeffer 2/25/2015.

Linac Marx Modulator Update

Trevor Butler & Howie Pfeffer2/25/2015

Overall Status Update• Finished up Marx 9 Cell Design• Started to build 25 cell Marx

– Determined to build 28 cell Marx instead– Determined many components will need to be redesigned for many reasons

• Air Flow concerns• Corona concerns• Voltage Standoff concerns• Personal Safety (floating metal in design)

• Changed design to 28 cell version for initial testing, then followed by 54 cell version– Determined that control system original intended for both the original 25

and 54 cell designs would not be feasible in the short term.– Decided to build a larger version of the control system original designed for

the 9 cell Marx test for both 28 and 54 cell design

9 Cell Marx Final Design• Finalized design of 9 cell Marx modulator• Upgraded the following components from the original 9

cell prototype– Replaced one snubber capacitor with two– Built gate clamp circuit– Finalized b-dot coil design– New low inductance stripline

• Ran all 9 cells in both with and without PWM– Achieved much greater than 20kV/us slew rate with all nine

cells fired simultaneously (15 kV/us spec)– Achieved the +/- 25 ripple specification. Have since

determined the ripple specification should have been listed as a voltage over frequency since the frequency response of the tube / accelerating cavity will filter this response ripple at higher frequencies.

• Results– Determined importance of cell timing accuracy to enable

low ripple operation. This will require accurately measuring each cell delay time (at full load current) to compensate.

– Was able to reduced short circuit current to 1700 Amps for the 9 cells using the gate clamping circuit

600V CPS, 2.5V refCh.1 Stripline output voltageCh.2 Filter output voltageCh.3 Stripline output current (100A/V) (includes filter current)

900V CPS, 2.5V peak ref.Ch.1 Stripline output voltageCh.2 Load Current (100A/V)Ch.3 Cell 1 gate clamp circuit active

900V CPS, 2.5V peak ref.Ch.1 Stripline output voltageCh.2 Load Current (100A/V)Ch.3 Cell 1 gate clamp circuit active

900V CPS, 2.5V peak ref.Ch.1 Stripline output voltageCh.2 Load Current (100A/V)Ch.3 Cell 1 gate clamp circuit active

550V CPS, 2.5V ref. Spark gap triggeredCh.1 Stripline output voltageCh.2 Common voltageCh.3 Stripline output current (100A/V)Ch.4 Cell 1 Gate clamp active

600V CPS, 2.5V refCh.1 Stripline output voltageCh.2 Filter output voltageCh.3 Stripline output current (100A/V) (includes filter current)

Filtered Voltage

Stripline Voltage

Stripline Current

Filtered Voltage

Stripline Voltage

Stripline CurrentCommon Voltage

Cell 1 Gate Clamp

Stripline Current

Load Current

Stripline Voltage

Load Current

Stripline Voltage

Load Current

Stripline Voltage

Stripline Voltage

25/54 Cell Original Design• Originally planned on developing control system for the 25/54 using and

FPGA controlling the CPLD’s, which in turn, fire and charge the IGBT’s• After investigating the technical requirements, decided that a SoC (system

on a chip) using the Altera Cyclone V chip would be the only option– This option would require a long time (> 1 year) to design, program, test, and

debug.– It was desired to be able to do high voltage testing on both the 25 and 54 cell

versions, which can’t wait for this development time– Using a modified version of the original 9 cell control system would work for

larger versions• Would not have the timing accuracy of the SoC FPGA design• Would require signals to be converted from A/D and back using D/A converters to do the

controlling• Would not be able to real-time feedback, but may be able to do some analog feedback

• Decided to switch over to a 28/54 cell design

28/54 Cell Modified Design• Determined that building the 54 cell version on top of the 25 cell version would not be feasible

– Air Flow concerns• focus each cell air through cooling fins and not around

– Corona concerns• Round all corners of existing heat sinks to prevent corona

– Voltage Standoff concerns• Modify cabinet to have greater than 6” between both walls and any Marx cells at high voltage• Will be able to reuse the existing enclosure for the lower voltage version

