Combustion Performance and Emissions Optimization through ...

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Combustion Performance and Emissions Optimization through Integration of Miniaturized High-Temperature Multi- Process Monitoring System Award No. DE-FE0031680 May 20, 2021 2021 Spring Project Review

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Combustion Performance and Emissions Optimization through Integration of Miniaturized High-Temperature Multi-Process Monitoring System

Award No. DE-FE0031680May 20, 2021

2021 Spring Project Review

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DisclaimerThis report was prepared as an account of work sponsored by an agency of the United States

Government. Neither the United States Government nor any agency thereof, nor any of their

employees, makes any warranty, express or implied, or assumes any legal liability or responsibility for

the accuracy, completeness, or usefulness of any information, apparatus, product, or process disclosed,

or represents that its use would not infringe privately owned rights. Reference herein to any specific

commercial product, process, or service by trade name, trademark, manufacturer, or otherwise does not

necessarily constitute or imply its endorsement, recommendation, or favoring by the United States

Government or any agency thereof. The views and opinions of authors expressed herein do not

necessarily state or reflect those of the United States Government or any agency thereof.

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No proprietary information is included in this presentation

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Agenda

▪ Project Overview

▪ Technical Discussion• R&D in Pilot-scale Testing Facility

• Demonstration at Leland Olds Station

• Summary

▪ Plan

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Reaction Engineering International

▪ Founded 1990 with Strong University and Specialist Affiliations

▪ Managed more than 40 government R&D projects in the past 15 years

▪ Has both management experience and technical expertise in the combustion and gasification related R&D programs

▪ Expertise• Combustion, Gasification, Fuel Conversion & Pollutant

Emissions• Unique, Proprietary Modeling Capabilities & Tools• Laboratory and Field Testing• Specialized Equipment & Controls

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Project Objectives

▪ Develop and demonstrate a miniaturized high temperature multi-process* monitoring system (mMPMS) that can provide a real-time indication of boiler condition in a lignite-fired full-scale boiler

▪ Develop and implement logic algorithms for the plant DCS to improve boiler energy efficiency, soot blowing, and NOx emissions by automated control of boiler operations

6mMPMS

*metal wastage, heat flux, metal surface temperature, ash deposit thickness and ash deposition rate

Conceptual Schematic of Boiler Condition Monitoring using mMPMS

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Technical Approach

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Modeling

400

600

800

1000

1200

0 0.2 0.4 0.6 0.8 1

Tem

pera

ture

, ̊F

Deposit Thickness, mm

Impacts of Deposit Thickness

on Metal Temperature

Tsensor Twall

Lab-scale Development

Pilot-scale studies

Full-scale demonstration

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Leveraging REI’s Previous Works▪ Electrochemical metal wastage sensing

system has been applied to• low and high temperature zones of the boiler• waste-to-energy system• material testing for ultra-supercritical steam

condition and oxy-firing combustion

▪ EN-based system provides high sensitivity, real-time, on-line monitoring technology

Lab Pilot Full

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Project Team

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Prime Recipient

Sub-Awardees

Pilot-scale Testing Full-scale Demonstration

• Project Management• mMPMS Development• Mechanism Derivation• Computational Modeling• Signal Conditioning and Data

Communication Module Development

Bill Smith Engineering, LLC

Boiler Control Logic

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Project Schedule

Year 1Oct 2018 – Sep 2019

Design and construction of prototype sensor body

Design and fabrication of data processing unit

CFD analysis of full-scale lignite coal-fired boiler

Year 2Oct 2019 – Sep 2020

Construction of power and cooling unit

Development of data processing software for lignite fired unit

Test and validation of multi-process sensor in a lignite firing

pilot-scale combustor

CFD analysis of demonstration site’s full-scale lignite-fired boiler

Demonstration of multi-process sensor in a commercial scale

lignite coal-fired boiler

Year 3Oct 2020 – Sep 2021

Control logic development and implementation for automated

control

• Pilot-scale testing delayed due to the COVID-19 pandemic and the following facility shutdown has been completed in July 2020

• The full-scale demonstration has started in February 2021

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mMPMS Design Concept

▪ Existing sensor placed in air-cooled probe

▪ Requires access port where tubes have been bent to allow access

▪ Need cooling air arrangement including cooling valve

▪ Use the gap in the membrane for sensor insertion

▪ Sensor embedded in body with heat management module “without” cooling air

▪ Multi-process measurements to help condition-based monitoring

▪ Requires only 110 V power to data processing unit (with active cooling)

Legacy Sensor System mMPMS

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miniaturized Multi-Process Monitoring System

Data Processing UnitEmbedded SoftwareWireless CommunicationActive Cooling

Sensor Assemblyminiaturized Multi-Process Electrochemical Sensor

Sensor Body with Heat management system

• Metal wastage rate• Heat flux• Temperature

• Deposition

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Key mMPMS Components

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Sensor Assembly• New ceramics assembled with metal elements• Designed and machined to fit the membrane hole• Designed to reach within ¼” of tube crowns

