Existing Structure Materials Testing
Transcript of Existing Structure Materials Testing
May 1, 2015
Mr. Gus Fischer
Dreyfus & Blackford Architects
Via email to: [email protected]
Existing Structure Materials Testing
AC TRANSIT D3 REACTIVATION PROJECT
2016 MacDonald Avenue
Richmond, California
WKA No. 10530.02
As authorized, Wallace-Kuhl and Associates (WKA) has provided materials sampling and
testing services to support evaluation of the existing AC Transit maintenance building in
Richmond, California.
The purpose of our work has been to provide information regarding the masonry wall and roof
slab materials to support evaluation of the building by Buehler & Buehler (B&B), the project
structural engineer. Our scope of work was based on email and verbal discussions with B&B
and the core sampling and testing locations shown on the attached Proposed Repair Plan
sketches prepared by B&B. Our findings are described below.
Masonry Walls
We observed the masonry walls at several accessible locations and verified the rebar
placement with non-destructive equipment (Hilti PS1000 ground penetrating radar (GPR)
machine) and some limited demolition. At the locations where we obtained our core samples,
the rebar in the 8 and 12 inch wide walls was placed in general accordance with the original
construction plans – both vertical and horizontal bars at approximately 16 inches on center.
As requested by B&B, we removed two face shells and a small amount of grout to expose the
extra rebar in the wall pier at Column Lines B @ 2 approximately four feet above ground level.
We found the No. 9 vertical bars and No. 3 ties were present at approximately the spacing
shown in Section G S-206/S-216 of the 1987 building plans.
We observed a significant amount of efflorescence buildup at the inside of the south wall near
core location WC10. It appeared that there was some loss of face shell material where the
efflorescence buildup was greatest.
Existing Structure Materials Testing Page 2
AC TRANSIT D3 REACTIVATION PROJECT
Richmond, California
WKA No. 10530.02
May 1, 2015
We obtained and tested ten core-drilled samples from the masonry walls to observe the
condition of the masonry and verify the strength of the wall materials. The cores were drilled
through the full thickness of the walls except at location WC 5 where the rebar congestion
made it impossible to drill through without cutting rebar. The interior face shell debonded from
the grout during coring at location WC9 (12” thick wall). The core also contained some of the
CMU block web, so a second core was drilled nearby. The interior face shell also debonded at
the second core at this location. Both face shells debonded during coring at location WC6 (16”
thick wall). In general, the grout at our core locations appeared to have been well
consolidated, with only a few small voids observed and little separation cracking at the grout /
CMU block interfaces.
We tested complete cores and portions of the cores for compressive and shear strength (ASTM
C39, C42 and C140; CBC Section 2105A.5). The compressive strength of the composite
cores, grout portion of the cores and CMU face shells we tested all exceeded 3000 pounds per
square inch (psi). The cores we tested for shear strength along the grout / CMU block interface
all exceeded 150 psi in shear strength. For comparison purposes, California Building Code
Section 2105A.5 requires a minimum shear strength of 2.5 x √ f’m or 137 psi for f’m = 3000 psi.
Please refer to the attached Masonry Materials Test Results for core locations and detailed test
results.
Concrete Roof Slab
We observed the roof slab at several locations and located the reinforcing steel with the GPR
machine in the areas where we obtained our core samples. As shown on the plans, there was
relatively little rebar or post tension tendon steel in the center of the bays between columns, but
larger amounts of banded tendons and transverse rebar were present along the column lines.
We observed some displacement (popping out) of the grout used to fill the tendon anchors
along the south side of the structure near the top of the ramp. When we lightly tapped the
grout at one anchor it fell off, revealing rusting of small amount of tendon protruding from the
anchor.
We obtained and tested core samples from the post-tensioned concrete roof slab. The
concrete at our core locations appeared to be well consolidated, with only a few small voids less
roughly 1/8 inch in diameter. The compressive strength (ASTM C39 and C42) of the cores
ranged from 3810 to 5700 psi, with an average of approximately 4680 psi. The average unit
Existing Structure Materials Testing Page 3
AC TRANSIT D3 REACTIVATION PROJECT
Richmond, California
WKA No. 10530.02
May 1, 2015
weight of the core samples was 145 pounds per cubic foot (pcf). Please refer to the attached
Concrete Core Compression Test Results for core locations and detailed test results.
