Cementing a Long Horizontal Wellbore Using CT Squeeze Technology

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    Copyright 2005, Society of Petroleum Engineers Inc.

    This paper was prepared for presentation at the 2005 SPE/ICoTA Coiled Tubing Conferenceand Exhibition held in The Woodlands, Texas, U.S.A., 12 – 13 April 2005.

    This paper was selected for presentation by an SPE Program Committee following review ofinformation contained in a proposal submitted by the author(s). Contents of the paper, aspresented, have not been reviewed by the Society of Petroleum Engineers and are subject tocorrection by the author(s). The material, as presented, does not necessarily reflect anyposition of the Society of Petroleum Engineers, its officers, or members. Papers presented atSPE meetings are subject to publication review by Editorial Committees of the Society ofPetroleum Engineers. Electronic reproduction, distribution, or storage of any part of this paper

    for commercial purposes without the written consent of the Society of Petroleum Engineers isprohibited. Permission to reproduce in print is restricted to a proposal of not more than 300words; illustrations may not be copied. The proposal must contain conspicuousacknowledgment of where and by whom the paper was presented. Write Librarian, SPE, P.O.Box 833836, Richardson, TX 75083-3836, U.S.A., fax 01-972-952-9435.

    AbstractCoiled Tubing (CT) cementing has been widely used and

    highly successful for remedial squeeze and plug back

    operations for over 20 year’s1,2,3. However, the vast majority

    of these wells were at deviations less than 90 degrees.

    A long horizontal well in the Alpine field on the North

    Slope of Alaska was drilled early in the development phase

    and was out of pattern (Fig. 1). The well required a plug back

    and sidetracking to maintain desired off-take strategy (Fig. 2).

    The well was drilled to a total depth of 11,984 feet and

    completed with approximately 2,050 feet of 4-1/2” slottedliner inside the 2,210’ of 6-1/8” hole. Near the middle of the

    horizontal section, the well’s deviation climbed to a maximum

    of 96 degrees.

    Cementing operations have long been recognized as a

     problem in horizontal wells. However, a search of the SPE

    online library identified only 5 papers that mentioned the

    challenge we faced while a search of “horizontal” yielded

    5,534 hits. Although the 5 papers did discuss the problem and

    gave some general guidance to cement design consideration,

    there was little specific information on the “best practice”

    approach to Plug and Abandon (P&A) long horizontal

    wellbores.

    Based on the successful CT squeeze program in Alaska, a

    team of engineers and field supervisors decided to use CT

    cement squeeze technology to seal the lateral portion of the

    wellbore and leave a cement base for subsequent sidetracking

    operations. This paper will discuss the details of this job

    including:

    1.  Job Planning2.  Cement design and testing3.  Tools and Equipment4.  Wellbore geometry and Placement details5.  Onsite Job Execution details6.  Results7.  Lessons learned

    Field OverviewThe operator, ConocoPhillips Alaska Inc., and partners in

    1994 discovered the Alpine field. The Alpine field is located

    in the Colville River Delta a few miles south of the Arctic

    Ocean and approximately 70 miles west of the Trans Alaska

    Pipeline. The facilities are connected to the North Slope road

    system via ice road for approximately three months of the

    year. Aircraft provide the only mode of transportation at othe

    times. Produced crude is transported to the Trans Alaska

    Pipeline via the East-West running Alpine and Kuparuk

    common carrier pipelines.

    The reservoir was under-saturated at discovery with a gas

    oil ratio of about 850 SCF/Bbl. The produced oil gravity

    currently averages 39°  API. As a result of the depositiona

    environment and minor fault offset, excellent vertica

     permeability is observed and the productive sands are pressure

    connected across large distances. A “water alternating

    miscible gas” flood is being conducted in the Alpine reservoir

    The field is developed with line drive patterns, utilizing

    horizontal producers and injectors in a one to one ratio (Fig

    2).

    Given the high mechanical strength of the clean fine-

    grained Alpine sandstones, the operator elected to leave thehorizontal sections on the wellbore uncased, to minimize the

    chance of formation damage. A 7.0” intermediate casing shoe

    is set just below the top of the producing formations at high

    angle. The uncased horizontal production hole typically

    extends 3000-4000 feet beyond the intermediate casing shoe

    Production and injection tubing is primarily 4.5” although

    some lower rate wells are completed with 3.5” tubing. A

     production or injection packer is located a few hundred

    measured feet above the casing shoe. A typical Alpine wel

    completion is shown in Figure 3.

    While performing above expectations, this completion

     practice has proven to be a difficult environment to access

    Early attempts at logging these wells using CT memory toolsand conductor line tractors provided less than ideal results in

    reaching the TD in the extended horizontal open-hole sections

    Drilling and formation debris and abrasive formations in

    combination with wellbore geometry limited our ability to

    reach the full measured depth of the lateral sections. Portions

    of open-hole lateral sections with fill or debris is not the only

     potential challenge to successfully cementing these wells

    recent caliper logs suggest that the wells may also have

    sections that are washed-out or significantly out of gauge.

