Best Practices In Energy Efficiency in Sponge...

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Best Practices In Energy Efficiency in Sponge Iron Nalwa Steel and Power Ltd. 1

Transcript of Best Practices In Energy Efficiency in Sponge...

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Best Practices In Energy Efficiency in Sponge Iron

Nalwa Steel and Power Ltd.

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Nalwa Steel and Power Limited is an Integrated Steel Plant set up by great visionary Late Shri O. P. Jindal. It works under the umbrella of Jindal Steel & Power Limited.

Introduction

Date:- 04-03-2016 2 Presented By:- Vishal Vashishtha & Debashis Roy

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The plant is equipped with DRI Plant, Coal washery, Power plant, Steel Melting Shop, Oxygen Plant, Rolling Mill, and P.G. Plant etc. which make it fully integrated steel plant having capacity to produce 0.25 MTPA finished product. The major product of Nalwa steel and power limited are Sponge Iron, MS Billets & TMT Rebar.

Nalwa Steel and Power Limited is committed to adopt Energy Efficient practices in all its verticals. In this regard, Company has implemented ISO 50001:2011 and aligning the same with organization's business objectives and goals

1. DRI : 198000 MT/Year

2. SMS : 160000 MT/Year

3. WRM : 250000 MT/Year

4. CPP : 3X8 MW

Introduction: Continued…

Date:- 04-03-2016 3 Presented By:- Vishal Vashishtha & Debashis Roy

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Energy Management Policy

Date:- 04-03-2016 4 Presented By:- Vishal Vashishtha & Debashis Roy

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Process flow diagram of NSPL

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Particulars UOM Base Year FY 2014-15

Production MT 161917.67 186355.00

Thermal SEC Gcal/MT 7.5 6.2

Electrical SEC KWH/MT 90.56 83.86

Utilization % 81.78 94.12

90.56

83.86

80.00

82.00

84.00

86.00

88.00

90.00

92.00

Base Year FY 2014-15

7.52

6.21

0.00

2.00

4.00

6.00

8.00

Base Year FY 2014-15

DRI Performance:

Baseline Vs. FY-2014-15

Thermal SEC Electrical SEC

Date:- 04-03-2016 6 Presented By:- Vishal Vashishtha & Debashis Roy

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Productivity = Sp. Energy Consumption

1. Installation of Iron Ore Wet Screening Plant

2. Installation of Deshelar System

3. Use of Pellet

4. Segregation of Injection Coal Size

5. Use of Imported Coal

Project Implemented/Process Change Activities

Date:- 04-03-2016 7 Presented By:- Vishal Vashishtha & Debashis Roy

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1. Installation of Iron Ore Wet Screening Plant

IRON ORE WET SCREENING PLANT UOM BEFORE AFTER VARIANCE

IRON ORE FACTOR REDUCES @ 62.5FeT MT 1.84 1.76 0.08

COAL FACTOR REDUCES MT 1.6 1.54 0.06

TOTAL INVESTMENT COST 5Cr.

Date:- 04-03-2016 8 Presented By:- Vishal Vashishtha & Debashis Roy

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Benefits of Deshelar

System:-

•Improves Quality of Coal

•Increases Efficiency of

Washery

•Increases Production of

Washery

•Generated by-product is

used in Power Plant

After Crushing, Coal is fed in Deshelar Chamber. Magnetic Powder is used as mix in the charged water to change the density of water. As density changes, the heavier particles settle down at the base of chamber and light articles floats on the charged water due to less density. Heavier Particles are dragged out from the settling chamber with the help of drag chain making the concentration heavier for the coal. It helps to improve quality of coal and increase the efficiency of coal Washery. The shale removed is by-product.

2. Installation of Deshelar System

Date:- 04-03-2016 9 Presented By:- Vishal Vashishtha & Debashis Roy

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BENEFITS UOM IRON ORE PELLET VARIANCE

YIELD IMPROVEMENT % 56.80% 67.57% 10.77%

PRODUCTION FACTOR MT 1.76 1.5 0.26

REDUCTION IN SOLID FUEL CONSUMPTION

MT 1.54MT/MT 1.4MT/MT 0.14MT/MT

3. Use of Pellet

Pellets are balls of iron ore used in the DRI Plant. They are made with technology that uses the powder that is generated during the ore extraction process, once considered waste. The process of pelletization enables converting Iron Ore Fines into “Uniformed Sized Iron Ore Pellets

Date:- 04-03-2016 10 Presented By:- Vishal Vashishtha & Debashis Roy

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Benefits of Segregation:-

•Production Efficiency Improved

•Coal Consumption reduced

•Coal Utilisation Increased

•FC in Ash Char Reduced

4-10mm 0-4 mm

Date:- 04-03-2016 11 Presented By:- Vishal Vashishtha & Debashis Roy

4. Segregation of Injection Coal Size

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Benefits of Imported Coal Usage:-

• Coal Factor Reduced

• Specific Air Requirement Reduced

• Approx 30% Load Reduced on FD Fan & ID Fan

• Dolachar Generation Reduced by 50%, resulting

reduction in logistic expenses

• Kiln Main Drive & Cooler Main Drive RPM Reduced by

50%, Resulting reduction in Power Consumption

5. Use of Imported Coal in DRI

Date:- 04-03-2016 12 Presented By:- Vishal Vashishtha & Debashis Roy

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1. Replacement of 70 Watt HPSV Lights with 12 Watt LED

Lights

2. Use of Transparent Sheets in Shed

3. Astronomical Timer for Lighting

4. 40 % DRI Equipments are Equipped with VVVF Drives

5. Erection & Commissioning of De-dusting System

6. SAP Based Preventive Maintenance Plan for Effective &

Improved Maintenance of Equipments

7. Monthly Review of Maintenance Statistics

8. Replacement of LDO Firing with FO Firing

Implementation of Small but Effective

Techniques in DRI

Date:- 04-03-2016 13 Presented By:- Vishal Vashishtha & Debashis Roy

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Date:- 04-03-2016 14 Presented By:- Vishal Vashishtha & Debashis Roy

ISO 50001:2011 Certificate

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Date:- 04-03-2016 15 Presented By:- Vishal Vashishtha & Debashis Roy

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Thank You

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Presented By:- Vishal Vashishtha & Debashis Roy, 04-03-2016