Containment Materials Issues In High-Temperature Black...
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Transcript of Containment Materials Issues In High-Temperature Black...
Containment Materials Issues in High-Temperature Black Liquor Gasification
James Keiser, James Hemrick, Roberta Meisner, Gorti Sarma and Kimberly Choudhury
Oak Ridge National Laboratory
Peter Gorog and Ray LearyWeyerhaeuser Company
7th International Colloquium onBlack Liquor Combustion and Gasification
July 31-August 2, 2006Jyväskylä, Finland
2
Our Study Of Containment Materials For High-Temperature Gasification Has Concentrated On The New Bern Gasifier
Construction of the New Bern high-temperature gasifier began in November, 1995
This gasifier had its first production run in December, 1996
Several refractory repairs or replacements were made in 1997 and 1998
In early 1999, the lining was replaced with a fusion cast alumina refractory
In December, 1999, cracking was discovered in the stainless steel gasifier vessel, and the gasifier was taken out of service
The rebuilt gasifier resumed operation in late June, 2003, with a different fusion cast alumina refractory
In October, 2004, a fusion cast magnesia-alumina spinel refractory lining was installed
3
The High-Temperature Gasifier Subjects The Structural Materials To Very Hostile Environments
The hot-face refractory is exposed to molten smelt at temperatures of 950-1000°C
The back-up refractory is exposed to somewhat lower temperatures (800-900°C) and to smelt components that are transported through cracks and joints in the hot-face refractory
The temperature gradients and the volume increase resulting from reaction with smelt components produce highly compressive stresses on the surface of the hot-face refractory
Expansion of the refractory lining can create large tensile stresses in the metallic shell
4
Containment Materials Used In The New Bern HT Gasifier
Time period Reactor shell Back-up refractory lining
Hot-face refractory lining
Dec 1996 –Early 1999
316L stainless steel
Super duty refractory brick
60% Al2O3, SiO2brick
Early 1999 –Dec 1999
316L stainless steel
Fusion cast βAl2O3
Fusion cast α/βAl2O3 –manufacturer A
Jan 2000 –June 2003
Gasifier out of service
June 2003 –Sept 2004
Carbon steel High-alumina bonded brick
Fusion cast α/βAl2O3 –manufacturer B
Oct 2004 –present
Carbon steel Bonded mullite –based refractory
Fusion cast MgO-Al2O3 spinel
5
ORNL Examined Two Mullite Bricks Removed From The Original Lining Of The New Bern Gasifier
After about ten months of operation, less that half the brick remained at time of removal. Samples taken from the bulk, reaction zone and surface regions of both
bricks were analyzed using XRD and microscopic techniques, and compounds were identified that were a result of reaction of the smelt with the refractory.
7.3 cm7.3 cm
2.5 cm2.5 cm
“Bulk”“Bulk”
Intermediate ZoneIntermediate Zone
4.7 cm4.7 cm
“Bulk”“Bulk”
Reaction ZoneReaction Zone
SurfaceSurface
0.5 cm0.5 cm
6
ORNL’s Smelt Immersion Test Facility Simulates Exposure Of Materials To Molten Smelt In The New Bern Gasifier
Exposures are typically conducted at 900 or 1000°C for 50 or 100 hours
7
Immersion Tests Are Able To Reproduce The Degradation Seen In Refractories Exposed In High-Temperature Gasifiers
Alumina-silica (mullite) based samples exposed in the New Bern gasifier and in the immersion test system have reaction products such as nosean (Na8Al6Si6O24SO4) and nepheline (Na2O·Al2O3·2SiO2) on their surfaces
Fusion cast alumina refractories exposed in the gasifier and the test system show an increase in the sodium content near the surface with a surface layer enriched in Na2O-Al2O3, sodium aluminate (NaAlO2)
8
The Sodium Oxide – Aluminum Oxide Phase Diagram Shows The Series Of Compounds That Can Form
Increasing the amount of Na2O in Al2O3 results in phase changes and volume increases, so it is not unreasonable to expect significant stresses to develop and some degradation to occur