Sensor Body • Designed for specific waterwall at Hunter plant• Designed to fit the sensor assembly• Based on heat transfer modeling to optimize heat

management

Data Processing Unit• Signal conditioning module• Hardened electronics with cloud-capable

software• Designed using industrial Internet of Things

(IIoT) paradigm• Scalable system to support unlimited sensors• Processing power to enable future support for

machine learning/artificial intelligence• Active Cooling

Signal conditioning module• Updated and improved the existing signal

conditioning module• Simplified electronic design and increased

resolution to allow detection of localized attack

• Implemented full digital signal conditioning• Implemented full digital data communications• Embedded “smart” electronics at board level

(embedded controller)

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Multi-Process Monitoring

▪ Leveraged the legacy metal wastage monitoring capability

▪ Developed quantitative heat flux and deposition correlation based on sensor signal

▪ Tested and validated during pilot-scale testing

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Electrochemical Noise and Temperature Measurements

Reference Temperature

Ash Deposit Surface Temperature

Deposit Thickness

Corrosion Rate, Deposition Rate, Temperature, Heat Flux

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Remote Access & Data Communication

On-site Computer Off-site Computer

Remote Desktop

Internet

Based on discussion with plant• No connection to plant

distributed control system (DCS) allowed

• All sensors wired to on-site computer through switchbox

• On-site computer connected to independent network

• Remote desktop software to connect to on-site computer

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R&D on Pilot-scale Testing Facility

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Pilot-scale Testing @ University of Utah

▪ Pilot-scale testing in 100 kW down-fired combustor at University of Utah (UoU) in Salt Lake City, Utah

▪ 4 different fuels

• Lignite*

• PRB (UoU has in storage)

• Bituminous – Illinois 6

• Wood

▪ Increased workscope includes Mg(OH)2

• Commonly added for deposition/slagging control

• Utilize pilot data to improve model deposit properties for plants that use additive

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Ash Deposition Correlation Development

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Reference Temperature Calculation

Deposits Surface Temperature Calculation

Deposits Thermal Resistance Calculation

Deposits Thermal Conductivity Calculation

Deposits Thickness Calculation

=Measured

Mass ?

Guess: Deposits Porosity

N

Y

Deposits Mass Calculation

Additional Verification by Measured Thickness

(element thermal conductivity)R

easo

nab

le?

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Measured and Calculated Deposits Thickness

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0

0.1

0.2

0.3

0.4

0.5

0.6

0 10 20 30 40

De

po

sits

Th

ickn

ess

(m

m)

All Deposits Samples

0

0.1

0.2

0.3

0.4

0.5

0.6

0 10 20 30 40

De

po

sits

Th

ickn

ess

(m

m)

All Deposits Samples

calculated thickness

measured thickness

Illinois 6 PRBLignite Wood

• The calculated deposits thicknesses agree well with the measured deposits thicknesses

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Demonstration at Leland Olds Station

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Basin Electric Power Coop (Demonstration)

▪ Located near Stanton, North Dakota

▪ Two lignite-fired units with total generating capacity 669 MW

• Unit 1 – 222 MW opposed wall-fired PC (demonstration plant)

• Unit 2 – 447 MW opposed wall-fired cyclone20

Leland Olds Station

Plant is interested in ash management and boiler tuning

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Demonstration Plan

Mounting hardware installation during Outage

•Support pipe

•Cutting the hole in the webbing

Pre-demonstration site visit

•After mounting hardware installation

•Site preparation check list (Equipment, Desired operating conditions…)

5-week Demonstration

•5-week monitoring

•Targets Feb 2021 –March 2021

•Monitoring continued

Data Analysis & Control Logic Development

•Focus of Year 3

•Plant and sensor data review

•Boiler operation logic including soot blower operation

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Sensor Locations

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▪ Placement of 3 side wall sensors guided by plant experience

• High deposition and moderate wastage rates

• One sensor on Left wall just above windbox

• 2 sensors slightly above OFA – 1 each on left and right wall

▪ Placement of 2 additional sensors on the front wall based on model predictions

• Regions of shifting deposit pattern at different loads

• Alternating reducing/oxidizing environment when cycling

#1

#2#3

#4#5

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System Installation

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Sensor #1

Sensor #2

Sensor #3

Sensor #4

Sensor #5

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Soot Blower and Sensor Layout

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xSensor #1

xSensor #2

x

Sensor #4 Sensor #5

x x

Sensor #3

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Real Time Data: Deposition ThicknessSensor #1, 3:00 Feb 27 – 15:00 Mar 1

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Dep

osi

tio

n T

hic

knes

s (m

)Lo

ad (

MW

)

