Case Study of Reconditioning of Air Preheater Gear Box

download Case Study of Reconditioning of Air Preheater Gear Box

of 9

Transcript of Case Study of Reconditioning of Air Preheater Gear Box

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    1/9

    CASE STUDY OF RECONDITIONING OF AIRPREHEATER GEAR BOX

    AtDr SHYAMA PRASAD MUKHARJEE THERMAL

    POWER STATIONSubmitted by

    NARENDRA PATELEASE KORBA

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    2/9

    DR SHYAMA PRASAD MUKHARJEE THERMALPOWER STATION AT A GLANCE

    Dr Shyama Prasad Mukharjee thermal power station is operated by Chhattisgarh

    state power Generation Company limited.

    Dr Shyama Prasad Mukharjee thermal power station, Korba is situated in the heart

    of the city. It is built in the place where the first power plant of Korba was built in 1958.

    It has a installed capacity of 5oo megawatts consisting of two coal fired Bhel boilers of 250

    megawatts each. The first unit was commissioned on 30thMarch 2007 and the second unit

    was commissioned on December 11 of the same year.

    Dr Shyama Prasad Mukharjee thermal power station has always welcomed new

    ideas and concepts for improvising its efficiency. Reformation of process is a regular feature

    at KTPS. The plants officials are always ready to adopt newer technologies and believe in

    continual improvement and setting newer bench marks. EWAC Association goes hand in

    hand from last 3 decades. EWAC services are regarded very high at Dr Shyama Prasad

    Mukharjee thermal power station. Various technologies have been offered to the plant

    which has been very well accepted by the plant

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    3/9

    ABOUT THE JOB

    The gear box is situated in the primary air fan area to reduce the rpm of electrical

    motor to that required for fan. During the changing of bearing the bearing sitting area of

    the gear box cracked due to miss handling.

    (crack of air preheater gear box)

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    4/9

    Application detailsNature of problem- crack developed due to improper handling

    Base metal- cast iron

    Recommended electrode-

    Eutectrode 27 and Xuper 2240

    Reason for recommending these electrodes

    The gear box contains oil inside for lubrication of gears. Since the base metal is cast iron, it

    soaks oil so a buffering layer of eutectrode 27 is required because it can seal the impurities

    and the bonding between the base metal and required joining electrode should be perfect.

    Xuper 2240 has a nodular cast iron deposit which provides improved crack resistivity.

    It is highly machinable.

    It provides a tensile strength of 57000 Psi which ensures a high safety of margin.

    The weldability of the electrode is excellent.

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    5/9

    STEP BY STEP WELDING PROCEDURE1st step

    The cracked metal part is removed by grinding. The grinding is done till the complete

    crack is removed.

    2nd stepDye penetration test is done to check that the crack is removed completely.

    3rdstepThe preheating is done with oxy- acetylene flame to 200 degree Celsius and welding

    is started.

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    6/9

    A single layer of eutectrode 27 is deposited to seal the contaminants inside. Due to

    use of eutectrode 27 the next phase of welding become easier because it sealed all the oil and

    impurities.

    4thstepWelding current is set to as low as possible to burn the electrode to preserve the

    quality of weld deposit and to prevent over heating of electrode.

    Short stringer beads of Xuper 2240 are welded and after welding the bead peening is

    done with a ballpin hammer to remove the internal stress and flux is removed with the help

    of a chipping hammer and with the help of stainless steel wire brush. This process is done

    till a complete layer is overlaid and then the weld overlay is slightly grinded to remove anyflux residues. Then temp of job is checked and preheating is done once again to bring the job

    temp to again 200 degree Celsius. The process is continued till the total area is completly

    buildup to required thickness.

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    7/9

    Final view of job after welding

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    8/9

  • 8/12/2019 Case Study of Reconditioning of Air Preheater Gear Box

    9/9

    For Further Information Please Contact

    NARENDRA PATEL

    EASE KORBA

    Ph-07509572413

    Mail- [email protected]

    The only way to do great work is to love what you do