Our representatives replaced the concrete we removed with high strength grout of greater
strength. We replaced the masonry materials in the areas where we cored through the
masonry walls with high strength grout. We replaced the face shells at the front (north) and
east sides of the building with CMU block of similar color and finish.
The information above is based on our exploration, sampling and testing of the building at
several discrete locations. All measurements should be considered approximate and may vary
at different locations within the structure. Please be aware that the conditions and configuration
of the construction materials may also vary throughout the structure.
Please contact me if you have any questions or need additional clarification.
Wallace - Kuhl & Associates
David A. Redford, P.E.
Senior Engineer
Attachments: Proposed Repair Plan Sketches with Core Locations
Photos of Tendon Anchor and Efflorescence
Masonry Materials Test Results
Concrete Core Compression Test Results
STAIR NO.3
STAIR NO.1
ELEVATOR
301
AA A B C D E F G H I
1
2
3
4
5
6
6.3
ma
tch
line
ma
tch
line
1 1/2" separation joint
South WingNorth Wing
4'
- 0
"4
' -
0"
add steel angle sheartransfer conn. alongshear walls pertyp all walls
provide additional steeljamb ea side of opngper typ
4' - 0" 4' - 0"
4'
- 0
"4
' -
0"
typ
typ
typ typ
1
SSK-08
1
SSK-05
JOB
JOB NO.
CLIENT BY SHEET NO.
DATE
BUEHLER & BUEHLERSTRUCTURAL ENGINEERS, INC.
600 Q St., Suite 200
SACRAMENTO, CALIFORNIA 95811
AC TRANSIT
2014-045500 Jan 23, 2015
- JDH SSK-03
1" = 20'-0"Proposed Repair Plan
Provide Cores at 1stfloor wall
- Indicates proposed location of concrete roof slab core testing
- Indicates proposed location of CMU wall core testing
H I J K L M N O P Q
1
22
3
4
5
6
6.3
R
5.2
6.1
ma
tch
line
ma
tch
line
1 1/2" separation joint
South Wing
22' - 3
"
4' - 0" 4' - 0"
typ typ
4' - 0" 4' - 0"
typ typ
4' - 0"
typ
typ
4'
- 0
"4
' -
0"
add steel angle sheartransfer conn. alongshear walls pertyp all walls
anlong line 5.2,provide slip condalong wall lentgth
provide new micropileFDN ea end of line Rwall per
1
SSK-05
provide additional steeljamb ea side of opngper typ
1
SSK-08
1
SSK-05
1
SSK-07
install shotcretealong Line R wallper
A
SSK-06
A
SSK-06
indicates added fiber wrap in east/west dir, typ
indicates added fiber wrap in north/south dir, typ
JOB
JOB NO.
CLIENT BY SHEET NO.
DATE
BUEHLER & BUEHLERSTRUCTURAL ENGINEERS, INC.
600 Q St., Suite 200
SACRAMENTO, CALIFORNIA 95811
AC TRANSIT
2014-045500 Jan 23, 2015
- JDH SSK-04
1" = 20'-0"Proposed Repair Plan
AC TRANSIT D3 REACTIVATION PROJECT
Richmond, California
WKA No. 10530.02
May 1, 2015
EFFLORESCENCE PHOTOS
Inside of wall at Core Location WC10
Detail of efflorescence with slight loss of material at CMU block face
AC TRANSIT D3 REACTIVATION PROJECT
Richmond, California
WKA No. 10530.02
May 1, 2015
TENDON ANCHOR PHOTOS
PT tendon anchors at south side near top of ramp
PT tendon anchors showing rust and displacement of grout cover
AC TRANSIT D3 REACTIVATION PROJECT WKA No. 10530.02
May 1, 2015
MASONRY MATERIALS TEST RESULTS
(ASTM C39, C42 and C140)
Page 1 of 2
Core
No.
