Class Presentation MBO
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Transcript of Class Presentation MBO
1. Process Improvement in ABC Ltd2. Implementation of 5S in Ware-house
GROUP
1.035– Yogeshwar Kulkarni
2.055 – Amit Sethia
3.018 – Ajitsingh Dubal
4.062 –Shashank Singh
5.042 – Amit S Pandey
6.058 –Parvez Shaikh
Mentor: Dr P. N. Mukherjee
Managing Business Operations
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Assembly of Pinion to the High Speed Motor Application of Motor
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1.Process Over View
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Process Overview-Current Scenario and Improvement Desired
Current Scenario Station cycle time was 18 seconds (including Inspection)
100% inspection as height is critical to quality.-Non Value Add
First Pass Yield below 70%- High Rejection/Rework Rate
Returned Motor Analysis (100nos /1000 dispatched quantity) had shown assemblies deviated upto 1mm in height.- Operator Dependability & Customer Dissatisfaction
Improvement Desired-Reduction of Wastages (MUDA) To imbibe in the people the need to improve the current system.
To reduce inventory by reducing the factor of rejection in the motor assembly.
Reduction of Cycle Time( processing Time) per Assembly.
Reduction of paper work by doing sampling inspection in place of 100% inspection
Reduction of Inspection cycle. To move from QC to QA-Non Value Add
Reduction of wastages. High Rejection/Rework Rate
Reduction in Customer Rejection level which is 10% at the moment.- Operator Dependability & Customer Dissatisfaction
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Process Improvement- Need
Problem Identification,Root Cause AnalysisProcess Review.
Implementation on a pilot scale
SPC study
Implement the change, Horizontal Deployment
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PLAN – Problem Identification
Process Improvement- Use Fish Bone Analysis tool Construct Cause & Effect Diagram•Agree on a problem statement (Effect). Write it at the center right of the flipchart or whiteboard. Draw a box around it and draw a horizontal arrow running to it.•Brainstorm the major categories of causes of the problem which are listed as below :
MethodsMachines (equipment)People (manpower)MaterialsMeasurementEnvironment
•Write the categories of causes as branches from the main arrow.•Brainstorm all the possible causes of the problem. Ask: “Why does this happen?” As each idea is given, the facilitator writes it as a branch from the appropriate category. Causes can be written in several places if they relate to several categories.•Again ask “why does this happen?” about each cause. Write sub–causes branching off the causes. Continue to ask “Why?” and generate deeper levels of causes. Layers of branches indicate causal relationships.•When the group runs out of ideas, focus attention to places on the chart where ideas are few.
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Plan- Root Cause Analysis
Fish-Bone Diagram
Height Out of Spec
Man Machine
Material Method Environment
Operator doesn’t know operation
Unable to Measure
Inconsistent while operating
Bought out -Pinion Height out of Spec
Bought out – Cup Plate Out of Spec
Motor Assembly Out Spec from previous operation
Process Inconsistency
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Plan- Process Review
Outcomes of Fish Bone analysis
Material – Within Tolerance
Machine- No Inconsistency
Man- Skill require to measure the component during entire production lot. May lead to inspection error. Reactive Measures
Method- Assembly process creating variation in the readings . Error Originator
Conclusion: Change the method of Assembly of Pinion to the motor.
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Do-Old Process of Assembly
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Do-New Process of Assembly
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Check- New Process Capability Study
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Act- After verification of Results of New Process
Results
As Pp & Ppk values are almost = 2; only 3.4 Parts per Million are expected to be defective. Hence process yield has improved from 70 % to 99.99966%.
This has reduced rework cost.
No 100% measurement. Only set-up approval measurement (first 5 pieces before start of production)
No Operator dependability.
Increased Customer Confidence Level.
Horizontal Deployment
ACT: Implement the new process of Assembly of Pinion to the motor.
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Implementation of 5S in the Warehouse of XXX Ltd
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2. WareHouse-Old (Before Implementation of 5S)
Seiri-Orderliness Kitting Time = 140 Minutes/ Motor Model
Seiso- Clarity Quantity Mismatch (ERP Vs Actual)= 48%Inventory Measurement Cycle = 7 daysNo. operator for kitting = 5
Seiton-Tidiness Damaged due to improper storage = 20%
Seiketsu-Cleaniness Warehouse was quite disaarayed and lacked cleaniness.
Shitsuke-Sustain No discipline at warehouse.
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Ware House- After Implementing 5s
Seiri-Orderliness Kitting Time reduced to 30 Minutes/ Motor ModelSeiso- Clarity Quantity Mismatch reduced to 4% only
Inventory Measurement Cycle reduced to 3 from 7 daysNo. operator for kitting reduced to 2 from 5
Seiton-Tidiness Material Damaged Cost reduced to 0% almostSeiketsu-Cleaniness Warehouse looks clean and organised with the same
allocation of resources to clean.
Shitsuke-Sustain Strict discipline in the ware house
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Ware House- After Implementing 5s
Advantages Particulars
Traceability Increased substantially which has resulted in decrease in manhours and thus savings for the company.
Clarity Mismatch in reporting has reduced which has helped the organisation to reduce inventory pile up because of false reporting of inventory.
Inventory Damage There is no damage of Inventory as each ite is located in a organised manner and as per the logic.
Labour Hours Saving
As there is no confusion in the warehouse operations there is less need of manhours to maintain the warehouse. The cost of labour has reduced by 60%.
Productivity There is substantial increase in productivity of the warehouse department. The Inventory physical verification has reduced to 3 days which was 7 days earlier.
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