Failure Analysis Results and Corrective Actions Implemented for … · 2016-06-09 · 1...

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1 International Conference on Environmental Systems Failure Analysis Results and Corrective Actions Implemented for the Extravehicular Mobility Unit 3011 Water in the Helmet Mishap John Steele, 1 Carol Metselaar, 2 Barbara Peyton, 3 Tony Rector, 4 and Robert Rossato 5 UTC Aerospace Systems, Windsor Locks, CT 06096-1010 Brian Macias 6 and Dana Weigel 7 NASA.Johnson Space Center, Houston, Texas, 77058 Don Holder 8 NASA/Marshall Space Flight Center, Huntsville, Alabama, 35812 Water entered the Extravehicular Mobility Unit (EMU) helmet during extravehicular activity (EVA) #23 aboard the International Space Station on July 16, 2013, resulting in the termination of the EVA approximately 1 hour after it began. It was estimated that 1.5 liters of water had migrated up the ventilation loop into the helmet, adversely impacting the astronauts hearing, vision, and verbal communication. Subsequent on-board testing and ground-based test, tear-down, and evaluation of the affected EMU hardware components determined that the proximate cause of the mishap was blockage of all water separator drum holes with a mixture of silica and silicates. The blockages caused a failure of the water separator degassing function, which resulted in EMU cooling water spilling into the ventilation loop, migrating around the circulating fan, and ultimately pushing into the helmet. The root cause of the failure was determined to be ground-processing shortcomings of the Airlock Cooling Loop Recovery (ALCLR) Ion Filter Beds, which led to various levels of contaminants being introduced into the filters before they left the ground. Those contaminants were thereafter introduced into the EMU hardware on-orbit during ALCLR scrubbing operations. This paper summarizes the failure analysis results along with identified process, hardware, and operational corrective actions that were implemented as a result of findings from this investigation. 1 Engineering Fellow, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2- W66, Windsor Locks, CT 06096-1010 2 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor Locks, CT 06096-1010 3 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor Locks, CT 06096-1010 4 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor Locks, CT 06096-1010 5 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor Locks, CT 06096-1010 6 EMU Life Support System Manager, Johnson Space Center, National Aeronautics and Space Administration, Houston, TX 77058 7 ISS Vehicle Manager, Johnson Space Center, National Aeronautics and Space Administration, Houston, TX 77058 8 Chief Engineer, Flight Programs and Partnerships Office, Marshall Space Flight Center, National Aeronautics and Space Administration, EE04 MSFC, AL 35812 https://ntrs.nasa.gov/search.jsp?R=20150003027 2020-04-05T05:24:36+00:00Z

Transcript of Failure Analysis Results and Corrective Actions Implemented for … · 2016-06-09 · 1...

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International Conference on Environmental Systems

Failure Analysis Results and Corrective Actions

Implemented for the Extravehicular Mobility Unit 3011

Water in the Helmet Mishap

John Steele,1 Carol Metselaar,

2 Barbara Peyton,

3 Tony Rector,

4 and Robert Rossato

5

UTC Aerospace Systems, Windsor Locks, CT 06096-1010

Brian Macias6 and Dana Weigel

7

NASA.Johnson Space Center, Houston, Texas, 77058

Don Holder8

NASA/Marshall Space Flight Center, Huntsville, Alabama, 35812

Water entered the Extravehicular Mobility Unit (EMU) helmet during extravehicular

activity (EVA) #23 aboard the International Space Station on July 16, 2013, resulting in the

termination of the EVA approximately 1 hour after it began. It was estimated that 1.5 liters

of water had migrated up the ventilation loop into the helmet, adversely impacting the

astronaut’s hearing, vision, and verbal communication. Subsequent on-board testing and

ground-based test, tear-down, and evaluation of the affected EMU hardware components

determined that the proximate cause of the mishap was blockage of all water separator

drum holes with a mixture of silica and silicates. The blockages caused a failure of the water

separator degassing function, which resulted in EMU cooling water spilling into the

ventilation loop, migrating around the circulating fan, and ultimately pushing into the

helmet. The root cause of the failure was determined to be ground-processing shortcomings

of the Airlock Cooling Loop Recovery (ALCLR) Ion Filter Beds, which led to various levels

of contaminants being introduced into the filters before they left the ground. Those

contaminants were thereafter introduced into the EMU hardware on-orbit during ALCLR

scrubbing operations. This paper summarizes the failure analysis results along with

identified process, hardware, and operational corrective actions that were implemented as a

result of findings from this investigation.

1 Engineering Fellow, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2- W66,

Windsor Locks, CT 06096-1010 2 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor

Locks, CT 06096-1010 3 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor

Locks, CT 06096-1010 4 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor

Locks, CT 06096-1010 5 Staff Engineer, Hamilton Sundstrand Space Systems International, 1 Hamilton Road, MS 1A-2-W66, Windsor

Locks, CT 06096-1010 6 EMU Life Support System Manager, Johnson Space Center, National Aeronautics and Space Administration,

Houston, TX 77058 7 ISS Vehicle Manager, Johnson Space Center, National Aeronautics and Space Administration,

Houston, TX 77058 8 Chief Engineer, Flight Programs and Partnerships Office, Marshall Space Flight Center, National Aeronautics and

Space Administration, EE04 MSFC, AL 35812

https://ntrs.nasa.gov/search.jsp?R=20150003027 2020-04-05T05:24:36+00:00Z

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Nomenclature ACTEX = Activated Carbon/Ion Exchange ALCLR = Airlock Cooling Loop Recovery

CAP = Corrective Action Plan

DI = deionized

ECLSS = Environmental Control Life Support System

EMU = Extravehicular Mobility Unit

EVA = extravehicular activity

Fe = iron

FPS = fan/pump/separator

ISS = International Space Station

JSC = Johnson Space Center

LCVG = Liquid Cooling and Ventilation Garment

mL = milliliter

Ni = nickel

pH = hydrogen ion concentration

ppm = parts per million

SEMU = Short Extravehicular Mobility Unit Si = silicon

TOC = Total Organic Carbon

Zn = zinc

I. Introduction

ater entered Astronaut Luca Parmitano’s helmet during U.S. extravehicular activity (EVA) 23 on July 16,

2013, on-board the International Space Station (ISS), resulting in early termination of the EVA at a phase

elapsed time of 1:05. Water entered the helmet at the ventilation loop inlet “T-2” port, which is located behind the

crew member’s head at the base of the helmet. The specific location where the water was entering and the source of

the water was unknown during the EVA. The water began to accumulate on the back of Luca’s head and he soon

reported that the water was increasing, Mission Control Center–Houston directed the crew to terminate the EVA.

