Flixborough+Disaster

35
Flixborough disaster By: Gautam Iyer Audumbar Jadhav Aniruddh Kamat Sushil Kansurkar Sukrut Khambete

Transcript of Flixborough+Disaster

Page 1: Flixborough+Disaster

Flixborough disaster

By:

Gautam Iyer

Audumbar Jadhav

Aniruddh Kamat

Sushil Kansurkar

Sukrut Khambete

Page 2: Flixborough+Disaster

Introduction• Largest peacetime explosion ever to occur in the UK

• Date: Saturday, 1 June 1974

• Location: Flixborough chemical plant owned by Nypro (UK) Ltd

• Deaths of 28 workers on the site

• Widespread damage to property within a 6 mile radius around the plant

Page 3: Flixborough+Disaster

• 1967: 20,000 TPA caprolactam plant built by DSM at the Flixborough site using process involving the hydrogenation of phenol

• 1972: 70,000 TPA ; new process used

• New process based on oxidation of cyclohexane

• Posed much greater hazard than phenol process

C6H5OH + 2 H2 → (CH2)5CO

Page 4: Flixborough+Disaster

Description of the cyclohexane process

• Process operates by injecting compressed air into liquid cyclohexane at a working pressure of about 9 bar and temperature of 155°C

• Cyclohexanone and cyclohexanol produced• Conversion is low and it is necessary to recirculate

the cyclohexane continuously through a train of six large SS-lined reactors

Page 5: Flixborough+Disaster

C6H12 + O2 → (CH2)5CO + H2O Cyclohexane Cyclohexanone

Caprolactum Nylon6

Page 6: Flixborough+Disaster

Simplified flow diagram of cyclohexane oxidation plant before March 1974 (Whittingham, 2005)

Page 7: Flixborough+Disaster

Events leading to the accident

1. Miners overtime ban of Nov, 1973

• Resulted in the government passing legislation to restrict the use of electricity by industry to 3 days a week

• Was not possible to operate the process on this basis

• Was decided to utilize existing emergency power generation on-site

Page 8: Flixborough+Disaster

• Major electricity user: 6 stirrers in the cyclohexane reactors

• Primary purpose: disperse compressed air that was injected into each reactor via a sparger

• Also ensured that droplets of water formed within the reactor system were dispersed into the cyclohexane

Page 9: Flixborough+Disaster

2. The No. 5 reactor problem

• Jan, 1974:normal electricity supply resumed

• Was found that the drive mechanism for the stirrer in the No. 4 reactor had been subject to severe mechanical damage

• No reason was found for this. It was therefore decided to continue to operate the plant with the No. 4 reactor stirrer shutdown.

Page 10: Flixborough+Disaster

• Cyclohexane reactors were MS vessels fitted with an inner SS lining to resist corrosion

• March,1974: Cyclohexane found leaking from 6 feet long vertical crack in the MS shell of the No. 5 reactor

• Due to technical problems experienced earlier and the effects of the 3-day week, the plant owners were keen to make up lost production

• Therefore decided to remove No. 5 reactor for inspection and continue operation with the remaining five reactors

Page 11: Flixborough+Disaster

3. Installation of 20” bypass pipe

• This pipe connected together the existing 28 inch bellows on the outlet of reactor No. 4 and the inlet of reactor No. 6

• Dog-leg shape of pipe

• Company did not have qualified mechanical engineer on site to oversee design and construction

• No hydraulic pressure testing of pipe carried out,

except for a leakage test using compressed air.

Page 12: Flixborough+Disaster

Simplified flow diagram of cyclohexane oxidation plant after March 1974 (Whittingham, 2005)

Page 13: Flixborough+Disaster

4. Resumption of production

• Plant restarted and operated normally, with occasional stoppages, up until the afternoon of Saturday, 1 June 1974

• Previous day: plant had been shut down for minor repairs

• Early hours of 1 June: plant in process of being restarted

• Start-up involved charging system with liquid cyclohexane to normal level and then recirculating this liquid through a heat exchanger to raise the temperature.

Page 14: Flixborough+Disaster

• The pressure in the system was maintained with nitrogen at about 4 bar until the heating process began to raise the pressure due to evaporation of cyclohexane.

• The pressure was then allowed to rise to about 8 or 9 bar, venting off nitrogen to relieve any excess pressure. The temperature in the reactors by then was about 150°C.

Page 15: Flixborough+Disaster

• On 1 June this procedure was followed except it was noted by the morning shift that by 06.00 hours the pressure had reached 8.5 bar even though the temperature in the No. 1 reactor had only reached 110°C

• Was not realized at the time that this discrepancy might have indicated the presence of water in the system

• The start-up continued until, at about 16.50 hours, a shift chemist working in the laboratory close to the reactors heard the sound of escaping gas and saw a haze typically associated with a hydrocarbon vapour cloud.