    Although the final field development plan called for long

    open-hole lateral wellbores with injection and producing wells

    in a line drive configuration, there were a few early

    SPE 94039

    Cementing a Long Horizontal Wellbore Using CT Squeeze TechnologyW. Rauchenstein and C.G. Blount, SPE, ConocoPhillips Alaska Inc.

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    2 SPE 94039

    development wells drilled that did not fit the final offtake line-

    drive strategy. The subject of this paper is the P&A of Well B

    in preparation for a sidetrack to put the well in pattern.

    Wellbore Completion and Geometry DetailsWell B was drilled early in the development of the Alpine

    development. This well did not conform to the final line drive

     production strategy for Alpine field. A P&A proposal wasconsidered to allow sidetracking of Well B to put this well in

    conformance with the rest of the Alpine development (Fig. 4).

    The original completion of Well B included:

    •  16” Conductor set at 109’ TVD/MD and cemented tosurface

    •  9-5/8” 40# L-80 Surface Casing set to 3,326’MD/3120’ TVD and cemented to surface

    •  7” 26# L-80 Production Casing set to 9,775’MD/7,200’ TVD

    •  6-1/8” Open Hole from 9,775’ MD to 11,984’ MDLined with a 4-1/2” 12.6# L-80 Production Slotted

    Liner from 9,590 to 11, 643’ MD/+-7,133’ TVD, no

    cement.•  4-1/2” 12.6# L-80 Production Tubing from surface to

    8,777’ MD/7,031’ TVD with SSSV nipple, side-

     pocket GLM’s, landing nipples, production packer,

    and tailpipe with entry guide.

    The schematic of the subject Well B is shown in Figure 5.

    The geometry getting down to the horizontal completion is

    shown in Figure 6.

    Pre-Job PlanningPreparations for this program started with a meeting to

    compare options to P&A the well in preparation for a

    sidetrack to normalize the well to field pattern. P&A options

    included:

    1.  Full-bore cementing the entire wellbore2.  Cementing through a retainer in the top of the liner3.  Setting a mechanical whipstock at the desired

    sidetrack location and down-squeezing cement

    4.  Performing a CT placed liner-top cement down-squeeze

    5.  Performing a bottom up cement squeeze using the CTsqueeze procedure commonly performed in more

    conventional wells in Alaska.

    During the meeting, the participants determined that one

    important goal of the job was to ensure that the original

    wellbore was not left as an underground conduit for injected

    or produced fluids that could affect sweep pattern efficiency.

    A literature search to help offer additional guidance provedof little use providing only 5 papers generally addressing

    horizontal cementing operations. The majority of these papers

    discussed the cement properties for horizontal wells and

     primary cement job considerations; none specifically

    addressing the operational challenges of this horizontal P&A

    squeeze job.

    Review of various other jobs performed in Alaska yielded

    some useful data points including a high angle CT squeeze on

    a 21,100’ well, and some work on performing a “chemical

     packer” job in another horizontal well4. This “chemical

     packer” refers to a thixotropic cement system designed to form

    discrete plugs of cement when pumped into horizontal

    wellbores.

    The more conventional approach of laying the cement

    from the deepest measured depth attainable in the wellbore

    was chosen for this well. The most compelling reason for this

    approach was due to the need to do the best job possible in

    hydraulically isolating the original wellbore to help assure

    conformance with the injection and offtake pattern strategyThe chance of leaving a 2,200’ high permeability channel was

    not tenable in this particular circumstance. One comforting

    aspect of using a more conventional approach was the sheer

    number of CT squeeze jobs performed on the North Slope

    numbering well over 1,000 operations over the last 20 years.

    The plan involved:

    1.  Running the cement nozzle to 11,570’ CTMD(staying in the slotted liner that was 341’ MD from

    the end of the openhole section, and above the pack

    off bushing near the bottom of the liner)

    2.  Liquid packing the wellbore, bottoms up3.  Laying in the cement while pulling up hole at abou

    a 1-1 volumetric ratio following spotting of 15 Bbls

    of cement near TD

    4.  Pulling up hole to a depth where the deviation wasless than 45 degrees so the cement top area would be

    more manageable

    5.  Hesitate squeezing by pumping fluid above thecement top to help displace any wellbore fluid

     pockets in the horizontal section back into the

    formation and filling the voids with cement

    6.  Running in hole and washing excess cement abovethe desired sidetrack depth

    7.  Pulling out of the hole washing all nipples and jewelry

    This bottoms-up approach brought with it numerous

    challenges. Reaching TD was not certain based on previousopen-hole experience in other Alpine wells. However, CT

    forces modeling suggested that since the well was lined, we

    should be able to reach the shoe of the liner at 11,643’ (341

    shallow of the open hole TD) using a tubing straightener 5  on

    the 1.75” OD tapered CT string.