The water migrated to Luca’s face during translation back to the airlock, thereby covering his eyes, ears, and nose.

Luca’s vision and communications were degraded as a result of the water shift, requiring Luca to use his safety

tether as a guide to navigate back to the Airlock. The crew successfully returned to the Airlock and performed an

expedited repress and suit doffing. Luca communicated with EV1, Chris Cassidy, during repress using only hand

squeezes. Following EVA 23, the crew reported approximately 1.5 liters of water in Luca’s helmet—a fact that was

later confirmed when the Extravehicular Mobility Unit (EMU) feed-water recharge was performed as part of the

standard post EVA suit servicing.1

This paper summarizes the investigative findings that lead to the proximate and root cause, provides associated

corrective actions, and outlines recommended forward work related to the EVA 23 water in the helmet mishap. The

mishap investigation, including the development of proximate and root cause for the failure and implementation of

corrective actions, culminated in returning the ISS Program to nominal EVA capability on August 11, 2013.

II. On-orbit Hardware Evaluation

On-orbit troubleshooting of the failed EMU began the day following the EVA and included eliminating the

Liquid Cooling and Ventilation Garment (LCVG), water tank structure, and hard upper torso tubing as leak sources.

The failure was easily repeated on-orbit in the intravehicular activity environment by pressurizing the fully-suited

EMU and “priming” the Transport (e.g., Cooling) Water Loop to initiate cooling loop water flow through the water

separator. During this troubleshooting, water entered the unmanned helmet within about 3 minutes of priming. A

fault tree was developed and more complex troubleshooting, including removal and replacement of various Life

Support System components, was conducted through late October 2013. This troubleshooting eventually led to the

removal and replacement of EMU 3011’s fan/pump/separator (FPS) (Item 123 S/N 006) on October 24, 2013, which

resolved the water crossover anomaly. The FPS became a focal point of the investigation going forward and was

returned to the ground for post-flight analysis. The S/N 006 FPS was removed from the Short Extravehicular

Mobility Unit (SEMU) 3011 on orbit and returned to ground for test, teardown, and evaluation on 11/11/2013. This

W

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approach was simple: move from least-invasive to most-invasive actions during the teardown of FPS 006 to preserve

as much evidence as possible for evaluation.1

The EMU fan, pump, and water separator are coupled together through a common shaft and magnetic coupling

to form what is called the FPS (Figure 1). The fan circulates oxygen over the crew member’s head and throughout

the suit, and pulls waste gases (e.g., carbon dioxide) and oxygen through a carbon-dioxide-removal cartridge. The

pump, which is isolated from the ventilation loop via a magnetic coupling, circulates coolant loop water through the

EMU’s sublimator heat exchanger and throughout the LCVG. Humidity from the crew member’s' exhalation and

sweat is also condensed in the sublimator and sent to the water separator where the water is removed and returned to

the water loops. In addition to this condensate, water from the EMU coolant loop is continuously flowing through

the water separator to facilitate constant coolant loop circulation for degassing purposes.2

Figure 1. Cutaway view of the EMU FPS.

III. Ground Hardware Evaluation

A receiving inspection was performed when the S/N 006 FPS assembly arrived at the United Technologies

Aerospace Systems (UTAS) facility and the Item-123 FPS assembly was separated from the Item-127/128 Pump

Inlet Filter. Both were repackaged and shipped to Goddard Space Flight Center for X-ray CT scans. The scans were

primarily looking for mechanical assembly or component failure areas or gross contamination that may have caused

the failure of the FPS to function properly. The result of the nondestructive evaluation showed no mechanical issues

such as cracks or loss of a weld plug in the pitot that would result in the failure mechanism seen on orbit. However,

both the X-ray CT scan and N-ray scan showed the presence of contamination within the drum of the separator.

Figure 2 shows the contamination indications in the drum from the CT scans. The contamination appeared to be in

and around the eight drum holes that feed the drum trough.3

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Figure 3: X-ray CT scan of FPS S/N 006 separator drum.

After the CT scans were complete, the hardware was sent back to UTAS for disassembly. All parts were

photographed and dimensionally inspected during disassembly. Once the FPS pitot and drum were removed, they

were packaged and shipped to McClellan Nuclear Research Center for N-ray scans. The N-ray scan was to

determine whether internal passageways within the pitot and drum were blocked or contained contamination.

Testing of the water separator was added to the plan, based on findings from the inspections and nondestructive

evaluations.

Upon return of the FPS, visual inspections identified contamination in all eight water separator drum inlet feed

holes (Figure 3) and along the walls leading to the feed holes. Analysis showed the material to be primarily loosely

bound silica, with zinc acetate, aluminum silicate, and aluminum oxide present as well. These constituents are all

native to the EMU/Airlock system, but the quantity and location were out of family. The majority of the material

was silica based.3

In operation of the EMU Transport Water Loop, small particles are filtered with a 20 micrometer filter prior to

entering the water separator, which indicates the contaminant material either entered as very small particles that

agglomerated in the separator or entered in solution followed by localized precipitation. Testing of EMU 3011’s

returned FPS (S/N 006) both with and without the drum-hole contamination confirmed that the blocked drum holes

were the cause of the water in the helmet mishap.

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Figure 3. Blocked water separator drum holes.

After the silica-laden contamination was found in the FPS, a causal tree was developed to determine the source

of the silica and the potential mechanisms for facilitating the precipitation and agglomeration in the water separator.1

All hardware and water sources that interface with the EMU were investigated. This included EMU 3011’s interface

with the Space Shuttle coolant loop prior to launch, Space Shuttle water from the Payload Water Reservoirs, which

are used to fill the EMUs on the ISS, the Airlock Cooling Loop Recovery (ALCLR) Ion Beds, and the Airlock Heat

Exchanger. Other potential contributors to the anomaly were the ISS environment (pH, temperatures), the EMU

Sublimator, and EMU hardware contamination (Braycote®

, system corrosion products, etc.). These investigations

led to the ALCLR Ion Beds as potentially being the primary contributors to the high levels of silica-laded

contaminants found in the FPS S/N 006 Water Separator drum holes.1

IV. Airlock Cooling Loop Recovery Ion Bed Evaluations

A. Airlock Cooling Loop Recovery Description

The ALCLR water processing kit was developed as a corrective action to EMU coolant loop flow disruptions

experienced on the ISS in May 2004 and thereafter. The components in the kit are designed to remove the

contaminants that caused prior flow disruptions. ALCLR water processing kits have been used since 2004 as

standard operating procedure. Periodic analysis of EMU coolant loop water and hardware examinations were used

as a means to determine adequate functionality and optimized processing cycles as well as ALCLR component shelf

life.