9
Samples Of New Bern’s Fusion Cast α/β Al2O3 Replacement Lining Contained The NaAlO2 Reaction Product
10
NaAlO2 Was Found On The Surface And In The Reaction Zones Of Fusion Cast Alumina Samples From The Skoghall
High-Pressure Black Liquor Gasifier
11
Core-Drilled Samples Of The Fusion Cast Alumina Linings Provided Information About Extent Of Reaction With Smelt
NaAlO2 found on hot face Increased Na content found at back of the working lining and front of backup lining No NaAlO2 detected in backup lining
Working Lining: α/β alumina Backup Lining: β alumina
1 inch
0%10%20%30%40%50%60%70%80%90%
100%
1.5 24.5 41.5 61.0
Distance from Hot Face (mm)
Cum
mul
ativ
e Ph
ase
(%)
Distance From Hot Face (mm)
Cum
ulat
ive
Phas
e (
%)
α-Al2O3
β-Al2O3
NaAlO2
1 inch
12
Material Volume Expansion
(%) Al2O3 - β-Al2O3 31 β’-Al2O3 32 NaAlO2 133
Reaction Of Alumina Refractory With Sodium Compounds Caused Dimensional And Microstructural Changes
~50% Conversion to NaAlO2
~25% Conversion to NaAlO2
<5% Conversion to NaAlO2
Original Structure
Hot
Fac
e
13
The New Bern Gasifier Was Out Of Service For More Than Two Years. When A Decision Was Made To Rebuild The Gasifier, A Number Of
Design And Material Changes Were Made
New Refractory/Shell System Design
Hemispherical Dome
Carbon steel refractory containment which is not susceptible to Cl- SCC
Crushable metal foam used between refractory and carbon steel shell
Fusion-cast alumina working lining (from different supplier) over high alumina backup lining
Expansion allowance for growth of refractory based on data collected after one year of operation
Test bricks of alternate materials were also installed
14
Laboratory Testing And Evaluation Of Previously Exposed Materials Guided Selection Of Alternate Refractories
Molten salt immersion test facility allowed immersion of refractory samples in molten salt at 1000°C
Light microscopy, scanning electron microscopy and electron microprobe were used to characterize the extent of reaction between refractories and salt
Studies of refractories exposed previously in operating gasifiers and exposed in the immersion test facility provided guidance on selection of the refractory lining material
Refractory studies also identified alternate materials to be exposed as test bricks in the lining of the rebuilt gasifier
15
In February 2004, The Gasifier Was Shut Down For Quench System Repairs And Refractory Examination
Pieces of refractory brick were being recovered on a regular basis from the trap on the quench tank
Visual inspection of the lining showed considerable damage of the refractory lining in some areas, while other areas appeared to be relatively unaffected
Core-drilling was used to collect samples from eight different bricks in the lining including samples from test bricks of threealternate refractories
Examination also showed severe thinning in some sections of the cooled support ring
16
Cross-Sections Of The Core-Drilled Samples Removed In January 2004 Showed Cracking And Discoloration
Fusion-cast magnesia-alumina refractory
Bonded magnesia-alumina refractory(outlined at left)
Fusion-cast alumina refractory
Alternate fusion-cast alumina refractory
Microprobe examinations showed extensive sodium penetration in the alumina samples
17
In September 2004, A Fusion-Cast Spinel Lining Was Installed And 40 Strain Gauges Were Mounted On The Vessel Shell
Strain gauges are installed on five levels of the gasifier vessel
Strain gauges replace some previously installed by Weyerhaeuser at different locations
Two strain gauges and a thermocouple are located in four positions around the circumference on each of the five levels
L1
L2
L3
L4
L5
18
During The First 7+ Months Of Operation, Strain On The Shell Increased At A Fairly Low Rate
Hoop and Axial 5-Day Averages for Levels 3-4 New Bern Gasifier Oct 2004 - May 25, 2005
-200
0
200
400
600
800
100015
-Oct
20-O
ct25
-Oct
30-O
ct4-
Nov
9-N
ov14
-Nov
19-N
ov24
-Nov
29-N
ov4-
Dec
9-D
ec14
-Dec