    Another concern was the possibility of becoming stuck

    while spotting the dense cement. Numerous open hole and

    even conventional cement squeeze jobs have proven how

    effective the viscous and dense cement can be in moving

    wellbore debris and occasionally bridging and sticking the CT

    Early field operations by Arco and BP in cementing other

    high-angle wells experienced problems in the heel area where

    the low viscous fluids mixed with the cement and droppeddebris that had been carried up in the cement. To furthe

    exacerbate the concern, historical trends have shown tha

    formation spalling and cuttings are not uncommon in Alpine

    wellbores6. The fact that this wellbore contained a slotted

    liner (1/4” slots) helped alleviate some of these concerns.

    In addition to determining the type of P&A, the nature of

    the isolated Alpine field and the time of year –no ice road at

    the time- precluded bringing in additional equipmen

    commonly used in Prudhoe Bay and Kuparuk CT squeeze

    operations. Alpine does not have a year-round road

    connection to the well-established oilfield infrastructure

    available to other North Slope fields. The only time large

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    equipment can be brought-in is during the three winter months

    when the ice roads are available. Any large items that cannot

     be transported by medium sized DC-6 or “Herc” aircraft,

    including CT and cementing equipment, must be staged in the

    field during the ice season.

    The only equipment available to mix and pump the cement

    was an Arctic Drilling Rig –located at the extreme distal end

    of the pad from the well to be P&A’d- some 600’ away (Fig7). The available onsite equipment options did not include a

    conventional batch mixer, commonly preferred to help ensure

    cement quality for CT cementing jobs in Alaska.

    Cement DesignA slow setting, low fluid-loss latex blend cement system was

    chosen given the wellbore geometry and condition, required

     placement and squeeze techniques, and necessity of attaining

    the best hydraulic seal possible. The class G cement was

    designed to 15.8 ppg in fresh water with .4% BWOC TIC

    dispersant D065, .2% BWOC mid temperature retarder D800,

    .2 gal/sk antifoam D047, and 2.0 gal/sk liquid latex D600G.

    The Pv was measured at 32.2 cP at 81 deg F and 68.2 cP at

    140 deg F. The Ty was 4.2 lbf/100ft2 at 81 deg F and 7.0 at

    140 deg F. The Fann 35 rehology numbers of the cement

    system are shown in Table 1.

    The thickening time of the cement system was increased

    from the traditional 3-8 hours to 8-10 hours at static bottom

    hole temperature of 160°  F (beginning with 80°  F mix

    temperature raised to 160°  F BHCT in 44 minutes) to allow

    trouble time should problems develop when laying in the

    cement through approximately 4,500’ of the wellbore

    including the horizontal section. The chance of rubble and

    debris sticking the CT was still of concern while pumping the

    cement job.

    A low fluid loss cement blend was selected to minimize

    the chance of prematurely bridging off localized areas thatmay take more fluid. The squeeze design called for an API

    fluid loss of approximately 15 mL in 30 minutes (blend tested

    at 14 mL). Since there was no plan to washout excess cement

    through the liner and considering the fact that the liner was

    slotted and uncemented, the normal requirement of developing

    adequate node height was not a concern.

    The cement’s API free water tested as close to 0% as

    measurable.

    The high latex content provided for the best possible

    cement bond, helped lower the fluid loss, and provided for a

    robust and resilient kick-off plug7.

    All needed cement additives were flown in from the

    service company base. The cement additives were mixed intothe mix-water and stored in a Vac truck the night before the

     job to allow ample time for hydration.

    Tools, Equipment, and ProcedureThe CT unit for this job was an Arctic Mast CT Unit with

    15,210’ of tapered 1-3/4” coiled tubing. A pipe straighter was

     previously installed on the CT unit to extend the attainable

    reach into the extensive horizontal sections of Alpine

    completions. Other equipment for the job included 3 Fluid

    supply tanks, 4 returns tanks including a 200 Bbl trip tank, 1

    HP cementing pump unit on the nearby drilling rig, 1 HP

     pump on the CT unit, a re-circulating cement mixer, 640’ of

    2” 1502 hard line, a HP dual choke manifold, a HP cementing

    manifold, and 1 HP downstream tank manifold.

    The simple Bottom Hole Assembly (BHA)  for Well B

    consisted of a 1 ¾” cold roll connector for 1 ¾” by .109” wall

    coiled tubing, 1 ¾” dual check valves, 5’ of 1 ¾” extension

     pipe, along with a 1 ¾” combination cement/jet-swirl nozzle

    (Fig. 8). The BHA size was selected to be slick to the CT

    diameter to minimize the chance of debris stacking on a BHAshoulder and sticking the CT. The combination cement/je

    swirl nozzle has been used extensively for CT squeeze work

    on the slope. The ball coverts the nozzle from a large bore

    low differential pressure cement nozzle to a high differentia

     pressure, up-down nozzle shown to effectively wash solids

    and produce a turbulent vortex of fluid above the nozzle to

    help “sweep” solids up-hole (Figs. 9 and 10).