The ALCLR water processing kit (Figure 4) was devised to scrub and remediate the various chemical and

biological contaminants and by-products that were found to have fouled the magnetically coupled pump in the EMU

Transport Water Loop FPS. The heart of the kit is the EMU Ion Filter, which is a 50:50 by volume packed bed of

mixed anion/cation exchange resin and activated carbon. This component is periodically installed inline to the EMU

and Airlock Heat Exchanger coolant loop and serves the purpose of removing inorganic and organic constituents

such as nickel and iron corrosion products and organic acids with the ion exchange resin. Furthermore, uncharged

organic contaminants are removed with the activated carbon.4

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Figure 4. ALCLR processing kit components.

In service, a 3-micrometer filter is placed downstream of the EMU Ion Filter to capture fines from the packed

bed prior to return of the polished water to the EMU Transport Loop. After scrubbing with the EMU Ion Filter, the

EMU Biocide Filter is installed to add residual iodine biocide for microbial control. The EMU Biocide Filter is a

packed bed of ion exchange resin impregnated.4

B. Airlock Cooling Loop Recovery Ion Bed Link to Short Extravehicular Mobility Unit 3011 Mishap In December 2013, five ALCLR Ion Beds and four post-Ion Bed 3-micrometer filters were returned from on-

orbit for a complete chemical analysis. The focus of this investigation was on the proper functionality of this

hardware since it was designed to remove the types of contaminants found in the SEMU 3011 S/N 006 FPS Water

Separator drum holes from the EMU Transport Water Loop.

Each of the five ALCLR Ion Beds underwent an initial free water drain, and that water underwent a complete

chemical analysis. The ion exchange resin from each was then removed, and different aliquots underwent separate

acid (0.5 N nitric acid) and base (0.5 N sodium hydroxide) extractions to remove the adsorbed anions and cations,

respectively, from the resins. Separate ion exchange resin samples from each Ion Bed then underwent capacity

testing with a variant of ASTM Method D 3375-95a (Standard Test Method for Column Capacity of Particulate

Mixed Bed Ion Exchange Materials) to determine the remaining ion exchange capacity for each resin.5

The free water (~60 mL) drained from ALCLR Ion Bed (S/N 1003) was found to have a relatively high

dissolved silicon level (41 ppm) when compared to the others (< 1 ppm dissolved silicon), thus indicating that the

ion exchange resin was saturated and unable to retain silicon in its common dissolved form, as ionic silicic acid.

Furthermore, the acid/base extracts from the ALCLR Ion Bed S/N 1003 ion exchange resin was found to have

relatively high chloride, sulfate, potassium, and silicon levels when compared to the data generated from the other

four beds. Finally, when the ion exchange resin capacity test was done on the resin from ALCLR Ion Bed S/N 1003,

it was found to have no remaining ion exchange capacity, and silicon immediately discharged from the ion exchange

resin when capacity challenge sodium chloride was added (Figure 5). This was a stark difference from the other four

Ion Beds, which all showed significant remaining ion exchange resin capacity (Figure 6).5

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Similar analyses of the entire inventory of ground and on-orbit and returned ALCLR Ion Beds determined that

several other Ion Beds were partially or completely exhausted. This suggested the ALCLR Ion Bed S/N 1003

contamination and partial exhaustion was not a single occurrence. An incremental root cause that linked several of

the Ion Beds together was thereafter investigated.5

Blue – Conductivity

Red – Silicon Concentration

Figure 5. Capacity test results—Ion Bed S/N 1003—no remaining capacity.

Figure 6. Capacity test results—Ion Bed S/N 1013—significant remaining capacity.

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The free water (~100 mL) drained from 3-micrometer filter housing S/N 1034 was found to contain a relatively

high dissolved silicon concentration (16 ppm) when compared to the other three 3-micrometer filter water samples

that were analyzed, thus indicating the Ion Bed that last interfaced with 3-micrometer filter S/N 1034 was putting

out relatively high silicon level.5

A search of the ALCLR-related records was conducted. It was found that 3-micrometer filter S/N 1034 was last

used with ALCLR Ion Bed 1003 on August 14, 2012, indicating silicon was being released from ALCLR Ion Bed

1003 at that time and then presumably flowed through 3-micrometer filter S/N 1034 and into the SEMU FPS that

was undergoing the ALCLR process at the time. The ALCLR-related records then showed that the ALCLR Ion Bed

S/N 1003/3-micrometer filter combination interfaced with SEMU 3011 on August 14, 2012—the first indication of a

source of silicon-rich water flowing directly into the SEMU 3011 FPS Water Separator drum. Furthermore, ALCLR

Ion Bed S/N 1003 interfaced two additional times with SEMU 3011 after it was determined to be exhausted on

August 14, 2012, prior to the July 16, 2013, water-in-the-helmet mishap. What remained unanswered at that time

was why the silicon was preferentially being released from ALCLR Ion Bed S/N 1003, why the silicon then

precipitated in the SEMU 3011 FPS Water Separator Drum, the reason for ALCLR Ion Bed S/N 1003 to exhibit out-

of-family exhaustion, and the source of the out-of-family silicon levels.3,5

C. Silicon Retention on an Ion Exchange Resin

A review of the literature and discussions with several subject matter experts helped provide an understanding of

why silicon was being preferentially released from ALCLR Ion Bed S/N 1003. Silicon, as dissolved silicic acid, is a

weakly bound anion to ion exchange resin. Other anions, such as carbonate, chloride, phosphate, and sulfate will

displace silicic acid from anion exchange sites in a competitive situation.6

As previously mentioned, ALCLR Ion Bed S/N 1003 used with EMU 3011 on August 14, 2012 (S/N 1003) was

found to be contaminated with high levels of silicon, chloride, and sulfate anions. The chloride and sulfate ions are

expected to more strongly bind to ion exchange resin vs. ionic silicic acid, which is weakly bound It was surmised,

at that time, that the high levels of chloride and sulfate anions would be expected to displace the normally weakly

bound ionic silicic. The displaced ionic silica would then be expected to either move further down the scrubber bed

to fresh anion exchange sites (if available) or would exit the scrubber bed.