– Personal Safety (floating metal in design• Will replace all metal shelving pieces, screws, and support structure with plastics to reduce corona and prevent

ungrounded metal from floating up to high voltage and creating a potential shock hazard

• Decided to use the existing cabinet and build a 28 cell version (4 rows with 7 cells per row)– Will test with both PWM and non-PWM cell simultaneously, similar to the final design– Will reuse the existing control cards that have been developed– Will require new CPLD to be installed to handle more logic elements than the present 1500 limitation– Will require backplane to be designed for both 28 and 54 cell versions– Will require building new main control card to interface between all cell and future FPGA

• This 28 cell version may be able to operate on LRF1– Depends on success of design to hold off voltage, prevent corona, and cool efficiently– Depends on gain of tube in LRF1

28 Cell Version

Changes from Existing Design• 7 cells wide instead of

9• Only 4 rows tall

instead of 6• More space on front

of cells• Lexan on backplane

for isolation• Self supported

structure (Does not relay on screws for strength)

• Two fans for better cooling

Dual Development of 28 / 54 Cell Design

• Testing the Marx topology at a lower voltage (28 cells * 900 Volts ~ 25 kV), a the lessons learned could would be applied to the 54 cell version

• The 54 cell version will be built into a newly designed cabinet– Larger Voltage Standoff between walls and cell– New Lexan based shelves– Mounting brackets with no metal screws– Increased airflow to each cell

• This cabinet will be designed after corona testing of the cells in 28 cell version• By building both the 28 cell and 54 cell simultaneously, then as the 28 cell is being

tested, the 54 cell construction can start.• The control cards developed for the original 54 cell version will still work with the

modified 28 and new 54 cell modulators.– Many of the control cards are complete– A new Preliminary FPGA Control Interface Card will be built to interface with both the 28 and 54 cell

designs, and be upgradable (by adding a additional FPGA card) to the final control system– This design will allow for the cards developed to be used in final system without any additional circuit

board design

Control Card Status

Task NameDrawing Number Schematic Layout Parts Assembled

Schematic Layout 28/54 28/54 28 54 28 54IGBT Gate Driver 0231-EC-281930 0231-BD-281931 100% 100% 100% 100% 50% 0%18 Cell Driver 0231-EC-281994 0231-BD-281995 100% 100% 100% 100% 100% 0%Status Input 0231-EC-281996 0231-BD-281997 100% 100% 100% 100% 100% 50%Status Sum 0231-ED-281998 0231-BD-281999 100% 100% 100% 100% 50% 10%Charge control 0231-EE-498000 0231-BD-498001 100% 100% 100% 100% 50% 50%Control Backplane 0231-EE-498004 0231-BD-498005 75% 0% 0% 0% 0% 0%Preliminary FPGA Control Interface 0231-EE-498006 0231-BD-498007 75% 0% 0% 0% 0% 0%Analog Compartor Interlock 0231-ED-498020 0231-BD-498021 100% 80% 0% 0% 0% 0%Charge Diode and Gate Clamp Circuit 0231-EB-498030 0231-BD-498031 100% 100% 100% 100% 100% 0%PLC Level Interface TBD TBD 0% 0% 0% 0% 0% 0%Inerface to Analog Compartor TBD TBD 0% 0% 0% 0% 0% 0%Interface with FPGA TBD TBD 0% 0% 0% 0% 0% 0%

• Many Cards have been designed, layout created, parts order, and built• Presently Finishing up the drawings for the two most complex cards, the

FPGA Control Interface Card (with CPLD) and the Backplane• Plan to have the drawings into EE Support drafting within two weeks to

start layout of boards (labor is promised)• 3 interface cards (only a few components per card) need to be designed

and layout create, but since they are simple, they should only take an addition 2-3 weeks to design, layout, and order parts

Corona Testing• Tested Heatsink without any polishing or

rounding of corners and it failed the test• Tested Heatsink with rounded edges and

passed test• Using multiple jumpers, create 3

complete cell version to test at high voltage.– Passed at 36 kVrms (50 kVpeak)