    The cement slurry was mixed “on-the-fly” using the

    drilling rig’s re-circulating cement mixer. The drilling rig’s

    cement pump was used to pump the spacers and cement to the

    CT unit’s high-pressure surface manifold. The CT unit also

    had a pump tied into the surface manifold and was used to

    displace the cement and tail spacer from the CT and for al

    subsequent pumping operations.

    General Procedure and Job DocumentationWith the limited resources available, it was necessary to begin

    the job setup several days in advance. As common with the

     beginning of all new programs, the first several hours were

    set-aside for Sim Ops and safety meetings.

    Following pre-job meetings, two 380 Bbl seawater, and

    one 380 Bbl diesel upright supply tanks were spotted inside a

    secondary containment system -which holds a minimum o

    110% of the capacity of the largest tank. Inspection of the

    tank farm, and approval by the on site supervisor completed

    filling the seawater uprights commenced by tapping into the

    seawater injection header available on the drill site. An onsite tanker then loaded the diesel upright tank with preheated

    diesel (80º F) for freeze-protect fluid.

    While the fluid transfers continued in the background, the

    CT crew, 3 roustabouts, and two cementers commenced

    hammering up the 640’ of 2” 1502 hardline.

    The returns tank farm downstream of the dual choke

    manifold consisted of three 400 Bbl open tops, one 400 Bb

    tiger tank, and one 200 Bbl gauge or “Trip tank”.

    Once the basic equipment was in place, the coiled tubing

    unit was spotted in front of the well and rigged up. After

    raising the derrick, the BOP’s were flanged up to the

    wellhead. The injector head and lubricator was then hoisted

    and the BHA was installed. The BHA consisted of a simple 1¾” cold roll, 1 ¾” dual check valves, 5’ of 1 ¾” spacer pipe

    and a 1 ¾” combination cement/jet swirl nozzle (Fig. 8).

    Following nipple-up completion, all employees

     participated in a safety and environmental walk thru of the

    location. All well control equipment and hardlines were

     pressure tested after the walk thru was completed.

    Radios were the primary communication tool due to the

    extensive distance between the cementing equipment, the

    choke manifold, the tank farms and the CT unit. All radio

    contact was performed with complete voice communication

    rather than abbreviated acknowledgement such as “radio

    clicking” for acknowledgement.

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    The cement pumps were brought on line at minimum rate

    to fill all hardline and coiled tubing while taking returns to the

    returns tank farm through the choke manifold. Once fluid was

    observed through all flow paths and at all return tanks, the

     pumps were shut down and individual components were

     pressure tested following standard operating procedures.

    After successful pressure testing, current wellhead valve

    conditions and all relevant pressures were recorded along withthe number of turns to open the swab valve.

    Preparations for mixing the cement slurry began as the

    coiled tubing operator ran in hole with the pipe straightener

    on. All cement additives were previously premixed into the

    mix water in a Vac truck and allowed to hydrate for about 12

    hours to achieve desired properties in the continuously mixed

    cement slurry.

    Weight checks were performed every 2.500’ Coiled

    Tubing Measured Depth (CTMD), while running in hole. The

     pipe straightener was turned off during weight checks to

    minimize coil life reduction.

    Due to the fact that this particular wellbore had an open

    guide shoe with a 2” pack-off bushing seal bore and 341’ of

    open 6 1/8” hole, the onsite CPAI supervisor chose to not exit

    the liner, and planned on down-squeezing cement to the toe.

    A depth correlation flag was painted on the coiled tubing

    11,570’ CTMD. Once on depth, the bottom up loading

     procedure was started to displace any gas and other wellbore

    fluids from the well. A wellbore liquid packed with known

    fluids would provide a means to monitor the bottom-hole

     pressure by using the CT by production tubing annulus

     pressure. The bottoms-up load job was selected due to the

    long horizontal section and concerns of effectively displacing

    the gas with the more common bullhead loading of

    conventional vertical cement jobs. The CT nozzle was moved

    up and down across the liner noting any weight anomalies,

    while the hole was loaded. Choke backpressure wasmaintained on the wellhead to assure slight overbalance to the

    formation and prevent any gas or oil influx. The cement

    supervisor began weighting up the blend toward the end of the

    loading process.