As nominal levels of more strongly bound anions continued to enter the scrubber bed, they would continue to

displace the more weakly bound ionic silica. Nominal ionic silica eventually would run out of fresh anion exchange

sites with which to bind as well and would exit the ion exchange bed. After the August 14 incident, ion exchange

scrubber bed S/N 1003 was effectively an ionic and precipitated silica generator.6,7

D. Silicon Precipitation A review of the literature and discussion with several subject matter experts also helped provide an

understanding of why silicon would precipitate in the SEMU 3011 FPS Water Separator Drum. The input suggested

that high levels of ionic silica in water are prone to agglomeration and particle formation, particularly where water

steams of varying pH join (the EMU Transport Water and Sublimator condensate streams merge in this area).

Furthermore, the input suggested that, once formed, particles of silicon would separate and migrate to the outer

walls of the FPS Water Separator in operation due to its centrifugation action at 19,300 revolutions per minute. The

Water Separator undergoes periodic drying during operation, which is further expected to lead to ionic silica

exceeding solubility limits and forming silica/silicate-rich precipitates. Finally, once a layer of silica/silicate

precipitates forms, it would be expected to attract additional silica/silicate that was introduced.6

Beaker level tests related to silicon solubility in water were conducted and showed that silicon solubility in

solution was a function of pH (↑ Si at ↑pH) which is in agreement with the literature sources that were referenced

and input from various subject matter experts.11

Shifts in water pH (start at pH 2 – 10, shift to pH 5 and pH 7) showed little effect on Si solubility with/without

centrifugation indicating that potential pH shifts due to the joining of two water streams in the EMU (Sublimator

condensate stream and Transport Water Loop) likely played a minimal if any role in the precipitation of

silica/silicates in the SEMU 3011 Separator Drum.11

The presence of metal cations (Fe, Ni, Zn) at various pHs (2 – 10) showed little effect on Si solubility,

suggesting that corrosion products from the SEMU 3011 Pump Rotor or other fluid loop sources played a minimal,

if any, role in the precipitation of silica/silicates in the SEMU 3011 Separator.11

The presence of Braycote® showed essentially no effect on Si solubility, suggesting that the excessive Braycote

®

observed in several areas of the SEMU 3011 Transport Water Loop likely played a minimal, if any, role in

facilitating the precipitation of silica/silicates in the SEMU 3011 Separator Drum. It should be noted, however, that

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once precipitates formed, excessive Braycote® would be expected to act as a “trap” for precipitated silica/silicates,

thereby serving as a potential collection point.11

Testing indicated that as water volume was reduced through evaporation, the ratio of total Si/reactive Si

increased at pH 9 – 10, indicating colloidal Si formation, essentially the first step in the precipitation of Si. Through

evaporation, the amount of Si-rich precipitate that formed was shown to be a function of water pH (↑ Si at ↑pH). So

a basic solution with high levels of Si would result in a relatively high Si precipitate due to the water evaporation

expected to occur in the EMU Water Separator, a feasible pathway to what occurred in the SEMU 3011 Water

Separator Drum.11

E. Contaminated Ion Bed Link to Ground Processing

Immediately following the EVA 23 mishap, it was evident that a water cleanliness problem on orbit would

require remediation. Since the ALCLR filters were the primary means of scrubbing the EVA water loops and the

investigation had not yet uncovered a reason to suspect the filters, manufacture of eight additional ALCLR units

(S/Ns 1020 – 1027) was initiated in anticipation of using them for the recovery effort. Assembly and ground

processing of the filters was completed on December 20, 2013, and three of the filters (S/Ns 1020, 1021, and 1022)

were shipped for flight on Orb-1 on December 23, 2013. The remaining filters were sent to Building 7 controlled

storage.8

On December 26, 2013, “smudges and scratches” were noted on the exterior of the housings of the recently

processed ALCLR filters, prompting an inspection. Further analysis of the hardware revealed that the housings were

pitting and corroding, in some cases all the way through the housings (Figure 7).8

Figure 7. Pitting and corrosion on the external surfaces of the ALCLR housings.

After discovery of the corroding filters, water samples were taken from the free water in the ALCLR filters, the

Activated Carbon/Ion Exchange (ACTEX) test stand (where the filters are processed), several DI water faucets in

the Building 7 facility, and the output of the Building 7 deionized (DI) water processing facility. In all cases, the

water conductivity and chloride concentrations exceeded the Type A Space Shuttle water specification, SE-S-0073,

which was the water specification for the EMU at the time of the mishap (see Table 1 for key data outages from SE-

S-0073).1

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These results suggested gross contamination of the ALCLR Ion Beds before they were launched to the ISS and

identified a potential issue with the flight hardware ground test facilities. All on-orbit ALCLR activities were

suspended at that point. ALCLR units were pulled from controlled storage and returned from the ISS for analysis,

which confirmed that ALCLR units were transported to the ISS in a contaminated state, though they were not

actually used on-orbit. ALCLR Ion Bed ground processing became a major focus of the mishap investigation

thereafter.

F. Airlock Cooling Loop Recovery Ion Bed Ground Processing

The building 7 centralized DI water processing facility provides the water that is used to process the ALCLR Ion

Bed. Several shortcomings of this water system were found upon further investigation, as follows:1

1. The water effluent conductivity sensor was set at 5.0 µS/cm vs. the requirement at that time of < 3.3

µS/cm. A visual indicator—a simple green/red light—indicated compliance with this requirement. 2. The system conductivity sensor was located after the last ion exchange bed (the industry standard is to

locate the conductivity sensor before the last ion exchange bed to provide a safety buffer), allowing

potentially poor quality water to be delivered to the processing area if no one noticed the green-to-red

light change

3. A single technician was assigned the task to periodically look at the conductivity indicator light in a

remote location. There was no requirement to notify building users of this water if the red light

indicated poor quality. Furthermore, the supplier of the system would be notified if a system ion

exchange bed was exhausted; replacement of that bed could take several days. Finally, there was no

backup in the event the primary technician was absent.

4. No recheck of the quality of the DI water occurred prior to the point of interface with the ALCLR Ion

Bed being processed, though several hundred feet of static water separated the final ion exchange bed

from the point of hardware interface.

