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Transcript of ACHIEVING UNIFORM COMBUSTION USING REAL …ferco.com/Files/MP220-Power-Gen2005.pdf · achieving...
MP220
ACHIEVING UNIFORM COMBUSTION USING REAL TIME COAL FLOW AND
GASEOUS EMISSIONS MEASUREMENT EQUIPMENT
Frederick P. Haumesser, P.E.Richard E. Thompson, P.E.Fossil Energy Research Corp
Douglas L. EakleAllegheny Energy Supply
MP220
EVIDENCE OF NON-UNIFORM COMBUSTION
Symptoms Of Non-Uniform Combustion Often Include:
• Uneven Excess Oxygen Readings (Side-To-Side)• Inconsistent Flyash Loss On Ignition (LOI) Values
And Localized High Carbon Monoxide (CO)• Uneven Waterwall Deposition Patterns• Side-To-Side O2, CO And NOx Data Change With
Firing Pattern • Uneven Flue Gas And Steam Temperatures
MP220
WHY BALANCE THE STEAM GENERATOR’S COMBUSTION?
Non-Uniform Combustion Can Lead To:• Poor Equipment Performance• Increased Flyash Loss On Ignition (LOI) And
Increased Carbon Monoxide (CO) Resulting In Lower Boiler Efficiency
• Waterwall Corrosion And Fouling In The Convective Section
• Elevated NOx Emissions Caused By Air Rich Burners
• Elevated CO Emissions Caused by Fuel Rich Burners
MP220
STEP ONE:
Address Pipe-to-Pipe Fuel Flow Distributions
MP220
MEASURING AND OPTIMIZING COMBUSTION –COAL FLOW DISTRIBUTION TESTING
• Extractive Sampling (RotorProbeTM ) Versus Real Time Coal Flow Measurements
• RotorProbeTM :– ISO Approved– Performed Well Under Most Test Conditions In FERCo’s
Evaluations And At The EPRI Coal Flow Test Loop– Sequential, “Snapshot” Testing
• MIC:– Real-Time Coal Flow Distributions – Data Logged Constantly For All Burner Lines Of A Pulverizer– Field Testing Confirmed Accuracy With RotorProbeTM Results– Data From The EPRI Test Loop Indicated Very Good
Agreement
MP220
MIC REAL TIME COAL FLOW DISTRIBUTION TESTING
• Two (Vertical Piping) or Three (Horizontal Piping) Sensors Required Per Burner Line
• Attach To Burner Line Using Existing Sample Ports (Valves)
• Data Logged And Displayed Simultaneously For All Burner Lines
• Distribution Changes Due To Operating Conditions, Such As Feedrate, Or To Equipment Settings, Such As Adjustable Orifices, Can Be Seen Immediately
MP220
TYPICAL MIC SENSOR SET-UP
MP220
STEP TWO:
Address Flue Gas Distributions for O2, CO and NOx (Side-to-Side)
MP220
MEASURING AND OPTIMIZING COMBUSTION –GASEOUS EMISSIONS DISTRIBUTION TESTING
• Traditional (Point-To-Point) or Real Time Using the FERCo Multipoint Combustion Diagnostic Analyzer (MCDA)
• Traditional Sampling:– Perform Flue Gas Analysis Sequentially, Requiring
Approximately 3-5 Minutes Per Point (24 Points = 72-90 Minutes)
– Boiler May Change, Thus Initial Data May Not Be Representative
MP220
• MCDA:– Perform Flue Gas Sampling Of Points In Parallel; 12
Points Can Be Sampled Simultaneously; 24 Points = 10-13 Minutes
– Data Logged Automatically Every 10-20 Seconds And Can Be Replayed For Additional Analyses
– Data Can Be Monitored In Real Time To See The Cause And Effect Relationships Of Operating Parameter And Equipment Changes, Such As Mill Loadings Or Air Register Settings