    Once a full wellbore plus 10% was circulated, cement

     pumping operations were initiated through the long hardline

    section, a Micro Motion meter and into the coiled tubing. Five

     barrels of fresh water spacer was pumped in front of the

    cement to minimize cement seawater mixing. The barrel

    counter was zeroed when the CT Micro Motion meter density

    indicated 11.5 PPG cement @ 68° F just before the full weight

    of 15.7 ppg cement. All subsequent pump volumes were

     based on this zero.The CT unit’s Micro Motion meter indicated the cement

    was a constant 15.7 ppg. The cement mixer’s density

    indicator showed the cement to be closer to 16 ppg. Samples

    were weighed which showed the density running within this

    range. The onsite supervisor elected to keep pumping at that

     blend ratio rather than try adjustment, which may have caused

    density fluctuations in the pumped slurry.

    Pump rates averaged 1.1-1.3 BPM at 1,545 psi coiled

    tubing pressure while holding 367 psi backpressure at the

    choke system when cement pumping began. All returns were

    taken into gauge tanks with 10 Bbl markers for tracking total

    volumes returned. The coiled tubing pressure climbed to

    3,568 psi at 1.3 Bbls/Min while filling the coil volume of 34

    Bbls. The pump rate was lowered to 1 BPM @ 2,328 ps

    coiled tubing pressure as the cement exited the nozzle and

     began to fill the liner from 11,527’ CTMD. From barrel count

    34 to 43, the well head pressure was slowly increased to assist

    in pushing the cement out the bottom of the liner through the

    2” seal bore located at approximately 11,630’ and into the

    openhole toe. At barrel count 44, the wellhead pressure wasslowly lowered back to 500 psi. Pump rate was maintained

     between 1 and 1.3 as constant as possible so minor changes in

     pressure could be seen that may have indicated potentia

     problems. At 50 Bbls pumped, the nozzle was slowly pulled

    up hole at 27 fpm laying in the 15.8 PPG latex cement 1 for 1.

    Proper laying-in cement procedure requires complete

    accountability of returns verses barrels pumped in order to

    ensure the nozzle remains below the cement top. Pulling the

    nozzle out of the top of the cement will contaminate squeeze

    cement. While this horizontal well posed a significantly

    different geometry than normal, the “keep the nozzle in the

    cement” logic was based on expected mixing, and a presumed

    more viscous cement “wave”. The large holes in the nozzle

    should have helped minimize in-situ mixing of cement and

    wellbore fluids. In reality, the nozzle depth may have had

    little effect on the efficiency of displacement while filling the

    horizontal section.

    As the 120 Bbls of 15.8 ppg latex cement count

    approached, the cement crew prepared to displace the cemen

    into the CT with 10 Bbls of fresh water followed by seawater

    The cement tail and CT nozzle depths were closely monitored

    and minor adjustments were made to assure that as the last o

    the cement exited the nozzle as the nozzle depth neared the

    calculated top of cement based on wellbore void volume. The

     pull out of hole rate was increased when approaching the pre-

    calculated worst-case top of cement timing the nozzle

     breakout of cement to the same time as the fresh water spaceexited the nozzle. The top of cement was over 1,000’ MD

    above the top of the formation in a 45° deviation section of the

    wellbore providing a small-area cement top. An illustration o

    the wellbore and relative depths is shown in Figure 11.

    The nozzle was pulled up to ‘safety depth” of

    7,200’CTMD for the duration of the hesitation squeeze period

    Circulation was broken occasionally to prevent freezing pump

    lines and coiled tubing given the negative 34°  F ambien

    temperatures during the job. The CT was also occasionally

    moved to assure that it remained free.

    Wellhead pressure and pumped volumes were closely

    monitored and used to estimate the volume of additiona

    cement that displaced any pockets of wellbore fluid into theformation during the hesitation squeeze. Eight hesitations

    steps were used to increase the final squeeze pressure up to

    1,040 psi shut in wellhead pressure, or about 800 ps

    overbalanced pressure for 40 minutes:Step SIW HP SICTP Vol ume pumped Post WHP Post CTP T ime/mi n Pressure Los

    1 81 113 0.2 200 230 12 130

    2 102 125 0.3 190 272 11 110

    3 70 120 0.3 200 250 10 100

    4 96 146 0.4 300 300 10 130

    5 370 480 0.4 500 500 13 180

    6 262 264 0.8 750 750 15 200

    7 460 560 1 1000 1000 10 310

    8 715 717 1 1040 1068 11 314

    30 min. circulation stage to warm up surface lines maintain 430# WHP. NO LOSSES

    One hour circulation stage to warm all surface lines and allow cement temp to rise. Maintain 70# WH

    Begin contamination proceedures with 2 PPG Biozan holding 500# W HP. NO LOSSES

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    SPE 94039 5

    The cleanout procedure to remove the excess cement

     began immediately following the final squeeze step (Fig. 12).