Various water samples from the Building 7 ALCLR Ion Bed processing laboratory (i.e., EMU lab) including the

test stand used for processing and several Building 7 locations were analyzed and were found to greatly exceed the

SE-S-0073 water quality requirements for process water. Some of these samples were found to be comparable to tap

water quality.1

The ion beds are processed at Johnson Space Center (JSC) in Building 7 in two phases: bed packing and bed

flushing. After the raw material is loaded into the ion bed, the bed is flushed with 150 pounds of DI water to remove

particulate. If there are any contaminants in the flush water, they are concentrated on the ion bed during the flush.

The ground processing investigation found a number of configuration and process management issues with the

Building 7 DI water system that lead to the facility DI beds passing silica and other contaminants downstream when

the facility beds were near the end of their life. The investigation concluded that the source of the excessive silica

and exhausted ALCLR Ion Beds was from ground processing and loading of the ALCLR ion beds.1,7

As long as the anion or cation resin in the ALCLR Ion Bed was properly processed with good quality water (not

exhausted), the effluent water would be free of ions and the pH will be close to neutral in the on-orbit ALCLR

application. Once the resin became partially or fully exhausted due to processing with poor quality water, in-

operation ions that were previously exchanged and held to the resin would be released into the bed effluent (into the

EMU FPS on-orbit during the ALCLR process). Since the ions would be concentrated and ordered within the bed

length by affinity for the resin, the ions would not be released in the order they enter into the bed. Rather, they

would be released from lower affinity to higher affinity to the resin functional group. That means all the weakly

Table 1. Post ALCLR Corrosion Discrepancy Free Water Test Results

Parameter ACTEX Test

Stand ALCLR S/N:

1023 ALCLR S/N:

1027 LCVG Test

Stand

Crew Escape DI

Sink

Bldg 7 DI Facility Output

SE-S-0073

Conductivity (μS/cm)

150 2500 130 107.9 141.9 717* < 3.3

Chloride (ppm) 36 730 26 23.2 - - < 1

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ionic contaminants on the resin will be displaced first (such as silicon as silicic acid) and be released into the

effluent due to adsorption of stronger ionic contaminants in the influent.6,7

V. Proximate and Root Cause Analysis

The process used to determine the causes of the SEMU 3011 FPS failure has been vetted through numerous

investigations of ISS hardware including the 2007 Russian computer failure, the starboard solar array rotary joint

failure, and the external thermal control system pump module failures. A fault tree is used to determine the

proximate cause(s), then a causal tree determines the intermediate cause(s) of the proximate cause (Figure 8).

Technical rationale is documented for each event and dispositioned as either a contributor or a non-contributor to the

failure. The intermediate causes are then assessed to determine the root cause(s) by repeatedly asking why that event

was able to manifest to failure. Definitions are consistent with NPR 8621.1B “NASA Procedural Requirements for

Mishap and Close Call Reporting, Investigating, and Recordkeeping.”1

Figure 8. Relationship of fault tree to causal tree.

The scope of the failure investigation effort was defined by the activities related to the evaluation of first a

proximate cause fault tree, and then a causal tree. The proximate cause for this failure investigation was determined

by a fault tree. Within days of the failure, a fault tree was created that included all credible hardware failure

mechanisms that could result in the observed failure signature during EVA 23. The top event, or failure signature,

was “Liquid leakage internal to EMU 3011 free volume on 07/16/2013 during EVA 23.” Potential leakage sources

included: bodily fluids that migrated to the helmet; EMU element failures that would result in water leakage into the

suit free volume, then migrate to the helmet; and EMU element failures that would import water directly to the

helmet or introduce it through the vent loop. This fault tree scoped the actions necessary to determine the proximate

cause of the failure.1

An action plan was created. This plan identified the investigative actions necessary to close each of the fault tree

events. Actions included inspections, tests, analyses, documentation reviews, etc. Initially, each event on the fault tree was

colored either yellow or orange, thus indicating that forward work was planned. Those events colored orange were given a

higher priority, and closure rationale would be discussed in team meetings. Closure rationale was documented for each of

the 44 basic events. The team evaluated the closure rationale to determine whether each basic event contributed to the

failure. Events were colored green if technical information confirmed that the event was not a contributor. Events colored

blue were determined to be non-contributors, but substantiated largely by engineering judgment. Contributors were

colored red in the fault tree. Through evaluation of the closure rationale, the proximate cause was identified as “Water

separator drum feed holes become plugged, redirects flow into vent circuit” (Figure 9).1

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Figure 9. Fault tree.

Once the proximate cause was identified, a causal tree was developed to include all potential causes of the

proximate cause, and all the sources of the contamination in the coolant loop that plugged the water separator drum

feed holes, and to determine the intermediate cause(s) (Figure 10). Sources of contamination included those

resulting when the ALCLR components are not capable of removing contaminants and become a source of silicon

(including ion bed S/N 1003, LCVG, Water Line Vent Tube Assembly, Payload Water Reservoirs, umbilicals, or

changes to pH); silicon in the EMU water exceeds the capability or precipitates between scrubs (from sublimator

hydrophilic coating, Space Shuttle coolant loop, or airlock heat exchanger); the temperature profile affects the

solubility of silicon; or static time between wet-dry cycles contributes to the accumulation of silicon. Closure

rationale was documented for each of the 42 potential causes, and was evaluated by the team. The findings (red

events) and significant observations (identified by rounded corners on the description box) were determined by

dispositioning each event.1

Figure 10. Causal tree.

These findings and significant observations were then categorized by similarity of the causes as either an

operational response, a response to water quality management, or an EMU hardware processing issue. Each finding

and significant observation causal tree event was then mapped to these categories on a root cause determination

matrix spreadsheet. The team then asked the “three whys”—a technique where the team asked why the event was

allowed to manifest at least three times until an organizational factor was identified. Corrective actions were then

identified for each root cause in a Corrective Action Plan (CAP) to ensure the failure would not be repeated. Finally,

the high-level investigation results were documented in an event sequence diagram (Figure 11).1

A “list of truths” was collected throughout the investigation. Examples of these truths are the order of processing

or use of ALCLR elements, physical barriers in the system, test results, hardware processing issues, etc. Once the

Liquid leakage internal to

EM U 3011 free volume on

07/16/2013 during EVA 23

GM T197

EM U element failure results

in water leak into suit f ree

volume (other than helm

G055

EM U element failure leaks

water into suit f ree volume

(other than helmet)

G001

External leakage of SSA

component is the source of

the f luid

G007

Drink bag leaks into free

volume of suit (other than

helmet)