– MCDA Data Compared With Traditional CEM Instruments For Increased Confidence
MEASURING AND OPTIMIZING COMBUSTION –GASEOUS EMISSIONS DISTRIBUTION TESTING (Cont’d)
MP220
TYPICAL MULTIPOINT NO, O2, CO ANALYZER (MCDA) INSTALLATION
MP220
CASE HISTORY:
Combustion Diagnostics Using Real Time Instrumentation
MP220
UNIT DESCRIPTION
• Allegheny Energy Supply’s Harrison Unit 2• 640 MWg• Foster-Wheeler Supercritical Boiler• Opposed Wall Fired• Six D9 Ball Tube Mills With Four Burner
Lines Per Mill• Firing Pattern: Three Elevations With Four
Burners Across For Both Walls
MP220
NON-UNIFORM COMBUSTION SYMPTOMS ON HARRISON UNIT 2
• High CO And LOI On One Side Only• Increased LOI Forced Operators To
Increase Excess Air• Higher Excess Air And High LOI Caused
Decreased Electrostatic Precipitator (ESP) Performance
• The Increased Ash In The Flue Gas Leaving The ESP Was Eroding An Induced Draft Fan
MP220
DIAGNOSTIC METHODOLOGY
• Perform Fuel Distribution Testing• Evaluate PC Samples For Fineness• Measure Concentrations of O2, CO and
NOx At Economizer Exit• Establish Cause And Effect Relationships
By Varying O2 Level, Firing Pattern, Mill Loading And Burner Register Settings
• Program Completed Within Seven Test Days
MP220
HARRISON 2E MILL COAL FLOW DISTRIBUTION DATA
• F-W BALL TUBE MILLS WITH 4 – 15¼” BURNER LINES
ROTORPROBE™ RECOVERED MASSES: Pipe 1 Pipe 2 Pipe 3 Pipe 4 (Four Minute Collection Period) Run 1 235gm 230gm 93gm 117gm Run 2 186gm 217gm 125gm 221gm Run 3 277gm 208gm 71gm 176gm CALCULATED % DEVIATION PIPE TO PIPE 20.0% 24.2% -39.4% -4.8%
• MIC % DEVIATIONS PIPE TO PIPE 20.8% 42.5% -42.0 -21.3% (MIC Data Recorded Over 4 ½ Hours)
MP220
MIC PLOT OF COAL FLOW DISTRIBUTIONS OVER TIME FOR 2E PULVERIZER
Mill 2E Burner Line Coal Flow Distributions
0
5
10
15
20
25
30
35
40
45
50
9:00
:44
AM
9:06
:30
AM
9:12
:15
AM
9:18
:01
AM
9:23
:47
AM
9:29
:32
AM
9:35
:18
AM
9:41
:03
AM
9:46
:49
AM
9:52
:35
AM
9:58
:20
AM
10:0
4:06
AM
10:0
9:51
AM
10:1
5:37
AM
10:2
1:23
AM
10:2
7:08
AM
10:3
2:54
AM
10:3
8:39
AM
10:4
4:25
AM
10:5
0:11
AM
10:5
5:56
AM
11:0
1:42
AM
11:0
7:28
AM
11:1
3:13
AM
11:1
8:59
AM
11:2
4:44
AM
11:3
0:30
AM
11:3
6:16
AM
11:4
2:01
AM
11:4
7:47
AM
11:5
3:33
AM
11:5
9:18
AM
12:0
5:04
PM
12:1
0:50
PM
12:1
6:35
PM
12:2
2:21
PM
12:2
8:06
PM
12:3
3:52
PM
12:3
9:38
PM
12:4
5:23
PM
12:5
1:09
PM
12:5
6:55
PM
1:02
:40
PM
1:08
:26
PM
1:14
:12
PM
1:19
:57
PM
1:25
:43
PM
Time
Perc
ent C
oal F
low
Dis
trib
utio
n
Pipe 1 Pipe 2 Pipe 3 Pipe 4
MP220
THE EFFECT OF 2E MILL ON COMBUSTION UNIFORMITY WITH ALL MILLS IN-SERVICE
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
NO corrected 297 ppmc ( 0.405 lb/MBtu )
0
2
4
6
8
10
12
Top
D
epth
, ft
B
otto
m
299
296
299
303
316
315
321
288
287
281
285
287
283
282
293
290
291
286
275
296
285
251
262
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
CO corrected 194 ppmc
0
2
4
6
8
10
12
Bot
tom
D
epth
, ft
To
p
58
71
52
31
7
5
3
26
16
22
20
32
23
