CDF Silicon Detector - ssd-rd.web.cern.ch · Last fall the CDF experiment faced a crisis due to...

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CDF Silicon Detector Wire-Bond Failures Induced by Resonant Vibrations Reid Mumford Johns Hopkins University CDF Collaboration CDF Silicon Detector – p. 1/1

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Page 1: CDF Silicon Detector - ssd-rd.web.cern.ch · Last fall the CDF experiment faced a crisis due to internal unrecoverable failures on the silicon detector The source of the problem has

CDF Silicon DetectorWire-Bond Failures Induced by Resonant

Vibrations

Reid Mumford

Johns Hopkins University

CDF Collaboration

CDF Silicon Detector – p. 1/18

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Component FailuresAfter commissioning, Several failures occurred under anomalous trigger conditions.

Two types of failures.

DVDD Jumper - loss of z information from detector

DOIM - loss of all information from the module

Anomalous trigger conditions

“Torture Tests”: tests to explore dead-time at high rate.

high occupancy mode in SVX3 chips

Both trigger conditions cause the system to be read-out at a fixed rate

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DVDD Jumpers

Layers of SVX are double-sided w/ bonds connecting z to

hybrids

Bonds supply power and move data from z channels during readout.

Bonds are in a plane orthogonal to the magnetic field in CDF.

CDF Silicon Detector – p. 3/18

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DOIMsD¯

ense O¯

ptical I¯nterface M

¯odule

Laser diode package that moves data from detector to VME crates in parallel (9-bit bus).

Power connection wire-bonds are in a plane parallel to magnetic field.

Vertical components however are perpendicular to magnetic field.

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The CDF Detector

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DOIM and Jumper Currents

DVDD Jumpers have

��

up to 150mA

� �� � occurs when readout shifts from

to z chips

DOIMs have

��

of no more than

40-50mA (top trace)

Current swings come from switching be-

tween laser diode and dummy loads

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Bond Specifications

� � � � in length

� �� � � in diameter

Composition: 99% Al 1% Si

Different profiles for DOIM,

and

z-side bonds

Not encapsulated

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Lorentz Forces

Ma

gn

etic

Fie

ld

Current

CurrentForceForce

DVDD DOIM

� ������ �� � � � � � ��� � � � �� � � � � � � � � � �� � � � �� ���

CDF Silicon Detector – p. 8/18

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ResonanceResonance enhances fatigue due to Lorentz forces

Visually scanned for resonance in bonds in a 1.4T test magnet

Resonances observed with driving currents of 10mA - 150mA.

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Characteristic Frequency

Initial calculations for 2mm SiAl bond predicted 15kHz

Many bonds tested w/ 40mA sinusoidal driving current (push and pull)

Fundamental frequency in agreement with calculations

1st harmonic was also observed

Typically 1kHz resonant width

Arbitrary Measurement Number0 5 10 15 20 25 30 35

Dri

vin

g F

req

uen

cy (

kHz)

0

5

10

15

20

25

30

35

40

45

50

Resonant Frequencies w/ SineHigh Resonance

Low Resonance

Resonant Frequencies w/ Sine

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More Realistic CurrentsBonds driven with a more realistic current pulse (100mA,

� � � �

) exhibit more resonances.

Resonant frequency

can be excited with pulses at

,

� � �

,

� � �

, etc

Width of resonance is between 1 and 200Hz.

Differently shaped bonds imply different frequencies.

Arbitrary Measurement Number0 20 40 60 80 100 120

Dri

vin

g F

req

uen

cy (

kHz)

0

5

10

15

20

25

30

35

40

Resonant Frequencies w/ PulseResonant Frequencies w/ Pulse

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Foot Fatigue

On the time-scale of minutes, a resonating bond will fail

At 10kHz this is about

�� � � � � �

cycles.

Breakage occurs at the bond’s foot

Breakage is due to stress fracture that forms during vibration

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Fatigue vs. Pulling

Failure due to fatigue looks very different from a pulled bond

Similar to a failure mechanism described in a paper by Raymond T. Fitzsimmons and C. E.

Miller (IEEE Transaction on Components, Hybrids and Manufacturing Technology, Vol. 14,

No. 4, December 1991)

Fatigue Failure Pull Failure

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Fast Video Analysis

A camera with a 40500Hz shutter rate was used to record the motion of bonds.

Single frames have been digitized and a quantitative analysis performed

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Excitation and Damping

Bonds were excited w/ a limited number of

� � � �

,

�� � �

current pulses

The amplitude was measured as a function of the number of pulses

The damping ratio was also measured from the decay of the free oscillations to be roughly

��� � �

Free Oscillation

� � � � �

0 200 400 600 800 1000

0

0.2

0.4

0.6

0.8

1

1.2

1.4

1.6

1.8 / ndf 2χ 26.98 / 70

offset 0.01843± 0.03918

amplitude 0.1283± 3.586

damping 0.000423± -0.007632

phase 0.06057± -0.5621

40 kicks: Amp vs Frame / ndf 2χ 26.98 / 70

offset 0.01843± 0.03918

amplitude 0.1283± 3.586

damping 0.000423± -0.007632

phase 0.06057± -0.5621

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Mitigation

3-4 current pulses at the bond’s characteristic frequency are enough to excite motion.

Efforts have been made to reduce Lorentz forces.

Reduce current swings by changing SVX3 chip settings

Reduce duration by lowering noise occupancy

Minimize time at resonance; trigger inhibit on resonances detected directly with FFT.

Banned “Torture Tests”

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Encapsulation

The foot of the bond was encapsulated w/ Sylgard 186 Silicon Elastomer

Encapsulant thickness is no more than

� � � �

Amplitude of resonant vibrations was reduced by more than an order of magnitude

Unable to break encapsulated bonds even when driving for several hours with large currents

( � � � � � �

)

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ConclusionLast fall the CDF experiment faced a crisis due to internal unrecoverable

failures on the silicon detector

The source of the problem has been understood to be a simple physics

mechanism

The understanding of this problem should be applied to the construction of

future silicon detectors

Counter measures have been studied and applied to the CDF experiment.

Since the implementation, no other failures have occurred

Resonance cannot be avoided but the accumulated stress and fatigue on

bonds has been minimized by

Reducing the strength of the Lorentz force

Reducing the time spent at resonance

An encapsulation method for future applications has been successfully

tested on a small number of samplesCDF Silicon Detector – p. 18/18