G003

W. Fritz

10/8/13

External leakage of Liquid

Transport System water into

suit f ree volume

G031

External leakage of LCVG

107 garment water lines into

suit f ree volume

G071

W. Fritz

11/06/13

External leakage of LCVG

M WC (garment side) in HUT

G072

W. Fritz

11/06/13

Leakage of water from HUT

into free volume

G036

Leakage from HUT hardlines

into free volume

G117

Leakage of liquid transport

circuit ports at crew neck

G060 Page 1

Failure of LCVG port T4 or

line at back of neck ring

G064

W. Fritz

11/06/13

Failure of LCVG port T5 or

line at back of neck ring

G061

W. Fritz

11/06/13

Failure of LCVG port T6 or

line at back of neck ring

G062

W. Fritz

11/06/13

Failure of LCVG port T7 or

line at back of neck ring

G063

W. Fritz

11/06/13

Crew/suit interference at

neck results in damage to

f luid f low elements

G019

W. Fritz

11/06/13

Leakage of line to port T8

into HUT at crew neck (from

tank)

G132

W. Fritz

10/25/13 R1

Leakage of cooling water at

M ult iple Water Connector

on HUT side

G038

W. Fritz

11/06/13

Leakage from Water Line

Vent Tube Assembly HUT

interface tubing

G045

W. Fritz

11/06/13

WLVTA - HUT interface (at

tube/ line connector)

G118

W. Fritz

11/06/13

Fit (suit /crew) induced

failure

G009

Crew/suit interference

results in damage to suit

element

G017

Crew/suit interference with

HUT results in damage to

f luid f low elements

G020

W. Fritz

11/06/13

(Restricted space) body

movement causes localized

damage to element

G018

W. Fritz

11/06/13

Improper donning of suit

results in binding or

crimping of suit element

G010

W. Fritz

11/06/13

Water migrates to helmet

(not absorbed by crew

clothing layers)

G056

W. Fritz

11/06/13

Bodily f luid from

crewmember migrates

through suit to helmet

G002

W. Fritz

10/15/13

EM U component failure

results in approx. 1.5L water

in crew helmet

G057

EM U element failure results

in water introduced into

vent ilat ion circuit

G012

Localized failure forces f luid

into vent circuit

G005

Gas trap 141 o-ring fails,

bypass orif ice, f loods WS

and enters vent

G044

B. Peavey

10/17/13

Blocked WS inlet causes

water backf low into

sublimator slurper holes

G079

W. Frost

8/7/2014

Pitot actuated valve 125

internal failure (WS out let to

WS inlet)

G081

W. Frost

11/1/2013

Valve module assembly

crossover leakage (internal

Water to O2)

G085

C. Yau

10/25/13

Water enters vent loop when

regulator fails

G086

H2O press regulator 113E

(gas side of water tanks)

failure overpress feed water

G087

W. Frost

10/15/13

Failure of dual mode relief

valve 120

G088

W. Frost

10/31/13

Failed 123 seal cup leaks

into vent loop

G140

B. Peavey

11/06/13

WS o-ring cut leaks water

into vent circuit

G141

B. Rossato

12/11/2013

LCVG leak in proximity of

vent loop return duct, thru

CCC, fan and vent

G119

W. Fritz

10/22/13

Leakage internal to M WC

into transport water line into

vent circuit

G123

W. Fritz

10/17/13

Redirected f low through

system

G008

Sublimator internal failure

results in water released into

O2 vent loop

G042

W. Frost

10/25/13

134 Filter/valve blockage

redirects f low through vent

loop

G039

Clogged 134 f ilter redirects

f low into vent circuit

G091

W. Frost

10/22/13

Condensate water relief

valve 134 fails closed

redirects f low into vent

circuit

G092

W. Frost

10/31/13, R3_11/6/13

Water separator internal

failure leaks water into vent

loop

G052

B. Rossato

12/11/2013

Rupture of water tank

bladder causes water to

enter T11

G047

C. Yau

10/15/13

WS pitot or drum feed holes

become plugged redirects

f low into vent circuit

G040

B. Rossato

1/31/2014

Blockage between 134

out let & 127 f ilter redirects

f low into vent loop

G146

D. Dihn

12/12/2013

Blockage between WS pitot

out let & 134 valve module

redirects f low to vent loop

G147

D. Dinh

12/12/2013

Drink bag contents released

through drink bite valve into

helmet

G014

W. Fritz

10/8/13

Condensate leaks into EM U

vent loop thru separator

drum

G143

Relief valve 135 fails closed

G144

B. Peavey

11/07/13

Bladders hard charged

G145

B. Peavey

11/07/13

Water introduced at PortT11

G120

Water tank bladder fails,

releases water thru 120A

orif ice and out T11

G121

W. Fritz

10/15/13

Leakage at internal HUT

water lines impinges on crew

neck

G130

Leakage of liquid transport

circuit ports at crew neck

G060

Page 1

Leakage of line to port T8

into HUT at crew neck (from

tank)

G132

W. Fritz

10/25/13 R1

HUT - PLSS interface 2

o-ring failure results in leak

(O2/H2O combo)

G142

C. Yau

11/5/13

Suit maintenance-induced

failures

G011

Suit servicing (Ground)

results in leakage

G022

B. Rossato

1/31/2014

Suit servicing (Orbit) results

in leakage

G023

B. Rossato

1/31/2014

Suit storage and/or handling

results in leakage of suit

element

G075

W. Frost

4/29/2014

Degradat ion of wetted suit

elements while stored

on-orbit

G076

W. Frost

5/15/2014

Contaminat ion in the

coolant water loop plugs

EM U3011 FPS Drum Holes

RCA_EM U3011

ALCLR is not capable of

removing contaminants,

becomes a source of Si

G017

Ion bed S/N 1003 releases

Si into EM U water

G018

Charcoal in ion bed

contributes to saturat ion of

ion bed

G020

Post-rinse (gnd processing)

insuff icient to remove

contaminants

G022

J. Steele

6/10/2014

M igrat ion of inherent Cl,

SO4, Si f rom act ivated

carbon to ion exchange resin

G023

J. Steele

6/10/2014

Inherent Cl and SO4 in ion

bed charcoal displace Si in

ion bed

G024

J. Steele

6/10/2014

Charcoal f ine part iculate

foul ion exchange resin

pores which reduces

capacity

G054

J. Steele

5/22/2014

Stat ic t ime between uses

increases concentrat ion of

Cl, SO4, Si

G053

J. Steele

5/22/2014

Lot-to-lot variat ion of

source charcoal with

increased contaminants

G066

J. Steele

5/22/2014

Poor water quality in Bldg 7

water (RO/DI test stand

&lines) introduced to bed

G021

Water processing system

not opt imized for this

applicat ion

G056

B. Greene

7/1/2014

Signif icant amount of

stagnant water prior to test

stand (~600' of lines)