Approximate
Location Dia.
Capped
Length Area
Correction
Factor
Maximum
Load
Compressive
Strength
(in) (in) (in2) (pounds) (psi)
Composite Masonry
Cores
WC1 8” wall, Line R @ 5.4 3.71 7.7 10.8 1.00 42,700 3950
WC2 8” wall, Line R @ 5.9 3.71 7.7 10.8 1.00 38,500 3560
WC8 8” wall, Line 6 @ H.7 3.71 6.0 10.8 0.97 42,400 3810
WC3 12” wall, Line Q @
3.5 3.71 11.7 10.8 1.00 44,500 4120
WC4 12” wall, Line 2 @ M 3.71 11.7 10.8 1.00 48,400 4480
Average 3980
Grout Cores
WC5 16” wall, Line 2 @ D 3.71 4.25 10.8 0.91 55,200 4650
WC6 16” wall, Line 2 @ B 5.64 11.2 25.0 1.00 95,200 3810
Average 4230
CMU Block
Coupons
Length
Thick-
ness Area
(in) (in) (in)
WC6A 16” wall, Line 2 @ B 5.02 1.25 6.3 NA 38,770 6150
WC6B 16” wall, Line 2 @ B 4.83 1.18 5.7 NA 30,420 5340
Average 5750
AC TRANSIT D3 REACTIVATION PROJECT WKA No. 10530.02
May 1, 2015
MASONRY MATERIALS TEST RESULTS
(CBC Section 2114A.9.3)
Page 2 of 2
Core No.
Approximate
Location Dia. Area
Maximum
Load
Shear
Strength Failure Description
(in) (in2) (pounds) (psi)
Grout / CMU Block
Shear Strength
WC7-A 8” wall, Line 6 @
C.6 3.71 10.8 3830 350
Partly at grout/face
shell interface and
partly in CMU
WC7-B 8” wall, Line 6 @
C.6 3.71 10.8 4620 430
Partly at grout/face
shell interface and
partly in CMU
WC9-A 12” wall, Line 6 @
M.5 3.71 10.8 1750 160
Along interface
between grout and
face shell
WC9-B 12” wall, Line 6 @
M.5 3.71 10.8 1750 160
Along interface
between grout and
face shell
WC10-A 8” wall, Line 6 @
Q.3 3.71 10.8 3800 350
Partly at grout/face
shell interface and
partly in CMU
WC10-B 8” wall, Line 6 @
Q.3 3.71 10.8 3810 350
Partly at grout/face
shell interface and
partly in CMU
Average 300
NOTES: Masonry materials testing was performed on cores and portions of cores that
were drilled horizontally through the walls.
One face shell debonded from Core WC8 during coring. The Composite
Masonry Core strength test was performed with one face shell and grout.
The face shells debonded from Cores WC5 and WC6 during coring, so the grout
and CMU block were tested separately.
The cores were obtained 3 to 4 feet above ground level except Cores WC7 and
WC8, which were obtained about 3 feet above the mezzanine floor.
AC TRANSIT D3 REACTIVATION PROJECT WKA No. 10530.02
May 1, 2015
CONCRETE CORE COMPRESSION TEST RESULTS
(ASTM C39 and C42)
Page 1 of 1
Core
No.
Approximate
Location Dia.
Capped
Length Area
Correction
Factor
Maximum
Load
Unit
Weight
Compressive
Strength
(in) (in) (in2) (pounds) (pcf) (psi)
Roof Slab
SC1 Line C.5 @
3.5 2.75 4.90 5.94 0.98 34,600 147 5700
SC2 Line J.5 @
3.5 2.75 4.65 5.94 0.98 27,400 145 4520
SC3 Line O.5 @
4.5 2.75 4.81 5.94 0.98 23,100 144 3810
Average 145 4680
NOTES: The slab concrete contained nominal 1-inch max size, normal weight aggregate.
The cores were drilled vertically down into the slab. Where necessary, the top
and/or bottom of the cores were trimmed with a wet saw prior to testing for
compressive strength.