    The excess cement from estimated depths 8,300’ to 8,880’

    CTMD (7,096 TVD) was diluted with 2 ppg welan polymer

    followed by seawater to circulate the diluted cement out of the

    well and leave the top of cement at the desired depth for the

     planned sidetrack. 8,880 ‘MD was 100’ MD deeper than the

     production tubing tail to assure that the 4-1/2” tubing tail wasnot cemented in place, which would have complicated the

    workover. This cement top TVD at this measured depth was

    also at least 26’ TVD higher than any depth to the measured

    TD of the well. The wellhead pressure was maintained at 500

     psi to assure overbalance and minimize the possibility of

    formation fluids contaminating the cement.

    All jewelry was washed with the swirl nozzle while pulling

    out of the hole to ensure wireline access to GLM’s and

    nipples. Cement returns were seen at close to the expected

     barrel count indicating the cement top was as designed.

    Pumped fluids were managed to leave a diesel freeze protect

    volume from 2,500’, approximate permafrost zone, to surface.

    Wellhead backpressure was adjusted to compensate for the

    reduced hydrostatic head of the diesel. Figure 13  shows a

    graph of various parameters during the job.

    Squeeze ResultsThe target depth for the Top of Cement (TOC) was 8,880’

    corrected depth. Following waiting on cement to cure, the

    conductor line tagged the TOC at 8,885’ corrected depth. This

    measured depth kept the TVD height of cement at least 26’

    higher than the highest point further down the lateral section.

    The combination of TVD height of cement and applied

    wellhead pressure on the wellbore assured that cement did not

    U tube; solid cement should have remained in the entire lateral

    section following the down squeeze.

    Washing the cement slurry down to 8,880’ MD allowedadequate distance below the production tubing to assure that it

    was not cemented into the casing. This depth also provided

    the drilling rig adequate distance to dress off the TOC to

    9,078’ MD in preparation to set the sidetrack whipstock at

    9,078’ MD. A pressure test verified a competent hydraulic

    seal. During the workover, the drilling rig encountered good

    hard cement drilling, set a whipstock, kicked off 30 degrees

    right of high side and recompleted the well in line with the rest

    of the field.

    Conclusions and Lessons LearnedEven with the challenges and departures from conventional

    CT squeeze techniques, the cement job was performed withoutsignificant problems. Available information suggests that all

     program goals were met.

    Factors that contributed to the success of this work

    include:

    1.  Extensive pre job planning and contingencyidentification

    2.  Workforce familiar with CT squeeze procedures3.  Knowledge and familiarity of cement slurry designs4.  On site and laboratory cement testing5.  A thorough record of the wellbore geometry to

    understand critical depths and hydraulics forces

    6.  Good CT depth correlation to assure leaving adequatevertical column of the cement while keeping below the

    top of 4-1/2” production tubing

    Lessons learned –or more accurately stated, relearned-

    during this job include:

    1.  Ensure all tanks and lines are thawed and clean. A potentially serious problem developed when the warm

    diesel was stored in an available upright tank that previously held water based drilling mud. The warm

    diesel melted a thin sheet of frozen mud lining the

    inside of the tank. This resulted in higher than norma

    CT pump pressures when a small volume of 11 ppg

    “diesel” was pumped down the CT during the freeze

     protect while coming out of the hole. This could have

     plugged a suction hose or caused triplex pump

     problems.

    2.  On larger programs such as this, 2 full sets of crewswould have allowed for fresh crews had lengthy

     problems developed during the squeeze.

    3.  A smaller trip tank with smaller volume barrelmarkers would have improved the accuracy of the

    fluids in and out management. The normal 40 Bb

    cement trip tank was not available at Alpine.

    4.  Continuous mixing operations are a convenienmethod to mix large volume jobs. However, there are

    fewer contingencies available during these “on-the

    fly” operations. Batch mixing allows a greater degree

    of quality control verification of all cement pumped

    into the well.

    The procedures and methods discussed in this paper appear

    to represent a viable technique for P&A or remedial squeeze

    work in long horizontal wells.

    Acknowledgements

    The authors thank the management of ConocoPhillips AlaskaInc., BP Alaska, and other Unit Owners for permission to

     publish this paper. This paper reflects the views of the

    authors, and does not necessarily reflect the views of the

    Colville River Unit, Greater Kuparuk Area, Prudhoe Bay Area

    or other Working Interests. The dedication of the on-site

     personnel to implement these procedures cannot be overstated

    and is greatly appreciated. The authors wish to specifically

    acknowledge the contributions of Perry Cline, Steve

    Doughten, Mike Burnett, Howard Gober, Cliff Crabtree, Chris

    Pierson, and Aras Worthington. A special thanks is given to

    Jack Kralick and Doug Cismoski for persevering in editing

    this paper and their technical input. The authors also

    acknowledge the contributions of the ConocoPhillips AlaskaWells Group, BP Alaska Wells Group, and Dowel

    Schlumberger.