G027

M . Jennings

8/1/2014

Signif icant amount of

stagnant water in test stand

and support ing tanks

G067

M . Jennings, B. Greene

7/30/2014

RO system degraded or

bypassed results in poor

quality water

G028

B. Greene

6/30.2014

DI water system not

conf igured to protect for

breakthru, so poor quality

water

G055

B. Greene

6/30/2014

M aintenance escape in

water processing results in

contaminated ion bed

G047

B. Greene

6/30/2014

Fails to have/meet

conf igurat ion control of

water processing plant

G048

B. Greene

7/7/2014

Insuff icient water polishing

and/or test ing at point of

use to ensure quality

G049

B. Greene

6/30/2014

B 7 water processing plan

fails to remove ions from

water (uses ALCLR

capacity)

G050

B. Greene

7/1/2014

DI bed exceeds life limit

sheds Cl, SO4 and/or Si

which loads ion bed

G052

M . Jennings, B. Greene

6/17/2014

Charcoal used in water

processing DI beds not

opt imized for this

applicat ion

G068

B. Greene

6/12/2014

B7 Super Q System

introduces Si into water

upstream of ACTEX stand

G070

B. Greene

7/30/2014

Ion bed not processed

correct ly (const ituents,

packing, cleaning, etc.)

G033

M . Jennings

5/22/2014

Iodinat ion of ion bed

charcoal accelerates use of

ion bed capacity

G034

J. Steele

5/8/2014

Ion bed housing/material

not built to spec, sheds

excessive Si, Cl or SO4

G041

M . Jennings

5/15/2014

Other contaminat ion sources

G019

LCVG 3228 processing

introduces contaminat ion

into suit water on orbit

G030

Residual detergent in LCVG

3228 adds CL & SO4 to

suit water

G029

W. Fritz

5/8/2014(rev)

LCVG sheds acetate,

changes pH of water

G002

J. Steele, L. Hewes

5/15/2014

LCVG not built to

specif icat ion (inadequate

cure, material)

G039

J. Clougherty

6/3/2014

Fan Pump Separator local

corrosion introduces

Ni(OH)2 and/or displaces

Si

G010

B. Greene

8/5/2014

WLVTA introduces

contaminat ion into water on

orbit

G051

WLVTA not built to

specif icat ion (inadequate

cure, material)

G057

J. Clougherty

5/15/2014

WLVTA sheds acetate,

changes pH of water

G058

L. Hewes

5/15/2014

PWR not to specif icat ion

(mat 'l, cleanliness)

introduces contaminat ion

G060

C. Vande Zande

6/5/2014

PWR source water not to

specif icat ion introduces

contaminat ion

G061

B. M acais

6/19/2014

Umbilical (IEU or SCU)

Tef lon Core hose introduces

contaminat ion into water

G059

Umbilical (IEU or SCU) not

built to specif icat ion

(inadequate cure, material)

G062

V. M argott

5/15/2014

Change in pH or water

chemistry exacerbates

shedding of Si

G042

High CO2 on orbit changes

pH and accelerates use of

anion exchange capacity

G044

J. Steele

5/8/2014

Low EM U water pH thru HX

accelerates release of Si

from ion bed/uses capacity

G046

D. Shindo, J. Steele

5/8/2014*

Human in the loop

introduces contaminat ion or

exacerbates suit water

chemistry

G009

J. Steele

5/22/2014

Si released into EM U water

exceeds ALCLR capability

or precipitates b/w scrubs

G037

EM U sublimator S/N 029

hydrophylic coat ing is

contaminat ion source

G003

Sublimator manufacturing or

coat ing-related defect

results in release of Si

G007

D. Holder, B. Greene

7/22/2014

Excessive shedding of Si

from EM U 3011 sublimator

G008

D. Holder, B. Greene

7/30/2014

Sublimator storage-related

defect results in shedding

excessive Si

G040

D. Holder

5/8/2014

Air Lock Heat Exchanger is

contaminat ion source (both

for current and last HX)

G001

Page 1

Shutt le coolant loop

introduces CL, SO4 or Si

into EM U 3011

G069

D. Cybulski

6/5/2014

Temperature prof ile

support ing EVA ( lower

solubility of Si @lower

temperature)

G064

J. Steele

5/22/2014

Stat ic t ime and/or wet/dry

cycles contribute to

accumulat ion of Si

G065

J. Steele

5/22/2014

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failure scenario, or sequence of events, was identified, it was challenged by the list of truths. The failure scenario

was confirmed when it didn’t invalidate any of the truths.1

In summary, a systematic, structured approach resulted in a CAP that ensures all findings and significant

observations are mitigated to preclude future failures. A fault tree was created to determine the proximate cause. The

investigation was bounded by identifying the actions necessary to evaluate each event as a contributor. The failure

mechanism was determined by dispositioning each event on the fault tree. The causal tree examined the potential

causes of the contamination to determine the intermediate cause. All findings and significant observations were

grouped by similarity, then the root causes were identified by asking why they were able to manifest to failure.

Corrective actions were assigned to each root cause to preclude a repeat of this failure signature. The results were

documented in an event sequence diagram.1

Figure 11. Event sequence diagram.

This exercise was a valuable, systematic means to arrive at proximate and root cause of the SEMU 3011 Water

in-the Helmet, as well as an organized means for a detailed treatment of corrective actions.

The proximate cause was determined to be: Water separator drum feed holes became plugged, and redirected

water flow into vent circuit.

The primary root cause was determined to be: Poor water quality in JSC Building 7 water introduced into

ALCLR Ion Beds during ground processing, resulting in partially and fully exhausted ALCLR Ion Beds being used

with the on-orbit ALCLR processing of SEMU 3011. The key elements of this root cause analysis numbered 31, with

numerous intermediated causes and significant observations. The key elements of the root cause analysis fit into

three broad categories: Operational Responses, Water Quality Management, and EMU Hardware Processing.

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VI. Corrective Action Plan

The investigation concluded with a number of intermediate causes, root causes, significant observations, and

corrective actions. A subset of these corrective actions was implemented as part of the effort to restore planned EVA

capability. These corrective actions included: water quality and management across the EVA ground facilities; on-

orbit recovery through water line flushing and component replacement; generation of associated safety

documentation; properly controlling and verifying ion bed processing; and implementing on-orbit sampling and

monitoring for the EMU/Airlock coolant loop.