Page 16: Flixborough+Disaster

The accident

• 16.53 hours on 1 June 1974: massive aerial explosion occurred with a force later estimated to be about 15 to 45 tonnes of TNT equivalent

• Explosion heard up to 30 miles away and damage sustained to property over a radius of about 6 miles around the plant

• 28 plant workers killed with no survivors from the control room

• All records and charts for the start-up destroyed• Following the explosion, 20 inch bypass assembly was

found in a ruptured condition

Page 17: Flixborough+Disaster

The Public Inquiry • Following the disaster, public inquiry

conducted under the chairmanship of Roger Parker QC

• To establish the causes and circumstances of the disaster

• To identify lessons to be learnt from the disaster

Page 18: Flixborough+Disaster

Conclusions of the inquiry• The immediate cause of the main explosion

was the rupture of the 20 inch bypass assembly between the No. 4 and No. 6 reactor

• Two main theories to explain

Page 19: Flixborough+Disaster

The 20 inch pipe theory• The 20 inch bypass assembly failed due to its

unsatisfactory design features• However, the assembly had survived 2 months of

normal operation.• A number of independent pressure tests were

commissioned to determine unusual conditions

Page 20: Flixborough+Disaster

• The normal working pressure = 8 bar • practice during start-up to allow the pressure to

build up to about 9 bar. • The safety valves for the system, were set to

discharge at a pressure of 11 bar• At pressure above 11 bar, squirming motion

which distorted the bellows.

Page 21: Flixborough+Disaster

• Even when the assembly squirmed, no rupture until pressure crossed 14.5 bar, a pressure not achievable in reactors.

• Inquiry concluded that a rupture of the 20 inch bypass due to pressure, temperature conditions

• Report conceded ambiguity in the hypothesis• Simulation tests could not replicate failure at

similar conditions

Page 22: Flixborough+Disaster

The 8 inch hypothesis• Alternative theory• 50 inch split in an 8 inch line connected to

separator below bypass• this failure led to a smaller explosion causing

failure of the main 20 inch bypass• Zinc embrittlement had caused the split• Small lagging fire at a leaking flange causing zinc

to drip onto the 8 inch pipe• Brittle failure – Vapour release – Explosion – 20

inch failure

Page 23: Flixborough+Disaster

• Inquiry Report had devoted discussion of this two-stage theory

• Finally dismissed as being too improbable• No other theories considered by them to explain

failure of 20 inch bypass pipe

Page 24: Flixborough+Disaster

The water theory• Another alternative theory • Not considered by the Inquiry• Much of scientific work after Inquiry closed• Examined the effects of not operating the No. 4

reactor stirrer during the start-up at a time when water may be present

• More probable explanation

Page 25: Flixborough+Disaster

• Cyclohexane and water are normally immiscible • Azeotrope forms due to the limited solubility of

water in cyclohexane. • This azeotrope has lower boiling point than

either water or cyclohexane• Unstable interfacial layer may form• Under certain conditions can boil and erupt

violently ejecting cyclohexane and superheated water from the reactor.

Page 26: Flixborough+Disaster

• Normally impossible for water layer to form due to dispersion of water by air distribution

• During start-up, the air to the reactors shut off• If stirrers running during start-up, no water layer• If stirrer stops, a layer of water could form, together

with the unstable azeotrope.

Page 27: Flixborough+Disaster

• As temperature of reactor increases, boiling point of azeotrope is reached

• Possibility of a sudden violent eruption from the reactor and ejection of slugs of liquid reactant

• Slugs exert high mechanical forces on the bypass assembly, loosely supported by scaffolding

• Causes bypass assembly to fail without the high static pressure in the reactors

Page 28: Flixborough+Disaster

Alternative event sequence• Most credible explanation• Explains failure of 20 inch bypass • Also provides an explanation for the whole

sequence of events

Page 29: Flixborough+Disaster

• Unexplained failure of drive mechanism of No. 4 reactor

• Crack developing in the lining and shell of No. 5 reactor

• Failure of the 20 inch bypass assembly.• Any/all failures caused by violent eruption of

reactor contents due to presence of water• Committee failed to see common thread

Page 30: Flixborough+Disaster

• Drive mechanism failure for No. 4 reactor unexplained

• Thought to be irrelevant• Crack in the shell of the No. 5 reactor due to

stress corrosion• Proposed by plant owners but not credible

Page 31: Flixborough+Disaster

• The failure of the bypass concluded by Inquiry due to reactors being over-pressurized

• Implies human error, not verifiable• Greatest failing of Inquiry was not taking

account of all the events 6 months prior to the disaster

• Issue of non-operation of the reactor stirrers ignored

Page 32: Flixborough+Disaster

Conclusions• Human error analysis

Table gives causes against the different types of error that occurred.

• Direct causeFailure of the 20 inch bypass pipe led to huge release of inflammable cyclohexane vapour which ignited

• Root causesA badly designed 20 inch bypass pipe installed rather than finding reasons for the crack in the No. 5 reactor Why bypass failed ?

Page 33: Flixborough+Disaster

(Whittingham, 2005)

Page 34: Flixborough+Disaster

Safety considerations• Learnings• Low inventory especially of flashing fluids • Before modifying process, carry out systematic

search for possible cause of problem• Carry out HAZOP analysis• Construct modifications to same standard as

original plant• Use blast-resistant control rooms and buildings

Page 35: Flixborough+Disaster

THANK YOU