19-D
ec24
-Dec
29-D
ec3-
Jan
8-Ja
n13
-Jan
18-J
an23
-Jan
28-J
an2-
Feb
7-Fe
b12
-Feb
17-F
eb22
-Feb
27-F
eb4-
Mar
9-M
ar14
-Mar
19-M
ar24
-Mar
29-M
ar3-
Apr
8-A
pr13
-Apr
18-A
pr23
-Apr
28-A
pr3-
May
8-M
ay13
-May
18-M
ay23
-May
stra
in
Ave Hoop Ave Axial w revision Linear (Ave Hoop) Linear (Ave Axial w revision)
19
Strain Showed A Perturbation After The Lining Was Partially Quenched In Water; Hoop Resumed Linear Increase
Hoop and Axial 5-Day Averages for Levels 3-4 New Bern Gasifier Oct 2004 - June 30, 2006
-200
0
200
400
600
800
1000
15-O
ct25
-Oct
4-N
ov14
-Nov
24-N
ov4-
Dec
14-D
ec24
-Dec
3-Ja
n13
-Jan
23-J
an2-
Feb
12-F
eb22
-Feb
4-M
ar14
-Mar
24-M
ar3-
Apr
13-A
pr23
-Apr
3-M
ay13
-May
23-M
ay2-
Jun
12-J
un22
-Jun
2-Ju
l12
-Jul
22-J
ul1-
Aug
11-A
ug21
-Aug
31-A
ug10
-Sep
20-S
ep30
-Sep
10-O
ct20
-Oct
30-O
ct9-
Nov
19-N
ov29
-Nov
9-D
ec19
-Dec
29-D
ec8-
Jan
18-J
an28
-Jan
7-Fe
b17
-Feb
27-F
eb9-
Mar
19-M
ar29
-Mar
8-Ap
r18
-Apr
28-A
pr8-
May
18-M
ay28
-May
7-Ju
n17
-Jun
27-J
un
stra
in
Axial 0ct '04 - Jul '05 Hoop 0ct '04 - Jul '05 Axial Aug '05 - June '06
Hoop Aug '05 - June '06 Linear (Axial 0ct '04 - Jul '05) Linear (Hoop 0ct '04 - Jul '05)
Linear (Axial Aug '05 - June '06) Linear (Hoop Aug '05 - June '06)
20
An Explanation Was Needed ForThe Increasing Strain Of The Shell
The fusion cast spinel refractory did not appear to be undergoing extensive reaction or volume change
Inspections of the foam lining showed it was being crushed by the refractory
These observations led to a question about the integrity of the back-up lining
In order to assess the condition of the back-up lining, a core-drilled sample was taken by drilling through the hot-face lining into the back-up lining
21
Only A Portion Of The Back-Up Lining Was Collected, But This Sample Showed Extensive Degradation On The Hotter Side
The sample was visibly degraded, and X-ray diffraction studies showed extensive reaction with components of the smelt suggesting the back-up lining likely made a
significant contribution to the strain on the gasifier shell
She
ll si
de
Hot
sid
e
22
The Observed Degradation Of The Back-up Lining Led To A Concentrated Effort To Find Alternate Refractories
At the urging of project participants, a number of high mullite content materials were tested
Results of tests conducted previously were reviewed, and vendors were sought for some of the promising materials
A company specializing in calcia-alumina refractories for the aluminum industry was found, and special compositions more suitable for smelt resistance were formulated and tested
Samples of magnesia-rich refractories from several manufacturers were obtained and tested
23
The Suggested Mullite Refractories Reacted Extensively, And In Some Cases, Completely, With Molten Smelt
Beforeexposure
Afterexposure
24
Formulations Of The Calcia-Alumina Refractories Showed Very Good Resistance To Molten Smelt at 900°C
A sample of an alkaline aluminate is shown in the badly reacted metal holder. This refractory will be installed during the next lining replacement.
25
Two Magnesia-Rich Refractories Have Demonstrated Good Resistance To Molten Smelt At 900°C
Magnesia-rich refractories after 100 h in molten smelt at 900°C
Further studies are planned
26
Summary
Degradation of the refractory linings has been attributed to reaction of the refractories with sodium compounds in the smelt and particularly with Na2O
Experience and laboratory studies have shown that a fusion-cast magnesia-alumina spinel refractory has very good resistance to molten smelt at 1000°C
Degradation of the back-up refractory lining appears to be a significant contributor to the stresses on the gasifier shell, but studies have found two refractory types with better resistance to molten smelt at 900°C
The refractory lining to be installed in October will employ therecommended materials – fusion cast magnesia-alumina spinelfor the “hot-face” lining and calcia-alumina refractory for the “back-up” lining