Future work• Test the cells at full loading conditions

– 350 amps, at 15 Hz, with full PWM switching• Test the Capacitor Charging Supply from Lumina power to determine if it will work for

these design– Could be used for either the 9 cell or 28 cell versions– More would need to be purchased for 54 cell design

• Design Charging Supply Controller Interface Chassis• Design PLC and touch panel interface for operation into existing RF systems• Build charging supply control interface for testing into development area and in

operational stations• Order and build additional 35 cells to complete 54 cell design in parallel with 28 cell

design• Finish Control Card Design and Layout• Build remaining cells and control cards (one item, but a lot of work involved in this

line)• Corona testing of the 28 cell version• Successfully regulate cavity gradient on operating station

– Will likely require many rounds of studies to check versus ideas– It may require more than feed-forward and learning to operate

One option for testing Marx• Considered Many Options for testing• Likely will place in the hallway• Minimizes cabling length• Only 66” hallway clearance (need 64”)• Fire Safety approved this location• Will be difficult to access when blocking

main door• May need to consider converting strip

line output to coaxial output

Different cavity gradient regulation schemesDirect Gradient Analog Feedback• Presently used to regulate our vacuum tube modulators• Op-Amp feedback loop with adjustable proportional gain• Advantages

– Simple in design, and robust in operation– Direct feedback cancels out any pulse to pulse variations as it noticed significantly on LRF1

• Disadvantages– Lack of real time tuning and optimization via ACNET.– Interfacing with existing LLRF Learning Algorithm can be problematic and require frequency

tuning

Feed-Forward Operation (often confused with Learning)• Uses a system model of the load (the 7835 triode, accelerating cavity, and beam

intensity) to predict the required amount of voltage to get the desired gradient level• Advantages

– Can act as a first guess before implement any learning or feedback• Disadvantages

– Almost impossible to get perfect model.– Even if you could, it could drift over time, requiring constant tuning to stabilize gradients

Different cavity gradient regulation schemesLearning Operation• Learns the waveform error from pulse to pulse, placing correction on next pulse• If the Learning Operation is used on top of the Feed-Forward loop, then the system

would have less error to correct• Advantages

– Able to learn out slow process (Aging of tube, drifting of cavity frequency, • Disadvantages

– Unable to regulate voltage within the pulse.

Real-Time Feedback• Realtime operating system, like the SoC FGPA topology• Error between the cavity fields is calculated in realtime and the error is sent to the

PWM for correction within the pulse• Advantages

– Able to Control cavity fields within the pulse, accounting for pulse to pulse variations• Disadvantages

– Complex to design– Long development time

Testing on LRF2• Tested Feed-forward loop on LRF2 during last downtime.• Was able to adjust parameters for the gain of the tube and the time constant

of the accelerating cavity (~30 us)• Was able to accurately predict gradient within about 25% over the entire

range• Next step will be to test the learning algorithm, with appropriate gain

clamping, and waveform advance, to see if flat gradient response is possible• If successful, the following test will be to compensate for beam loading and

check learning response• It may turn on that beam is not stable without real-time or analog feedback,

which will be visited if this is an issue– LRF2 is not a sensitive to pulse to pulse variations as LRF1, so it may be a good place

for testing• The goal is a final installation where the interlock system could be fully

integrated into the modulator controls, resulting in the ability to run the system over multiple days, checking the long term stability

Voltage Command to Modulator - Red

Gradient Reference (Desired) - Green

Measured Gradient Waveform - Blue

Project Timeline• Finish control card development and have final boards laid, ordered, and

built (2 months)• Finish assembly of Marx cells with the modifications learned from corona

testing (3 months)• Finish up design of 28 cell support structure and fabricate support

structure and backplane (3 months)• Continue work on testing learning algorithms on actual RF system until

system can run without user interaction• Test 28 cell version into dummy load (3-4 months)• Build 54 cell version using what is learned in the 28 cell building and

testing (6 months)• Test 54 cell version into dummy load, followed by testing in actual RF

system, using the code developed by testing on present tube modulator (6-7 months)