    NomenclatureBbl = Barrel

    HP = High Pressure

     ppg = pounds per gallon

     psi = pounds (f) per square inch

    Pv = Plastic Viscosity in cP

    TD = Total Depth

    TVD = True Vertical Depth

    Ty = Yield Point in Pounds Force per 100 square feet

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    References1. Harrison, T. W. and Blount, C. G., “Coiled Tubing Cement

    Squeeze Technique at Prudhoe Bay,” paper SPE 15104, 56th California Regional Meeting of the SPE, Oakland, California, 2-4 April, 1986.

    2. Krause, R. E. and Reem, D. C., “New Coiled-Tubing UnitCementing Techniques at Prudhoe Developed to WithstandHigher Differential Pressure,” paper SPE 24052 presented at the

    1992 Western Regional Meeting, Bakersfield, March 30-April 1,1992.

    3. Gantt, L. L. and Smith, B. E., “Advancements in the CoiledTubing Cement Squeeze Process at Prudhoe Bay,” presented atthe 2nd  International Conference and Exhibition on Coiled

    Tubing Technology, Houston, Texas, 28-31 March, 1994.

    4. Bond, A. J., Blount, C. G., Davies, S. N., Keese, R. F.,

    Lai, Q. J., and Loveland, K. R., “Novel Approaches to

    Profile Modification in Horizontal Slotted Liners at

    Prudhoe Bay,” paper SPE 38832 presented at the 1997

    SPE Annual Technical Conference and Exhibition, San

    Antonio, Texas, 5-6 October, 1997.5. Bhalla, J., “Coiled Tubing Extended Reach Technology,” paper

    SPE 30404 presented at the SPE Offshore Europe Conference,

    Aberdeen, Scotland, 5-8 September, 1995.6. Blount, C., Crabtree, C., Kralick, J., Pierson, C., Rennie,

    S., Diller, G., and Mackenzie, G., “Inflatable CT

    Conveyed Selective Well Testing System for Logging

    Open Hole and Horizontal Wellbores: Development and

    Use,” paper SPE 81718 presented at the 2003 SPE/ICoTA

    Coiled Tubing Conference, Houston, Texas, 8-9 April,

    2003. 

    7. Blount, C. G., Brady, J. L., Fife, D. M., Gantt, L. L.,

    Huesser, J.M., and Hightower, C. M., “HCL/HF Acid-

    Resistant Cement Blend: Model Testing and Field

    Application,” paper SPE 19541 presented at the 1989 SPE

    Annual Technical Conference and Exhibition, San

    Antonio, Texas, 8-11 October, 1989. JPT February 1991, pages 226-248 

    SI Metric Conversion Factors Bbl x 1.590 E - 01 = m3 

    Ft x 3.048 E - 01 = m

    in. x 2.54 E + 00 = cm

    Lbf x 4.448 222 E + 00 = N

    Psi x 6.894 757 E - 03 = Mpa

    Tables

    Fann Readings

    (rpm)

    81 deg F 140 deg F

    300 36.0 74.0

    200. 26.0 53.0

    100 15.0 32.0

    60 11.0 21.030 7.0 12.0

    6 4.0 4.0

    3 3.0 3.0

    Cement Fann 35 reading (Bob 1 Spring 1)

    Figures

    laska North Slope 

    Figure 1: Map of Alpine development andsurrounding area on the North Slope of Alaska.

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    SPE 94039 7

    Figure 2: Drillsite 2 in-line pattern configuration. Subject Well B area is circled.

    Figure 3: Typical Alpine horizontal openhole completion.

      1  8

      3  1

     5

      3 6

      3 0

     4  3

     4 0

      3  7

     5 5

     1 6

      2  3

      1  2

      2 0

      9  1 0

      8

      1  3

      2  8

      2  2

      2  9

      1  9

     4 6

     4  8

     4  1

      3  8

      3 5 a

     4 5

     4 4

     5  3

     5  7

     5  8

     5  2

     5  1

     5 6

      8

    Alpine 3

    Alpine 1B

    Alpine 1

    42PB

    33A

    Neve 1

    23PB

    34PB

    50PB

    39PB

    35

    24PB

    32PB

    13PB

    Alpine 1A

      1 4

      1 5

      1  7

      2 4

      2 5

      2 6

      3  3  B

      3 4

      3  9

     4  2

     4  7

     4  9  5 0

      3  2

    9-5/8" Casing at 2,727' MD / 2,377' TVD

    Cemented to surface

    7" Production Casing at 9,444'MD / 6,824' SS

    4-1/2" SSSV at 1,796' MD / 1,697' TVD,

     

    16" Conductor to 114'

    GLM at 4,176' MD / 3,388' TVD

    GLM at 6,759' MD / 5,203' TVD

    GLM at 8,878' MD / 6,670' TVD

    Calculated

    TOC +/- 9,286' MD

    6,803' SS

    SSSV

    6-1/8" to TD at 13,977' MD / 6,841' SS

    4,533' openhole

      X  N

    X

    4-1/2" Tubing w/ Thermal Centralizers

    Between 3,250' - 6,250' MD

    X Nipple at 8,940' MD / 6,708' TVD

    4-½" x 7" Packer at 8,994' MD / 6,739' TVD

    XN Nipple at 9,070' MD / 6,780' TVD

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    8 SPE 94039

    Figure 4: Close-up of subject Well B between offset wells A and C; before P&A and after sidetrack 

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    SPE 94039 9

    Figure 5: Completion diagram of Well B prior to P&A and sidetrack.