Full Load Full LoadLow LoadTransition

• The peaks in deposition thickness reflect the operation of the IR type soot blowers near the sensor (the frequency is about once per hour)

• The white bottom line represents a clean condition (~ 0 mm thickness) of the sensor after soot blowing

Tref = 1407 K

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Real Time Data: Deposition Thickness - CalibratedSensor #1, 3:00 Feb 27 – 15:00 Mar 1

It is more reasonable to compare the deposits thickness between various loads after calibration

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xSensor #1

Test 1: Testing Proceduresensor #1, 9:00 to 15:00, March 3, 2021, full load

• The periodic increase-decrease of the real time deposits thickness is truly an interaction between the sensor and the soot blowers

• The reported absolute value of the real time deposits thickness is reasonable

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Test 1: Real Time Behavior sensor #1, 9:00 to 15:00, March 3, 2021, full load

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sensorinserted

IR37 in operation

minor impaction from the operation of

the far away soot blower

sensorretraction(~8mm)

sensorinsertion

IR8, IR9, IR22, IR23, WB3, WB5

back in operation

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Test 1: Deposits Thickness Validationsensor #1, 13:00, March 3, 2021, full load

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~2-3mm

~6mm

membraneThickness ¼”

Sensor reported value is about 8mm

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Test 1: Real Time Behavior sensor #1, 9:00 to 15:00, March 3, 2021, full load

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sensorinserted

IR37 in operation

minor impaction from the operation of

the far away soot blower

sensorretraction(~8mm)

sensorinsertion

IR8, IR9, IR22, IR23, WB3, WB5

back in operation

before soot blowing

after sootblowing

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Test 2: Real Time Behavior sensor #1, 9am to 15:00, March 2, 2021

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Dep

osi

tio

n T

hic

knes

s (m

)Lo

ad (

MW

)

soot blowing

sensorretraction

sensorretraction

before soot blowing

after soot blowing

soot blowing

sensorinsertion

soot blowing

decreased by about half

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Test 3: Real Time Behavior sensor #2, 12am to 15:00, March 3, 2021

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Dep

osi

tio

n T

hic

knes

s (m

)Lo

ad (

MW

) Sensor is relatively clean, which is consistent with the data

sensorretraction

sensorinsertion

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Real Time Data: Deposition ThicknessSensor #4 & 5, 3:00 Feb 27 – 15:00 Mar 1

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Dep

osi

tio

n T

hic

knes

s (m

)Lo

ad (

MW

)

Full Load Full LoadLow LoadTransition

No need to blow No need to blow

6pm 6amNo need to blowFine to blow

Dep

osi

tio

n T

hic

knes

s (m

) Fine to blow Fine to blowFine to blowNo need to blow

Sensor #4

Sensor #5

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Real Time Data: TemperatureSensor #1, 3:00 Feb 27 – 15:00 Mar 1

34Sensor surface temperature is consistent with the low change

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Real Time Data: Heat FluxSensor #1, 3:00 Feb 27 – 15:00 Mar 1

35Heat flux is consistent with the low change

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Summary

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▪ Successful upgrade of REI’s legacy corrosion monitoring system• Miniaturization and modification of the sensors accommodating membrane installation and passive

cooling

• Development of new signal conditioning module with improved data communication and resolution

• Legacy data acquisition hardware successfully replaced with easily maintainable and scalable electronics

• Development of new big data platform for collection and analysis

▪ Five miniaturized MPMS (i.e. mMPMS) sensors and associated control boxes were successfullyinstalled through the membrane walls in LOS1

▪ Sensor deposition and corrosion data were collected during a 5-week testing campaign

▪ Pilot scale testing (University of Utah) verified reliability of new electronics, and provided for thedevelopment of a correlation for lignite-based deposit thickness

▪ LOS1 tests have confirmed that the sensors are very sensitive to the surroundings includingoperation of soot blowers and water lances (i.e. deposit growth) and impacts of boiler ramping(i.e. corrosion)

▪ Tests demonstrate that the mMPMS deposition measurements are qualitatively and quantitativelyreliable

▪ Tests show that corrosion rates at the 5 sensor locations are generally very low except for spikesduring load ramps

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Plan

▪ Data analysis and control logic development will continue for the rest of the Year 3 in this project

▪ Presenting results at the following conferences:

• Clearwater Clean Energy Conference, June 20-24, 2021

• The Thirty-Eighth Annual Pittsburgh Coal Conference, September 20-23, 2021

• AFRC 2021 Industrial Combustion Symposium, October 10-13, 2021

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Acknowledgements

▪ U.S. Department of Energy - National Energy Technology Laboratory (DOE/NETL) through DOE Cooperative Agreement No. DE-FE0031680

▪ DOE/NETL Project Manager: Mr. Omer Bakshi

▪ Thank you to Basin Electric headquarters and the LOS personnel for their support of this project

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