An EVA Suit Hardware Components and Processes Audit was performed in March 2014. This audit focused on

items contained within the feed-water and coolant loop system of the EMU. These five facilities were audited: SGT;

UTAS Windsor Locks; ILC; JSC Building 7; and JSC Building 9. Four critical non-conformances were found and

addressed.1

Following the water audit, auditors developed CAPs for audit findings and closed them by providing objective

evidence to the EVA hardware engineers. Final CAP closures occurred at the EMU Panel. Of the 98 audit items

assigned, 38 CAPs remain open as of mid-July 2014. All open items have closure plans and dates identified in their

CAP response.1

As the investigation continued to reveal that contamination of water used in the EMU and its ancillary systems

was a significant concern, it was determined that an update to the specifications governing water quality in the EMU

was necessary. Historically, either the Space Shuttle Specification Fluid Procurement and Use Control Document

(SE-S-0073) or the System Specification for the International Space Station (SSP41000) was used to control the

quality of water in both the EMU feed-water and transport water circuits; although these where not in conflict with

the needs of the EMU, they lacked certain parameters that were discovered as contaminants in the proximate cause

of the SEMU 3011 water intrusion failure. As such, a new document was crafted to address water quality needs

specific to the EMU system. JSC-66695, EMU Water Quality Specification, was written to define the water quality

for any water used in the maintenance, processing, or testing of EMU hardware or any hardware that interfaces with

the EMU transport water circuit and feed water circuit.9

The requirements found in JSC-66695 define the quality of source water prior to being used in the EMU in an

effort to mitigate contamination failures of various components. These requirements are not intended to control

water quality within the EMU during operations. Controlling water quality during operations is accomplished via

maintenance, both on the ground and on-orbit. The feed-water circuit receives periodic flushing, referred to as a

dump and fill. The transport circuit receives loop scrubs using the ALCLR hardware. From a technical perspective,

the requirements found in the EMU Water Quality Specification add the need to evaluate silica, total carbon,

bacteria count, and particulate in source water, as well as tighten the threshold of acceptable quantities of other

contaminants when compared to the heritage Space Shuttle and Space Station documents.9

The EMU Water Quality Specification was written by a team comprised of chemistry and hardware experts

throughout the NASA and contractor community. It was reviewed from April through June 2014, including multiple

team meetings to finalize and validate the requirements. Final signature was obtained on June 14, 2014.

In parallel to the work that was done to create the JSC-66695 EMU Water Quality Specification, the OneEVA

contractor began formation of a Water Management Plan to address how water is being managed throughout all the

various facilities used during EMU processing or testing. This document was needed to respond to the changes in

water sampling required in response of the EMU 3011 Water Intrusion Failure. Each facility used by OneEVA and,

in many cases, each specific test stand, maintains its own requirements and verifications to validate performance and

water quality. The Water Management Plan describes the intent, operation, and changes required for each of these

end items. The single greatest change throughout the processing of EVA hardware is the sampling plans, including

ensuring sampling is consistent throughout any stage of processing or testing. The OneEVA Water Management

Plan describes each of the facilities on contract and how the contractor will execute sampling, source water

processing, and maintenance.10

The corrective actions to this investigation continue to be worked. Key corrective actions that have been

implemented include: the generation of an EMU-specific water quality specification and water management plan;

the development and certification of an ALCLR Ion Bed process independent of direct Building 7 DI water; the

implementation of numerous water quality checks prior to, during, and after the processing of ALCLR Ion Beds; the

implementation of on-orbit sampling before and after ALCLR scrub events; the evaluation of every ALCLR Ion Bed

and 3-micrometer filter after flight use; and a reduction in the number of ALCLR Ion Bed uses on orbit to enhance

safety margin.

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VII. Summary

The proximate cause of the U.S. EVA 23 water-in-the-helmet mishap was blockage of all water separator drum

holes by a mixture composed primarily of silica and silicates. The blockages caused a failure of the water separator

function that resulted in EMU cooling water spilling into the ventilation loop, migrating around the circulating fan,

and ultimately pushing into the helmet. The root cause of the failure was determined to be JSC Building 7 ground-

processing shortcomings of the ALCLR Ion Filter Beds, which led to various levels of contaminants being

introduced into the filters before they left the ground. Those contaminants were thereafter introduced on-orbit into

the EMU hardware during ALCLR scrubbing operations. A methodical fault tree/causal tree activity was used to

uncover 31 key elements to the root cause as well as numerous intermediate causes and significant observations. A

regimented CAP was prepared to address all findings in a prioritized fashion to ensure a return to, and a

sustainability of, nominal ISS EVA status.

References 1 EVA Recovery Team Summary Report, EVA 23 Mishap Action Response, November 21, 2014. 2 NASA Extravehicular Mobility Unit (EMU) Life Support Subsystem (LSS) and Space Suit Assembly (SSA) Data Book,

September 2009. 3 United Technologies Aerospace Systems (UTAS) Presentation, “SEMU 3011 Investigation”, R. Rossato, February 13, 2014 4 Steele, J. W., Boyle, R., Etter, D., Rector, T., Vandezande, C., 2013. “Efforts to Reduce International Space Station Crew

Maintenance for the Management of the Extravehicular Mobility Unit Transport Loop Water Quality”, AIAA 43rd International

Conference on Environmental Systems, Vail, Colorado. 5 United Technologies Aerospace Systems (UTAS) Presentation, “SEMU 3011 Mishap Investigation ALCLR Ion Bed & 3-

micron Filter Analysis”, J. Steele, December 16, 2013.

6 Iler, Ralph K., 1079, “The Chemistry of Silica – Solubility, Polymerization, Colloid, Surface Properties and Biochemistry”,

John Wiley and Sons. 7 Lorch, Walter, 1987, “Handbook of Water Purification”, W. Lorch/Ellis Horwood Limited. 8 United Technologies Aerospace Systems (UTAS) Presentation, “ALCLR Cartridge Corrosion Investigation – Status

Update”, J. Steele, January 22, 2014. 9 JSC-66695, “EVA Management Office EMU Water Quality Specification”, June 11, 2014. 10 “EMU Water Management Plan” In Revision as of 01/23/2014. 11 United Technologies Aerospace Systems (UTAS) Internal Document, SVME 6997 “EMU Delivery Order DO-72 Final

Report” J. Steele, October 30, 2014.