57
82
17
161
412
958
232
475
1333
1400
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
O2 4.14%
0
2
4
6
8
10
12
Bot
tom
D
epth
, ft
To
p
3.7
3.3
3.6
3.8
4.2
4.3
4.0
4.2
4.2
4.3
4.1
4.4
4.1
4.1
4.0
4.2
4.2
4.0
3.5
4.5
4.2
3.1
3.1
MP220
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
NO corrected 316 ppmc ( 0.431 lb/MBtu )
0
2
4
6
8
10
12
Top
D
epth
, ft
B
otto
m
297
299
300
308
315
321
317
308
303
305
311
306
301
301
317
308
317
311
306
318
308
286
301
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
CO corrected 4 ppmc
0
2
4
6
8
10
12
Bot
tom
D
epth
, ft
To
p
16
21
20
18
3
2
0
4
3
-1
-1
1
3
0
1
2
3
3
6
2
5
6
8
0 5 10 15 20 25 30 35 40 45 50 55 60A side Duct Width, ft (Gas Flow Out of Page) B side
O2 5.25% E MOOS
0
2
4
6
8
10
12
Botto
m
Dep
th, f
t
Top
3.7
3.4
3.9
4.1
4.6
5.2
4.3
5.6
5.7
5.9
5.6
5.5
5.0
5.1
5.2
5.0
5.3
5.3
5.2
5.3
5.3
4.5
5.0
THE EFFECT OF 2E MILL ON COMBUSTION UNIFORMITY WITH 2E MILL OUT OF SERVICE
MP220
COMBUSTION IMPROVEMENTS
• CO Was Reduced From 194 ppmc To 4 ppmc
• O2 Increased From 4.14% To 5.25% (Dry Basis)
• NOx Increased From 0.405 To 0.413 lb/MBtu• Flyash LOI Reduced From 6.0% to 3.2%• Improvements Realized With No Changes In
Fuel Flow, Total Airflow, Steam Flow Or Any Burner Settings
The Results Of Removing 2E Mill Were:
MP220
COMBUSTION IMPROVEMENTS
• Additional Tuning Reduced NOxEmissions From 0.413 lb/MBtu To 0.372 lb/MBtu With Minimal Impact On CO (4ppmc to 90ppmc) At A Reduced Excess Oxygen Level (5.3% to 3.7%)
• ESP Performance Restored To Expected levels
• 2E Mill Fineness Was Found To Be 98.15% Passing 50 Mesh And 74.47% Passing 200 Mesh
The Results Of Removing 2E Mill Were:
MP220
CONCLUSIONS
THE KEY POINTS OF THIS CASE HISTORY ARE:1. The Unsteadiness Of The Combustion Could Easily Be
Misinterpreted By Conventional, “Snapshot-Style” Extractive Coal Flow Sampling.
2. Real Time Coal Flow And Emissions Sampling Allows A Much Quicker And More Accurate Analysis Of Combustion Variability.
3. Real Time Pulverizer Fuel Distribution Data Can Be Monitored Over Time And Compared To The Unit’s DCS Data For Impact-Based Analysis Of Combustion, Emissions And Efficiency.
4. Real Time Gaseous Emissions Monitoring Allows The Effects Of System Changes To Be Readily Evaluated In Terms Of The Unit’s Combustion, Emissions And Efficiency.
MP220
CONCLUSIONS (Continued)
5. The Performance Of Only One Pulverizer Can Have A Very Pronounced Impact On Combustion Uniformity And Equipment Performance.
6. The Combustion Impacts Were Reducing Unit Availability And Key Equipment Life.
7. These Combustion Impacts Were Quickly And Accurately Identified Using The FERCo Proprietary Real Time Combustion Diagnostic Technologies.
8. These Same Diagnostic Technologies Were Used To Make Corrections To Key Operating Parameters, Which Were Proven To Improve The Unit’s Combustion And Reduce The Associated Impacts On Key Equipment Performance.
MP220
ACKNOWLEDGEMENTS
• Doug Eakle And The Entire Staff At The Harrison Generating Station