    Figure 6: Plan view and section view of Well B prior to sidetrack.

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    Figure 7: Layout of major equipment. Due to seasonal road access, the drilling rig’s cement equipment had tobe used to perform the CT P&A. The rig-up required use of over 800’ of hardline.

    Tool Description Sketch Tool O/D Tool I/D Length

    Inches Inches Feet

    1.75" 1" 0.35

    1.75" Cold Roll Connector 

    1.75" 1" 1

    1.75" Dual Check Valve

    1.75" Spacer Pipe

    1.75" 1" 5

    1.75" Ball Drop Nozzle 1.75" 1" 0.5

    6.85  Figure 8: CT Bottom Hole Assembly. The BHA OD was the same as the CT OD to minimize the chance ofwellbore debris sticking the CT during the cement job.

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    SPE 94039 11

    Figure 9: Example of a combination cement/jet swirl ball-drop nozzle. The ball is pumped following cemendisplacement to land on seat blocking larger holes in nozzle and converts the nozzle to a jet swirl cleanoutnozzle. Note up/down swirl configurations in the nozzle to enhance cleanout efficiency.

    Figure 10: CT with combination Cement/Jet Swirl nozzle with ball on seat. Picture is downward toward top of CTin 7” casing showing swirl vortex while pumping biopolymer gel.

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    12 SPE 94039

    Figure 11: Vertical section of wellbore illustrating various positions of equipment, fluid interfaces, andcompletion overlaid on a graphically accurate representation of the inclination survey.

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    SPE 94039 13

    Hesitation Squeeze

    0

    500

    1000

    1500

    2000

    2500

    3000

    3500

            1        6      :        4        2      :        3        9

            1        6      :        5        2      :        3        9

            1        7      :        0        2      :        3        9

            1        7      :        1        2      :        3        9

            1        7      :        2        2      :        3        9

            1        7      :        3        2      :        3        9

            1        7      :        4        2      :        3        9

            1        7      :        5        2      :        3        9

            1        8      :        0        2      :        3        9

            1        8      :        1        2      :        3        8

            1        8      :        2        2      :        3        8

            1        8      :        3        2      :        3        8

            1        8      :        4        2      :        3        8

            1        8      :        5        2      :        3        8

            1        9      :        0        2      :        3        8

            1        9      :        1        2      :        3        8

            1        9      :        2        2      :        3        8

            1        9      :        3        2      :        3        8

            1        9      :        4        2      :        3        8

            1        9      :        5        2      :        3        7

            2        0      :        0        2      :        3        7

            2        0      :        1        2      :        3        7

            2        0      :        2        2      :        3        7

            2        0      :        3        2      :        3        7

            2        0      :        4        2      :        3        7

            2        0      :        5        2      :        3        7

            2        1      :        0        2      :        3        7

            2        1      :        1        2      :        3        7

            2        1      :        2        2      :        3        7

            2        1      :        3        2      :        3        7

            2        1      :        4        2      :        3        6

            2        1      :        5        2      :        3        6

            2        2      :        0        2      :        3        6

            2        2      :        1        2      :        3        6

            2        2      :        2        2      :        3        6

            2        2      :        3        2      :        3        6

    Time

       P  r  e  s  s  u  r  e   (   P   S   I   G   )

    010

    20

    30

    40

    50

    60

    70

    80

    90

    100

    110

    120

    130

    140

    150160

    170

    180

    190

    200

    210

    220

    230

       P  u  m  p  e   d   V  o   l  u  m  e   (   B   b   l  s   )

    WH Pressure psig

    CT Pressure

    Total Volume (Bbls)

    Squeeze Circulate Squeeze

    SqueezeSqueeze

    Reset

    MM Tot.

    RIH to Cleanout

     Figure 12: Graph of Well B hesitation squeeze. Areas marked where wellhead pressure was squeezed.Circulation took place between squeeze intervals: fluids were circulated to the choke to prevent freezing surfacelines. Fluids in and fluids out were carefully checked during circulation periods.

    Figure 13: Graph of various parameters during the execution of the P&A of Well B. Weight is on the right Y-axis.Density was adjusted to #/100 gallons for resolution. Hesitation squeeze interval is between 500 and 840 min.